N104LP

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CHEVRON USA PRODUCTION COMPANY (AC2A)Operator2012-03-12 – 2012-03-12Operator named in NTSB report
Chevron USA IncOperator2012-03-12 – 2012-03-12Operator named in NTSB report

Accident & incident history

Acc · 2012-03-12 Operator named in NTSB report
BELL 206L-3 None injury Part 91Chevron USA Inc
Source: NTSB case CEN12CA191

Maintenance disclosures

B · 2011-10-07 Matched by certificate designator
ATA 2120

BEFORE TAKEOFF, TURNED THE DEFOG VENT MOTOR ON FOR VENTILATION. AFTER TAKEOFF, CLOSED THE CABIN VENT. MIDWAY THROUGH CLOSING, SPARKS AND SMOKE COULD BE SEEN IN THE NOSE NEAR THE DEFOG VENT MOTOR. DEFOG VENT MOTOR CIRCUIT BREAKER TRIPPED AND SMOKE AND SPARKS STOPPED. FOUND THAT VENT DOOR CABLE CONTACTED THE FAN WHEN CLOSED, INSPECTED FAN MOTOR, FOUND SERVICEABLE, REPOSITIONED AND RETURNED TO SERVICE.

Source: SDR AC2A4LP10072011 · FAA SDRS
R J · 2006-07-21 Matched by certificate designator
ATA 7230

HEARD A LOUD POP FOLLOWED BY YAWING AND FLUCTUATIONS IN INDICATED TORQUE. PILOT IMMEDIATELY LOWERED THE COLLECTIVE MAINTAINED AIRSPEED, AND CROSSCHECHECKED THE INSTRUMENTS.I PILOT INITIATED A TURN TO LAND BACK AT SP 58D. AFTER LANDING THE PASSENGERS GOT OUT TO PROCEED A VISUAL INSPECTION. THE PASSENGERS CONFIRMED THERE WAS NO APPARENT VISUAL PROBLEMS WITH THE EXTERIOR OF THE AIRCRAFT. I DECIDED TO TEST RUN THE AIRCRAFT OVER THE HELIPORT FOR AIRWORTHY STATUS. ALL ENGINE AND FLIGHT INSTRUMENTS INDICATED NORMAL AND THE AIRCRAFT HAD NO ADVERSE FLIGHT CHARACTERISTICS. THE POLIT PROCEEDED TO CONTINUE FLIGHT TO SP 77C AND WD 109 AND BACK TO SP78B. THERE WERE NO OTHER ABNORMAL OCCURRENCES AFTER THAT INCIDENT.

Source: SDR AC2A110424 · FAA SDRS
W · 1998-07-30 Unresolved
ATA 5302

DURING 100-HOUR INSPECTION, FOUND UPPER LEFT TAILBOOM ATTACH FITTING CRACKED. ALSO, FOUND LEFT FUSELAGE AFT LONGERON CRACKED. LONGERON PIN 206-031-329-037. ON REMOVAL, REPAIR, FITTING HAD A .020 INCH GAP BETWEEN LONGERON AND FITTING CREATING A LOADED CONDITION WHEN RIVETED AT FACTORY.

Source: SDR 98ZZZX3155 · FAA SDRS