N110AX

BEECH 1900C · 1990 · Valid Registration

Registered owner: ALASKA CENTRAL EXPRESS INC, AK (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ALASKA CENTRAL EXPRESS INC (YADA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2024-06-03 Matched by certificate designator
ATA 3233

WHILE PERFORMING AD 2009-23-01 (E)(3) NDT INSPECTION, INDICATION OF CRACKING WAS IDENTIFIED IN THE END CAP – SEE ATTACHED NDT REPORT. THIS INSPECTION WAS PERFORMED ON UC-93 AND THE ACTUATOR HAD 1015 CYCLES SINCE LAST INSPECTION. NO CRACKS WERE VISUALLY VISIBLE AND NO LEAKS WERE DETECTED.

Source: SDR YADA202406040301 · FAA SDRS
B · 2021-12-22 Matched by certificate designator
ATA 3397

STRONG SMELL OF SOMETHING BURNING SUB PANEL LIGHTS FLICKERING THEN COMPLETELY SHUT OFF. FOUND EEL PANEL A321 114-384007-15 SHORTING INTERNALLY.

Source: SDR YADA20211223201 · FAA SDRS
O · 2019-12-18 Matched by certificate designator
ATA 3243

CAPT AND FO LEFT BRAKE PEDAL UNRESPONSIVE.

Source: SDR YADA20191223001 · FAA SDRS
O · 2018-09-24 Matched by certificate designator
ATA 3414

PILOT REPORTED THAT THE RIGHT HAND (CO-PILOT'S) AIRSPEED INDICATOR WAS INTERMITTENT. AIRCRAFT RETURNED BACK TO ANCHORAGE FOR AN UNSCHEDULED LANDING, NO ISSUES WITH LANDING. MAINTENANCE PERSONAL REMOVED AND REPLACED THE RIGHT HAND (CO-PILOT'S) AIRSPEED INDICATOR, SYSTEM OPERATIONAL CHECK SUCCESSFUL, AIRCRAFT RETURNED TO SERVICE.

Source: SDR YADA201809254001 · FAA SDRS
Y · 2018-05-18 Matched by certificate designator
ATA 7321

PILOT REPORTED WHILE TAXIING THE RIGHT HAND ENGINE HAD A HUNG START WHILE USING BATTERY POWER TO START THE ENGINE AND THAT THE ENGINE FAILED DURING THE TAXI, PILOT RETURNED TO HOME STATION. MAINTENANCE IS CURRENTLY TROUBLESHOOTING THE ISSUE BUT HAS FOUND THAT THE FUEL CONTROL UNIT IS THE REASON AND IS AWAITING POST ENGINE RUNS FOR OPERATIONAL CHECKS. REMOVED FUEL CONTROL TEST/TEARDOWN DISCLOSED CDP BELLOWS DISTORTED (STRETCHED) CAUSING LOW FUEL SCHEDULING.

Source: SDR YADA20180518001 · FAA SDRS
B · 2017-10-20 Matched by certificate designator
ATA 2210

ON ENGINE SHUTDOWN, THE PILOT NOTICED AN ELECTRICAL ODOR, ACCOMPANIED WITH SMOKE COMING FROM THE CENTER CONSOLE AUTO-PILOT CONTROL HEAD. MAINTENANCE CONFIRMED THE SMOKE WAS FROM AUTO-PILOT CONTROL HEAD BOX, AND REMOVED THE COMPONENT.

Source: SDR YADA20171020001 · FAA SDRS
O · 2017-03-20 Matched by certificate designator
ATA 5310

AIR STAIRS DOOR FRAME CRACKED ALONG BOTTOM AFT SECTION.

Source: SDR YADA20170320001 · FAA SDRS
O · 2016-09-17 Matched by certificate designator
ATA 3260

NOSE GEAR DOWNLOCK SWITCH FAILED FOR WATER INTRUSION.

Source: SDR YADA20160917001 · FAA SDRS
N · 2016-09-01 Matched by certificate designator
ATA 3260

RED HANDLE LIGHT ON, MAINS DOWN AND LOCKED NO NOSE GEAR GREEN LIGHT. GEAR WAS MANUALLY PUMPED DOWN TO GET 3 GREEN DOWN AND LOCKED LIGHTS. NOSE GEAR DOWN LOCK SWITCH RERIGGED.

Source: SDR YADA20160901001 · FAA SDRS
B · 2015-04-10 Matched by certificate designator
ATA 2460

AFTER TAKEOFF, CREW REPORTED SEEING & SMELLING ELEC SMOKE FROM BEHIND THE FUEL QTY PANEL. THE CREW DEPLOYED OXYGEN MASKS & MADE AN UNEVENTFUL EMER LANDING AT THE AIRPORT OF ORIGIN. THE CREW REPORTED THE SMOKE & ODOR HAD DISSIPATED UPON LANDING. NO SYS FAULTS OR FAILURES WERE OBSERVED. IDENTIFIED & CORRECTED CONTACT BETWEEN A POWER CABLE TERMINALS & AIRFRAME STRUCTURE BEHIND THE HINGED FUEL QTY PANEL & RETURNED THE ACFT TO SERVICE.

Source: SDR YADA20150410001 · FAA SDRS