N11107

EMBRAER EMB-145XR · 2002 · Valid Registration

Registered owner: UNITED AIRLINES INC, IL (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2022-03-04 Matched by certificate designator
ATA 3350

SERVICE DOOR EMERGENCY LIGHT INOPERATIVE. REMOVED AND REPLACED SERVICE DOOR EMERGENCY LIGHT ASSEMBLY. OPS CHECK FAIL. UPON FURTHER INVESTIGATION FOUND BROKEN SPLICE IN WIRE BUNDLE ON DOOR HINGE. REPAIRED SPLICE. OPS CHECK SAT.

Source: SDR JJBA20220304004 · FAA SDRS
O · 2022-03-04 Matched by certificate designator
ATA 3350

LH EXTERNAL EMERGENCY WING FAIRING LIGHT FOUND TO BE DIM. REMOVED AND REPLACED LH EXTERNAL EMERGENCY WING FAIRING LIGHT. OPS CHECK FAILED. FOUND HOUSING TO HAVE A BAD GROUND. REMOVED LH EXTERNAL EMERGENCY WING LIGHT HOUSING. INSTALLED LH EXTERNAL EMERGENCY WING FAIRING LIGHT ASSEMBLY. OPS CHECK SAT.

Source: SDR JJBA20220304003 · FAA SDRS
O · 2022-02-17 Matched by certificate designator
ATA 3350

FLOOR PATH LIGHTING STRIP "EXIT" PLACARDS ARE MISPOSITIONED. CORRECTLY ORIENTED FLOOR PATH LIGHTING STRIPS "EXIT" PLACARDS.

Source: SDR JJBA20210217018 · FAA SDRS
B · 2022-01-31 Matched by certificate designator
ATA 2530

FA REPORTS BURNING SMELL FROM COFFEE MAKERS. CLEANED UP COFFEE BREW WARMER, PERFORMED VISUAL INSPECTION COFFEE BREW CRACKS, WIRES. NO DEFECTS NOTED. OPS CHECK GOOD

Source: SDR JJBA2022020431033 · FAA SDRS
O · 2021-12-13 Matched by certificate designator
ATA 3350

EMERGENCY EXIT LIGHT FORWARD OF WING INOPERATIVE. REMOVED AND REPLACED EMERGENCY EXIT LIGHT. OPS CHECK SAT.

Source: SDR JJBA20211213009 · FAA SDRS
O · 2021-06-03 Matched by certificate designator
ATA 3350

FWD CEILING CABIN EMERGENCY EXIT LOCATOR LIGHT INOPERATIVE. R&R EMERGENCY LIGHT INVERTER 6. OPS CHECK SAT.

Source: SDR JJBA20210603008 · FAA SDRS
O · 2021-05-17 Matched by certificate designator
ATA 3350

ENTRYWAY EMERGENCY LIGHT BULB BURNT OUT. R&R ENTRYWAY LIGHT BULB. OPS CHECK SAT.

Source: SDR JJBA20210517015 · FAA SDRS
B · 2020-07-10 Matched by certificate designator
ATA 3160

IAH - FLIGHT 3980, THE CREW REPORTED PFD#1 FAIL "SMOKED SMELL". THE AIRCRAFT LANDED AT IAH WITHOUT INCIDENT. MAINTENANCE REMOVED AND REPLACED PFD#1, OPERATIONALLY TESTED WITH NO DEFECTS AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA2020071304016 · FAA SDRS
O · 2020-02-03 Matched by certificate designator
ATA 5522

DURING C CHECK INSPECTION FOUND LEFT ELEVATOR LEADING EDGE SKIN WAS CHAFED INTERNALLY JUST FORWARD OF CUTOUT REINFORCEMENT BETWEEN RIB YH983.4 AND YH1280. MAINTENANCE REPLACED LEADING EDGE SKIN I/A/W SRM 51-10-04 AND SB 145-27-0034.

Source: SDR ASOA2020030433020 · FAA SDRS
O · 2020-01-29 Matched by certificate designator
ATA 5320

DURING C CHECK INSPECTION FOUND VENTRAL TANK FORWARD FACE OF RIB 1 HAS CORROSION AT LOWER CENTER SUPPORT BRACKET. MAINTENANCE REPAIRED VENTRAL TANK RIB 1 I/A/W ETD 2020-145-004783 REVISION C

Source: SDR ASOA2020030693026 · FAA SDRS
O · 2020-01-09 Matched by certificate designator
ATA 5330

DURING C CHECK INSPECTION FOUND CORROSSION ON FUSELAGE SKIN AT AFT RADIO ALTIMETER AT FRAME 65 STRINGER 21L-21R. MAINTENANCE REPAIRED I/A/W ETD2020-145-001101

Source: SDR ASOA202002193015 · FAA SDRS
O · 2020-01-06 Matched by certificate designator
ATA 5320

DURING C CHECK INSPECTION FOUND FLOOR BOARD SUPPORT CORRODED FRAME 18-23 STRINGER 15L-16L. MAINTENANCE REPLACED FLOOR BOARD SUPPORT

Source: SDR ASOA2020030463025 · FAA SDRS
O · 2020-01-05 Matched by certificate designator
ATA 3210

DURING C CHECK INSPECTION FOUND RIGHT FORWARD MAIN LANDING GEAR BEARING CAP HAD CORROSION/PITTING. MAINTENANCE REPLACED THE RIGHT FORWARD MAIN LANDING GEAR BEARING CAP.

Source: SDR ASOA2020020353006 · FAA SDRS
O · 2020-01-05 Matched by certificate designator
ATA 5330

DURING C CHECK INSPECTION FOUND CORROSSION AND MISSING RIVET ON AFT RADIO ALTIMETER BASE FRAME 68-69 AND STRINGER 21L-21R. MAINTENANCE PERFROMED REPAIR I/A/W ETD 2020-145-001101

Source: SDR ASOA202002193016 · FAA SDRS
O · 2020-01-03 Matched by certificate designator
ATA 5320

DURING C CHECK INSPECTION FOUND LAV FLOOR CENTER GUSSET AT FRAME 61 HAS SURFACE CORROSION. MAINTENANCE REPLACED LAV FLOOR CENTER GUSSET.

Source: SDR ASOA2020020633014 · FAA SDRS
O · 2020-01-03 Matched by certificate designator
ATA 5320

DURING C CHECK INSPECTION FOUND CENTER FUSELAGE IV FLOOR GUSSET HAT BEAM AT FRAME 61 HAD CORROSION. MAINTENANCE REPLACED GUSSET HAT BEAM AT FRAME 61

Source: SDR ASOA2020020633013 · FAA SDRS
O · 2020-01-03 Matched by certificate designator
ATA 3210

DURING C CHECK INSPECTION FOUND LEFT AFT MAIN LANDING GEAR BEARING CAP HAD CROSSION PITTING IN 1 AREA. MAINTENANCE INSPECTED AND REMOVED CORROSION IA/W SRM 57-51-07.

Source: SDR ASOA202002033008 · FAA SDRS
O · 2020-01-03 Matched by certificate designator
ATA 3210

DURING C CHECK INSPECTION FOUND LEFT FORWARD MAIN LANDING GEAR BEARING CAP HAD 3 AREAS OF CORROSION/PITTING. MAINTENANCE REPLACED LEFT FORWARD MAIN LANDING GEAR BEARING CAP.

Source: SDR ASOA202002033007 · FAA SDRS
O · 2020-01-03 Matched by certificate designator
ATA 5330

DURING C CHECK INSPECTION SKIN SPLICE WAS FOUND CORRODED AT FRAME 60-61 STRINGER 20R-21R. MAINTENANCE REPAIRED I/A/W SRM 53-00-02 AND 51-40-02.

Source: SDR ASOA2020021903017 · FAA SDRS
O · 2020-01-03 Matched by certificate designator
ATA 5320

DURING HEAVY CHECK INSPECTION FOUND CORROSION ON CENTER LAV FLOORBOARD SUPPORT AT FRAME 60-61. MAINTENANCE REPLACED LAV CENTER FLOOR BOARD SUPPORT. (GUSSET)

Source: SDR ASOA202001313005 · FAA SDRS
O · 2020-01-03 Matched by certificate designator
ATA 5320

DURING HEAVY MAINTENANCE CHECK CORROSSION WAS FOUND ON RIGHT SIDE LAV FLOORBOARD SUPPORT. AT FRAME 60 THRU61. MAINTENANCE REPLACED HAT BEAM GUSSET AT FRAME 60 TO 61.

Source: SDR ASOA202001313004 · FAA SDRS
O · 2020-01-02 Matched by certificate designator
ATA 5320

DURING C CHECK INSPECTION FOUND SERVICE DOOR SILL CORRODED@HOLES FOR SCREWS. MAINTENANCE REPLACED THE SERVICE DOOR SILL CHANNEL.

Source: SDR ASOA202002263018 · FAA SDRS
O · 2019-12-31 Matched by certificate designator
ATA 5310

DURING C CHECK INSPECTION CARGO DOOR CUTOUT SILL BEAM CORRODED AT FORWARD CORNER. MAINTENANCE REPLACED THE LOWER FRAME DOOR CARGO DOOR BEAM.

Source: SDR ASOA2020030313019 · FAA SDRS
O · 2019-12-30 Matched by certificate designator
ATA 5753

DURING C CHECK INSPECTION RIGHT INBOARD FLAP UPPER SURFACE HAS DAMAGED COMPOSITE AT INBOARD EDGE. MAINTENANCE REPAIRED COMPOSITE DAMAGE AT UPPER SKIN INBOARD EDGE I/A/W SRM 57-52-00.

Source: SDR ASOA2020030403024 · FAA SDRS
O · 2019-12-26 Matched by certificate designator
ATA 4910

DURING C CHECK INSPECTION FOUND LEFT APU LOWER MOUNTING ROD END CORRODED.MAINTENANCE REPLACED LEFT LOWER ROD ASSEMBLY.

Source: SDR ASOA202002063012 · FAA SDRS
O · 2019-12-26 Matched by certificate designator
ATA 4910

DURING C CHECK INSPECTION FOUND UPPER APU MOUNTING RODENDS CORRODED. MAINTENANCE REPLACED APU UPPER SUPPORT RODS .

Source: SDR ASOA20200206311 · FAA SDRS
O · 2019-12-22 Matched by certificate designator
ATA 5712

DURING C CHECK INSPECTION THE LEFT WING RIB 21 WAS FOUND CRACKED. MAINTENANCE PERFORMED REPAIR I/A/W SRM 57-20-07.

Source: SDR ASOA2020304223022 · FAA SDRS
O · 2019-12-20 Matched by certificate designator
ATA 5330

DURING C CHECK INSPECTION FOUND CENTER FUSELAGE IV DRAIN PLUG DOUBLER HAD CORROSION, FRAME 53-FRAME 54 STRINGER 21 LH TO 21 RH. MAINTENANCE REPLACED DOUBLER I/A/W ETD2020-145-001840

Source: SDR ASOA20200203009 · FAA SDRS
O · 2019-12-19 Matched by certificate designator
ATA 5712

DURING C CHECK INSPECTION FOUND RIGHT WING RIB 21 CRACKED. MAINTENANCE REPAIRED RIGHT WING RIB 21 I/A/W SRM 57-20-07.

Source: SDR ASOA2020030493023 · FAA SDRS
O · 2019-12-15 Matched by certificate designator
ATA 5330

DURING C CHECK INSPECTION FOUND GOUGE ON FORWARD FUSELAGE SKIN II BELOW GPU ACCESS DOOR. MAINTENANCE REPAIRED DAMAGED SKIN I/A/W SRM 53-12-01 AND ETD2020-145-002945

Source: SDR ASOA2020030453021 · FAA SDRS
L · 2019-06-29 Matched by certificate designator
ATA 3350

IAH - FLIGHT 4197, THE CREW REPORTED THAT THE EMERGENCY LIGHT NEAR THE EXIT DOOR IN THE CEILING WAS INOPERATIVE. MAINTENANCE REMOVED AND REPLACED THE DEFECTIVE LIGHT BULB, OPERATIONALLY TESTED WITH NO DEFECTS AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA201906294038 · FAA SDRS
L · 2019-02-26 Matched by certificate designator
ATA 3350

IAH - DURING MAINTENANCE INSPECTION SEVERAL EMERGENCY LIGHTS WEER FOUND TO BE INOPERATIVE. MAINTENANCE REMOVED AND REPLACED THE NUMBER ONE AND TWO EMERGENCY LIGHT BATTERY PACKS, OPERATIONALLY TESTED WITH NO DEFECTS NOTRED AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA201902264008 · FAA SDRS
L · 2019-02-26 Matched by certificate designator
ATA 3350

** SUPPLEMENTAL TO ASOA201802264007 CONTROL NUMBER SHOULD HAVE BEEN ASOA201902264007*** IAH- DURING MAINTENANCE INSPECTION SEVERAL EMERGENCY LIGHTS WEER FOUND TO BE INOPERATIVE. MAINTENANCE REMOVED AND REPLACED THE NUMBER ONE AND TWO EMERGENCY LIGHT BATTERY PACKS, OPERATIONALLY TESTED WITH NO DEFECTS NOTRED AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA201902264007 · FAA SDRS
O · 2018-02-17 Matched by certificate designator
ATA 5330

FOUND A CREASED AREA AFT OF A RECENT REPAIR BETWEEN FRAMES 19 - 20 AND STRINGERS 11L AND 12L. MAINTENANCE REMOVED THE OLD DOUBLER AND CUT OUT THE DAMAGE AREA AND INSTALL A FILLER AND A NEW DOUBLER ENCOMPASSING ALL OF THE DAMAGE IAW ETD2018-145-019052.

Source: SDR ASOA201802177017 · FAA SDRS
O · 2014-05-29 Matched by certificate designator
ATA 5751

DURING C-CHECK, INSPECTION FOUND THE LT AILERON PCA BRACKET INBD HAT BUSHING FOR INBD ATTACH POINT HAS NO INTERFERENCE FIT. MAINTENANCE R & R THE LT AILERON PCA BRACKET IAW AMM 27-10-00. ALL WORK ACCOMPLISHED AND WILL BE RELEASED AT THE END OF THE CHECK.

Source: SDR ASOA20140529087 · FAA SDRS
R J · 2014-02-19 Matched by certificate designator
ATA 7410

THE CREW REPORTED AT FL350 WITH THRUST SET FOR CRUISE FLIGHT, THEY EXPERIENCED TWO AUTO RELIGHT SEQUENCES WITH NO ASSOCIATED CAUTION AND WARNING MESSAGES BUT DID FEEL THE EFFECT OF THE ASSOCIATED POWER LOSS AND SUCCESSFUL RELIGHT. MAINTENANCE INSPECTED AND REPLACED THE NR 2 ENGINE PMA IAW MM 74-11-10. PERFORMED OPS GROUND RUNS WITH NO DEFECT NOTED. MAINTENANCE ALSO REPLACED THE NR 2 ENGINE FPMU AND THE NR 2B FADEC IAW POWERPLANT ENGINEERING.

Source: SDR ASOA20140219019 · FAA SDRS
B · 2013-06-10 Matched by certificate designator
ATA 2120

CREW REPORTED A ODOR OF SMOKE IMMEDIATELY AFTER THE ACFT WAS POSSIBLY STRUCK BY LIGHTNING. MX INSPECTED ACFT, RAN AIR CONDITIONING PACKS, TAXIED, AND HAD ELECTRICAL POWER ON ACFT FOR HOURS WITH NO ODOR OF SMOKE OR LIGHTNING STRIKE DAMAGE NOTED. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20130610057 · FAA SDRS
W B · 2013-04-24 Matched by certificate designator
ATA 4990

CREW REPORTED A STRONG ELECTRICAL ODOR IN COCKPIT AND CABIN AT FL220. MX PERFORMED FAULT ISOLATION TASK 21-20-00-810-801A AND 21-20-00-810-803A WITH NO DEFECTS NOTED, NO FAILED ELECTRICAL COMPONENTS OR FLUID LEAKS NOTED. RAN ENGINES, APU, AND AIR CONDITIONING PACKS WITH NO SMOKE NOTED. FOUND APU OIL LEVEL OVERSERVICED, SERVICE APU OIL LEVEL ACCORDING. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20130424039 · FAA SDRS
L · 2012-12-21 Matched by certificate designator
ATA 3397

MAIN DOOR EMERGENCY LIGHT AND MAIN ENTRANCE EMERGENCY LIGHT INOPERATIVE. REPAIRED SHORTED WIRE AT OVERHEAD LIGHT. OPS CHECK GOOD.

Source: SDR ASOA20121224182 · FAA SDRS
K B · 2012-10-25 Matched by certificate designator
ATA 7200

THE CREW REPORTED SMOKE IN THE COCKPIT & CABIN AFTER TAKE-OFF, ALONG WITH LAVATORY SMOKE MESSAGE WARNING. AIRCRAFT RETURNED TO DEPARTURE AND LANDED WITHOUT FURTHER INCIDENT. MX INSPECTED AND REPLACED THE NR 1 ENGINE. OPS CHECKED GOOD.

Source: SDR ASOA20121025085 · FAA SDRS
O · 2012-05-08 Matched by certificate designator
ATA 2810

BOTTOM CENTER OF THE VENTRAL TANK WAS FOUND GOUGED. MX REPAIRED VENTRAL TANK BY INSTALLING A DOUBLER IAW EC 2810-01053. ALL WORK ACCOMPLISHED AND WILL BE RELEASED AT THE END OF THE CHECK

Source: SDR ASOA20120508096 · FAA SDRS
L · 2012-04-05 Matched by certificate designator
ATA 3350

DURING ROUTINE MX, EMERGENCY LIGHT INOPERATIVE AT EXIT ROW 12 A, B, C. REPLACED NR 4 EMERGENCY LIGHT BATTERY. OPS CHECKED GOOD.

Source: SDR ASOA20120405037 · FAA SDRS
B · 2012-02-29 Unresolved
ATA 2120

AFTER SHUTTING DOWN THE APU ON ARRIVAL CREW REPORTED AN ELECTRICAL BURNING ODOR. MX INSPECTED THE ACFT WITH NO DEFECTS NOTED, OPS TESTED APU WITH NO DEFECTS NOTED, THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20120229028 · FAA SDRS
O · 2012-02-18 Matched by certificate designator
ATA 5330

ACFT HAD GROUND DAMAGE AND WAS FERRIED FOR THE REPAIRS. THE FUSELAGE BETWEEN FR 65 TO FR 66 AND BETWEEN STR 17L AND 18L WERE DAMAGED. THE WORK WAS ACCOMPLISHED IAW EC5300-01025. ALSO THE TEMPORARY REPAIRS WERE COMPLIED WITH IAW THE REPAIR ETD2012-145-001697C. UPON COMPLETION OF ALL WORK THE ACFT WILL BE RELEASED TO SERVICE.

Source: SDR ASOA2012180003 · FAA SDRS
J · 2011-09-20 Unresolved
ATA 2740

THE CREW REPORTED A PITCH TRIM BACK-UP FAIL MESSAGE IN FLIGHT. THE AIRCRAFT DIVERTED INTO CLE AND LANDED WITHOUT INCIDENT. MAINTENANCE REPLACED THE BACK-UP PITCH TRIM SWITCH.OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA11CL211 · FAA SDRS
N · 2011-08-09 Unresolved
ATA 3260

FLIGHT 3124 - EWR - FLIGHT CREW REPORTED L/G AIR GROUND FAIL INDICATION ON EICAS. EWR MX PERFORMED AIR GROUND SYSTEM RESET AND PERFORMED OPERATIONAL CHECK SUCCESSFULLY. ACFT WAS APPROVED TO RETURN TO SERVICE.

Source: SDR C2XA11RI131 · FAA SDRS
B · 2011-05-12 Unresolved
ATA 2350

FLIGHT 4940 - EWR - FLIGHT CREW REPORTED FO AUDIO CONTROL PANEL GAVE OUT ELECTRICAL SMELL. EWR MX REMOVED AND REPLACED FO AUDIO CONTROL PANEL AND PERFORMED OPERATIONAL CHECK SUCCESSFULLY. ACFT WAS APPROVED TO RETURN TO SERVICE.

Source: SDR C2XA11RI078 · FAA SDRS
J · 2010-12-12 Unresolved
ATA 3010

FLIGHT 2640 - MSN - FLIGHT CREW REPORTED WING ANTI-ICE FAIL IN ICE CONDITION - ANTI ICE INOPERATIVE. EWR MX REMOVED AND REPLACED NR 2 WING LOW PRESSURE SWITCH AND PERFORMED OPERATIONAL CHECK SUCCESSFULLY. ACFT WAS APPROVED TO RETURN TO SERVICE.

Source: SDR C2XA10RI156 · FAA SDRS
O · 2010-10-04 Unresolved
ATA 5330

SHV - DURING C-CHECK EXTERNAL FUSELAGE HAS POSSIBLE CRACKS AROUND FASTENER HEAD AT FRAME 78 STR 5L. MAINTENANCE PERFORMED REPAIR ON FRAME 78-79 STR 5L-6L IAW EC5330-02251. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH323 · FAA SDRS
O · 2010-10-04 Unresolved
ATA 5320

SHV - DURING C-CHECK CROSSBEAM AT FRAME 23 FROM CENTER OMEGA BEAM TO RT AFT FLOOR SILL HAS CORROSION (LEVEL 2 LOCAL). MAINTENANCE REMOVED AND REPLACED CROSSBEAM AT FRAME 23 FROM CENTER OMEGA BEAM TO RT AFT FLOOR SILL. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH322 · FAA SDRS
O · 2010-10-04 Unresolved
ATA 5320

SHV - DURING CHECK CENTER OMEGA BEAM RAMP ANGLE SUPPORT CORRODED (LEVEL 2 LOCAL) AT FRAME 20. MAINTENANCE REMOVED AND REPLACED CENTER OMEGA BEAM RAMP ANGLE SUPPORT AT FRAME 20. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH321 · FAA SDRS
O · 2010-10-04 Unresolved
ATA 5755

SHV - DURING C-CHECK LT GROUND SPOILER INBOARD HINGE OUTBOARD HAT BUSHING MIGRATED. MAINTENANCE REMOVED AND REPLACED LT GROUND SPOILER INBOARD HINGE IAW EMB-145 SRM 51-40-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH320 · FAA SDRS
L · 2010-07-20 Unresolved
ATA 2611

FLIGHT 2851 - YHZ - FLIGHT CREW REPORTED BAG SMOKE LIGHT WOULD NOT ILLUMINATE DURING TEST. EWR MX REMOVED AND REPLACED RELAY K0629 AND PERFORMED OPERATIONAL CHECK SUCCESSFULLY. ACFT WAS APPROVED TO RETURN TO SERVICE.

Source: SDR C2XA10RI104 · FAA SDRS
B · 2010-04-15 Unresolved
ATA 3040

IAH - FLIGHT 2865, DURING DESCENT THE CREW REPORTED A BURNING SMELL IN THE COCKPIT. THE AIRCRAFT LANDED IN IAH WITHOUT INCIDENT. MAINTENANCE REMOVED AND REPLACED THE NR 1 WINDSHIELD HEAT CONTROLLER, OPERATIONALLY TESTED WITH NO DEFECTS NOTED. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA01IA118A · FAA SDRS
O · 2009-04-30 Unresolved
ATA 3350

DURING ROUTINE MAINTENANCE THE CENTER AISLE EMERGENCY EXIT SIGN AT THE OVERWING ESCAPE HATCH WAS ONLY ILLUMINATED HALFWAY. MAINTENANCE REPLACED THE EXIT SIGN AND OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA09CL058 · FAA SDRS
L · 2009-03-20 Unresolved
ATA 3350

RIC - DURING ROUTINE MAINTENANCE, RIC MX FOUND BOTH AFT EXTERIOR EMERGENCY LIGHTS INOPERATIVE. MX REMOVED AND REPLACED BATTERY CHARGER NR 4 AND PERFORMED OPERATIONAL CHECK SUCCESSFULLY. AIRCRAFT WAS APPROVED TO RETURN TO SERVICE.

Source: SDR C2XA09RI036 · FAA SDRS
L · 2009-02-09 Unresolved
ATA 3350

LT AND RT EMERGENCY AFT LIGHT INOP. R&R FUSE ON NR 4 EMERGENCY LIGHT BATTERY. OPS CHECK GOOD IAW EMB 145 VCMM 33-21-70. ACFT RELEASED AND RETURNED TO SERVICE.

Source: SDR C2XA09TY026 · FAA SDRS
L · 2009-01-17 Unresolved
ATA 3350

DURING ROUTINE MX, RIC MX FOUND LT AND RT OVERWING EMERGENCY LIGHTS INOPERATIVE. MX R&R NR 4 BATTERY POWER SUPPLY AND PERFORMED OPS CHECK SUCCESSFULLY. ACFT WAS APPROVED TO RETURN TO SERVICE.

Source: SDR C2XA09RI014 · FAA SDRS
F · 2009-01-05 Unresolved
ATA 2721

THE CREW REPORTED T/O YAW DAMPER ENGAGE RUDDER RT DEFLECTION. WHEN TRIM KNOB WAS ACTIVATED, EXTREME LT WAS OPERATED. THE ACFT RETURNED TO IAH WHERE IT LANDED WITHOUT INCIDENT. MAINT REMOVED AND REPLACED THE TRIM CONTROL MODULE, OPERATIONALLY TESTED WITH NO DEFECTS, AND THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA09IA005 · FAA SDRS
J · 2008-07-27 Unresolved
ATA 3150

IAH - FLIGHT 2836, THE CREW REPORTED AN AIR GROUND FAIL MESSAGE ON EICAS AFTER T/O THAT REMAINED ON DURING THE ENTIRE FLIGHT. THE AIRCRAFT LANDED AT IAH WITHOUT INCIDENT WHERE MAINTENANCE INSPECTED THE AIRCRAFT, OPERATIONALLY TESTED THE AIR GROUND SYSTEM WITH NO DEFECTS NOTED, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE. (A)

Source: SDR C2XA081A175 · FAA SDRS
L · 2008-05-22 Unresolved
ATA 3350

DURING ROUTINE MAINTENANCE BOTH AFT EXTERIOR EMERGENCY LIGHTS WERE FOUND INOPERATIVE. MAINTENANCE REPLACED THE NR 4 BATTERY POWER SUPPLY. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA08CL062 · FAA SDRS
L · 2008-03-11 Unresolved
ATA 3350

EWR, DURING POST FLIGHT INSPECTION THE LEFT HAND AND RIGHT HAND EXTERIOR OVERWING EMERGENCY EXIT LIGHTS WERE FOUND TO BE INOPERATIVE. MAINTENANCE REMOVED AND REPLACED THE NUMBER FOUR EMERGENCY LIGHT BATTERY PACK POWER SUPPLY, OPERATIONALLY CHECKED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA08IA080 · FAA SDRS
N · 2008-01-12 Unresolved
ATA 3150

IAH FLIGHT 2140 - THE CREW REPORTED A ELECTRICAL EMERGENCY ABNORMAL MESSAGE ON THE EICAS. THE CREW DIVERTED INTO CLE AND LANDED WITHOUT INCIDENT. MAINTENANCE INSPECTED AND AFTER RESET COULD NOT DUPLICATE. THE NR 1 AND NR 2 BUSS TIE CONTACTORS AND ESSENTIAL TIME RELAY AND POWER SWITCH WERE REPLACED FOR PRECAUTIONARY REASONS. OPERATIONAL CHECKS OF THE DC DISTRIBUTION SYSTEM WERE GOOD.

Source: SDR C2XA08CL006 · FAA SDRS
L · 2007-12-20 Unresolved
ATA 3350

OVERWING EMERGENCY LIGHTS INOP. REMOVED AND REPLACED EMERGENCY LIGHT NR 4 BATTERY POWER SUPPLY IAW EMB 145XR AMM 33-50-04. OPS CHECK GOOD. AIRCRAFT RELEASED AND RETURNED TO SERVICE.

Source: SDR C2XA07TY086 · FAA SDRS
O · 2007-11-28 Unresolved
ATA 3350

IAH - FLIGHT 2556 THE CREW REPORTED THAT THE OVERWING EMERGENCY EXIT LIGHTS ILLUMINATED IN FLIGHT WITH ALL OTHERS OFF, AND FINALLY EXTINGUISHED AFTER APPROXIMATELKY 20 MINUTES. THE AIRCRAFT LANDED AT IAH WITHOUT INCIDENT. MAINTENANCE REMOVED AND REPLACED THE AFFECTED EMERGENCY LIGHT BATTERY PACK, OPERATIONALLY CHECKED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA07IA240 · FAA SDRS
N · 2007-07-29 Unresolved
ATA 3260

IAH - FLIGHT 2317, THE CREW REPORTED A LANDING GEAR AIR/GROUND FAILURE MESSAGE ON EICAS DURING FLIGHT. THE AIRCRAFT LANDED IN IAH WITHOUT INCIDENT WHERE MAINTENANCE REMOVED AND REPLACED THE LEFT HAND MAIN LANDING GEAR DOWNLOCK PROXIMITY SWITCH, OPERATIONALLY CHECKED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA07IA178 · FAA SDRS
Y J · 2006-11-06 Unresolved
ATA 7200

IAH - FLIGHT 2780, THE CREW REPORTED AN UNCOMMANDED ENGINE SHUTDOWN DURING DESCENT INTO IAH. THE AIRCRAFT LANDED WITHOUT INCIDENT WHERE MAINTENANCE REMOVED AND REPLACED THE NR 2 ENGINE, OPERATIONALLY CHECKED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE. AWAITING FINAL DETERMINATION.

Source: SDR C2XA06IA173 · FAA SDRS
O · 2005-12-09 Unresolved
ATA 5315

TYS, DURING A SCHEDULED INSPECTION, CORROSION WAS FOUND ON FLOORBEAM AT CARBON FIBER CROSS BEAM AT FRAME 20. MAINTENANCE REMOVED THE ANGLE AND DAMAGED AREA FROM THE LEFT OMEGA BEAM, FABRICATED NEW REPAIR PIECES, ALODINED, PRIMED AND INSTALLED IAW EMB145XR SRM 51-20-03, 53-00-10 AND CPM-51-21-04/05/06.

Source: SDR C2XA05TY060 · FAA SDRS
J · 2004-04-28 Unresolved
ATA 3260

TYS FLIGHT 2797, AFTER TAKEOFF THE NOSE GEAR DOORS REMAINED OPEN. A/C WAS FERRIED TO TYS WHERE MAINT REMOVED AND REPLACED THE NLG SEQUENCE SWITCH IAW EMB 145XR MM 32-63-03. OPS CHECK GOOD. A/C RELEASED TO REVENUE SERVICE.

Source: SDR C2XA04TY075 · FAA SDRS
K · 2003-08-27 Unresolved
ATA 4930

EWR LOG BOOK SQUAWK MASSIVE FUEL LEAK. LOCATED LEAK ON APU FILTER. RED BYPASS BUTTON WAS LEAKING WHEN PUMP PRESSURE APPLIED. REMOVED AND REPLACED APU FILTER HOUSING. OPS AND LEAK CHECK GOOD IAW EMB145 MM 49-31-07.

Source: SDR C2XA03BT084 · FAA SDRS
B · 2003-08-08 Unresolved
ATA 2121

FLIGHT 3499 FROM RDU TO IAH, CREW REPORTED THAT THERE WAS A BURNING SMELL IN THE COCKPIT. THE CREW ELECTED TO DIVERT AND LANDED AT HSV WITHOUT FURTHER INCIDENT. THE FAN WAS DEFFERED UNDER MEL 21-23-03. THE MEL WAS CLEARED ON 8/8/2003 IN EWR WHERE MAINTENANCE REMOVED AND REPLACED THE AFFECTED FAN. THE SYSTEM OPERATIONALLY CHECKED GOOD AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA03IA080 · FAA SDRS