N111P

GULFSTREAM AEROSPACE G-IV · 1998 · Valid Registration

Registered owner: TPR AVIATION LLC, CO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
INTERNATIONAL JET AVIATION SERVICES INC. (CJPA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

K J · 2021-07-14 Matched by certificate designator
ATA 2910

ABOUT 20 MILES FROM LANDING, ATC ISSUED INSTRUCTIONS TO SLOW TO 190 KTS. I USED THE AIRBRAKES TO SLOW, AND WHEN RETRACTING THE AIRBRAKES, THE PM NOTICED THE #2 HYD PUMP WARNING LIGHT FLICKER, ACCOMPANIED BY LOW PRESSURE AND NEAR ZERO QUANTITY. THERE WAS STILL RESIDUAL PRESSURE, SO I ELECTED TO START CONFIGURING FLAPS FOR LANDING (FLAPS ARE ON #2 SYSTEM). THE PM REFERRED TO THE CHECKLIST, WHICH LISTED THE ITEMS ON THE #2 SYSTEM: FLAPS, AIRBRAKES, NOSEWHEEL STEERING, AND EMERGENCY BRAKES. THERE WAS NO OTHER CONCERNS ABOUT GEAR OR MAIN BRAKES WHICH ARE ON THE #1 SYSTEM. WHEN CHECKING IN WITH CENTENNIAL TOWER, WE DID NOT DECLARE AN EMERGENCY, BUT DID ADVISE OF OUR #2 SYSTEM LOSS AND POSSIBLE STEERING DIFFICULTIES WHEN ATTEMPTING TO EXIT THE RUNWAY. WE LANDED WITH FLAPS 20 INSTEAD OF FULL FLAPS, ADDING 5 KNOTS TO REF SPEED PER THE AFM. DURING LANDING ROLLOUT, NORMAL BRAKES WORKED JUST FINE, AND AS I SLOWED TO TAXI SPEED, I WAS ABLE TO STEER WITH DIFFERENTIAL BRAKING AND CLEARED THE RUNWAY WITHOUT INCIDENT. STEERING CONTROL WAS ADEQUATE TO ALLOW NORMAL TAXI BACK TO THE RAMP. UPON SHUTDOWN, HYDRAULIC FLIUD WAS LEAKING FROM THE AFT SECTION OF THE AIRPLANE. OUR MECHANIC OPENED THE COWLING AND DISCOVERED A LOOSE FITTING ON THE MAIN PRESSURE LINE.

Source: SDR CJPA2021072600021 · FAA SDRS
O · 2017-06-14 Matched by certificate designator
ATA 3097

WINDSHIELD HEAT ELECTRICAL CABLE AND INSULATION BURNED INTERIOR COVERINGS ABOVE THE MAIN ENTRY DOOR. PROBLEM CAUSED BY WRONG WIRE SPLICE INSTALLED IN THE POWER CABLE.

Source: SDR JGVR20170614004 · FAA SDRS
B · 2017-01-04 Matched by certificate designator
ATA 3440

AT FL30, THE PILOT REPORTED SMOKE IN THE COCKPIT. DECLARED AN EMERGENCY AND DIVERTED. NOTICED THE SMOKE WENT AWAY AND AFTER DESCENDING TO FL15, CANCELED THE EMERGENCY. PROBLEM WAS THE BLOWER MOTOR ON THE NR 1 IRU. NO C/B’S TRIPPED, AND NO SYSTEMS WERE COMPROMISED.

Source: SDR CJPA20170104001 · FAA SDRS