N1127M

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
WORLDWIDE JET CHARTER, INC. (WWQA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2020-01-20 Matched by certificate designator
ATA 3230

ON APPROACH INTO KHPN LEFT MAIN GEAR WAS NOT DOWN AND LOCKED ALSO VERIFIED BY TWO RED GEAR DOOR LIGHTS. CYCLED THE LANDING GEAR UP AND DOWN AT LEAST FOUR TIMES WITH THE SAME INDICATION. AS PER THE CHECKLIST WE PERFORMED AN ALTERNATE GEAR EXTENSION USING THE EMERGENCY GEAR AIR. WITH NO CHANGE IN THE INDICATION WE USED THE EMERGENCY BRAKE AIR BOTTLE. WITH STILL NO CHANGE IN INDICATION WE DECLARED AN EMERGENCY AND DECIDED THE BEST COURSE OF ACTION WOULD BE TO DIVERT TO KEWR WHERE RUNWAY LENGTH WOULD BE SUFFICIENT. EMERGENCY EQUIPMENT WOULD BE AVAILABLE AND CUSTOMS AND BORDER PROTECTION WOULD BE AVAILABLE SINCE WE WERE ON AN INTERNATIONAL FLIGHT. THE NECESSITY OF ALTERNATE GEAR EXTENSION RESULTED IN THE LOSS OF HYDRAULICS WHICH THEN RESULTED IN A PARTIAL FLAPS LANDING. ON THE WAY TO KEWR OUR LANDING GEAR FINALLY GAVE A DOWN AND LOCKED INDICATION. UPON TOUCHDOWN ON 4L THERE WERE NO SPOILERS EXTENDED AS EXPECTED. THE THRUST REVERSERS ONLY UNLOCKED AND DID NOT DEPLOY. THE TOE BRAKES DID NOT WORK AS EXPECTED AND NECESSITATED EMERGENCY BRAKING. WE STOPPED THE AIRCRAFT ON THE RUNWAY AND WAITED FOR GROUND CREWS TO REMOVE US.” MAINTENANCE FOUND THE LH MLG DOWN AND LOCKED SWITCH FAULTY. PART NUMBER 1EN1-8 AN OPERATIONAL MX CHECK FLIGHT WAS TO BE PERFORMED AND IT WAS DISCOVERED BOTH MLG DOORS REMAINED OPEN AFTER ENGINE START. AIRCRAFT WAS FERRIED FROM KEWR TO KTEB FOR ADDITIONAL MAINTENANCE. IN TEB MX REPLACED THE LH MLG RETRACTION ACTUATOR P/N: 6027100-001 FAILED S/N: KL0237. GEAR SWINGS CHECK GOOD, OPERATIONAL MX CHECK FLIGHT SATISFACTORY. RELEASED FOR SERVICE

Source: SDR WWQA202001232001 · FAA SDRS
O · 1998-05-15 Unresolved
ATA 2150

FOUND BROKEN OUT PIECES OF AIR BOX IN TAIL COMPARTMENT. SUSPECT CRACKED WELD SEAM AND VIBRATION, CAUSE - FAILURE. INSTALLED NEW REINFORCED AIR BOX P/N 5419680-16.

Source: SDR 98ZZZX2197 · FAA SDRS