N11565

EMBRAER EMB-145LR · 2002 · Valid Registration

Registered owner: CORPORATE FLIGHT MANAGEMENT INC, TN (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CORPORATE FLIGHT MANAGEMENT, INC. (FJTA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2018-06-08 Matched by certificate designator
ATA 5330

RT REAR FUSELAGE SKIN AT FRAME 75, STRINGER 2R-3R CRACKED. REPAIRED FUSELAGE SKIN IN ACCORDANCE WITH SRM 53-31-01.

Source: SDR ASOA201806087105 · FAA SDRS
O · 2018-06-08 Matched by certificate designator
ATA 5530

RT AND LT SPHERICAL BEARING HOUSINGS HAVE DISPLACED METAL. REPAIRED LT AND RT SPHERICAL BEARING HOUSING IN ACCORDANCE WITH SRM 55-30-02.

Source: SDR ASOA2018060871051 · FAA SDRS
O · 2018-06-04 Matched by certificate designator
ATA 5330

FUSELAGE SKIN CRACKED AT FRAME 75, STRINGER 2L. CUTOUT THE DAMAGE SECTION, FABRICATED A FILLER, AND DOUBLER. INSTALLED THE REPAIR.

Source: SDR ASOA201806067098 · FAA SDRS
O · 2018-05-27 Matched by certificate designator
ATA 5330

TYS A/C IS IN FOR A C-CHECK WHEN INSPECTION FOUND A CRACK IN THE REAR FUSELAGE SKIN AT FRAME 75 AND STRINGER 2R. MAINTENANCE CUTOUT A 2" BY 2" SECTION OF SKIN AND INSTALLED A FILLER AND DOUBLER IAW SRM 51-31-01. ALL WORK ACCOMPLISHED AND WILL BE RELEASED AT THE END OF THE CHECK.

Source: SDR ASOA201805277094 · FAA SDRS
B · 2015-12-15 Matched by certificate designator
ATA 3420

CREW REPORTED AN ELECTRICAL ODOR AFTER CAPTAINS MFD WENT BLANK. MAINTENANCE R & R CAPTAIN`S MFD WITH OPS CHECK GOOD. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20151215060 · FAA SDRS
B · 2015-12-15 Matched by certificate designator
ATA 3420

THE CREW REPORTED MFD 1 IS OUT WITH BURNING ODOR IN FLIGHT DECK. THE ACFT LANDED IN ECP WITHOUT INCIDENT WHERE MAINTENANCE PLACED THE AFFECTED MFD ON MEL 34-22-01-1 AND THE ACFT WAS APPROVED FOR RETURN TO SERVICE. MAINTENANCE R & R THE NR 1 MFD, OPERATIONALLY TESTED WITH NO DEFECTS, REMOVED THE MEL, AND THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20151215091 · FAA SDRS
B · 2015-10-09 Matched by certificate designator
ATA 4930

THE CREW REPORTED A FUEL ODOR COMING FROM APU BLEED. AFTER ROTATION WHEN APU WAS PROVIDING AIR TO THE PACKS. MAINTENANCE INSPECTED AND REPLACED THE APU FUEL CONTROL ASSY. OPS CHECKED WERE GOOD.

Source: SDR ASOA20151009058 · FAA SDRS
B · 2015-02-10 Matched by certificate designator
ATA 2150

CREW REPORTED A BURNING ODOR BEFORE LANDING. MAINTENANCE PERFORMED TROUBLESHOOTING AND NO UNUSUAL ODORS COULD BE DETECTED OR REPRODUCED. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20150210009 · FAA SDRS
O · 2014-11-17 Matched by certificate designator
ATA 3350

THE CREW REPORTED EMERGENCY LIGHT WAS INTERMITTENT. MAINTENANCE INSPECTED AND PERFORMED OPERATIONAL CHECKS OF THE EMERGENCY LIGHTS. NO DEFECTS WERE FOUND. THE AIRCRAFT WAS RELEASED FOR SERVICE.

Source: SDR ASOA20141117092 · FAA SDRS
O · 2014-10-14 Matched by certificate designator
ATA 5310

ACFT WAS ON TAKEOFF WHEN A BIRD HIT THE NOSE. ACFT LANDED WITHOUT INCIDENT AND MAINTENANCE REMOVED THE BAD RIVETS AND INSTALL 5 OF A OVERSIZE RIVETS. ALODINED, PRIMED AND PAINTED IAW SRM 51-40-02 AND CPM 51-=21-07. PERFORMED A HIGH FREQUENCY EDDY CURRENT INSPECTION OF AREA. SOP 5711, NO DEFECTS NOTED AND WAS RELEASED BACK TO SERVICE.

Source: SDR ASOA20141014109 · FAA SDRS
L · 2014-08-04 Matched by certificate designator
ATA 3350

DURING MX INSPECTION, THE LT OVERWING EMERGENCY LIGHT WAS FOUND INOPERATIVE. MAINTENANCE REMOVED BULB, CLEANED DEBRIS FROM SOCKET AND REINSTALLED BULB, OPS CHECKED GOOD. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20140804085 · FAA SDRS
M B · 2014-07-06 Matched by certificate designator
ATA 3040

THE CREW REPORTED A STRONG SMOKE ODOR, CIGARETTE & PAPER ODOR EMITTING FROM MCD, F/A JUMPSEAT, AROUND EQUIPMENT CLOSET. THE ACFT RETURNED, WHERE IT LANDED WITHOUT INCIDENT. MAINTENANCE INSPECTED THE ACFT AND FOUND THE NR 1 WINDSHIELD TEMP CONTROLLER TO HAVE MELTED TERMONAL LUGS. MAINTENANCE R & R THE AFFECTED WINDSHIELD TEMP CONTROLLER, OPS TESTED WITH NO DEFECTS, ANDTHE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20140706089 · FAA SDRS
B · 2014-04-17 Matched by certificate designator
ATA 2530

F/A REPORTED AN ODOR COMING FROM THE GALLEY COFFEEMAKERS. MAINTENANCE CLEANED THE WARMERS ON BOTH COFFEE BREWERS AND PERFORMED AN OPS CHECK, CHECKED GOOD, WITH NO BURNING ODORS DETECTED. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20140417046 · FAA SDRS
J · 2014-01-12 Matched by certificate designator
ATA 3240

A "BRAKE DEGRADE" MESSAGE APPEARED ON EICAS DURING LANDING AND REPORTED MORE THAN NORMAL BRAKE PEDAL PRESSURE NEEDED. ACFT PULLED TO THE LEFT. R & R NR 4 BRAKE ASSY, TEMP SENSOR, HYD FUSE AND BRAKE CONTROL VALVE, OPS CHECKED SUCCESSFUL. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20140112005 · FAA SDRS
O · 2014-01-09 Matched by certificate designator
ATA 5753

DURING C-CHECK, LT OTBD FLAP INBD ROOT RIB INTERNAL WEBBING CRACKED. MAINTENANCE REPAIRED IAW EC 5750-01562.

Source: SDR ASOA20140109011 · FAA SDRS
O · 2014-01-07 Matched by certificate designator
ATA 5340

DURING C-CHECK, INSPECTION FOUND VERTICAL STAB SPAR TO FRAME 75 FRETTING AT THE FUSELAGE. MAINTENANCE COMPLIED WITH THE EC 5310-01317 TO REMOVED FITTING, REMOVED CORROSION, CHECK LIMITS AND REINSTALL FITTING.

Source: SDR ASOA20140107010 · FAA SDRS
B · 2013-07-24 Matched by certificate designator
ATA 2120

PILOT REPORTED A STRONG ODOR OF PLASTIC/ELECTRICAL SMOKE INFLIGHT DURING DESCENT WITH THE TOP OF GLARESHIELD/AVIONICS PANEL EXTREMELY HOT TO THE TOUCH. MX INSPECTED CABIN AND COCKPIT FOR PLASTIC/ELECTRICAL ODOR WITH NONE FOUND OR NOTED. ALSO RAN BOTH ENGINES AND BLEEDS PACKS WITH NO ODOR NOTED. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20130724078 · FAA SDRS
F · 2013-06-09 Matched by certificate designator
ATA 2700

MAIN PITCH TRIM INOPERATIVE MESSAGE ON CLIMBOUT, AUTO TRIM FAIL, ELEVATOR MISTRIM. R & R PITCH TRIM SWITCH AND ACTUATOR. OPS CHECK GOOD ACFT RELEASED AND RETURNED TO SERVICE.

Source: SDR ASOA20130609328 · FAA SDRS
B · 2012-08-06 Matched by certificate designator
ATA 3320

THE CREW REPORTED SMOKE FROM 4C SIDEWALL LIGHT. MX REPLACED 4 B & C LIGHT ASSY AND 4 B&C LIGHT BALLAST. OPS CHECKS WERE GOOD.

Source: SDR ASOA20120806068 · FAA SDRS
L · 2012-02-01 Matched by certificate designator
ATA 3397

EMERGENCY LIGHT FLOOR STRIP INOP. R & R LIGHT STRIP. OPS CHECK GOOD.

Source: SDR ASOA20120201004 · FAA SDRS
J · 2011-11-03 Matched by certificate designator
ATA 2450

IAH - FLIGHT 4457 THE CREW REPORTED A BACKUP BATTERY OFF BUSS INDICATION IN FLIGHT. THE AIRCRAFT RETURNED TO IAH WHERE IT LANDED WITHOUT INCIDENT. MAINTENANCE REMOVED AND REPLACED THE BACKUP BATTERY PUSHBUTTON SWITCH, AND CONTACTOR K0305, OPERATIONALLY TESTED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA11IA248 · FAA SDRS
L · 2011-08-01 Matched by certificate designator
ATA 3350

DURING ROUTINE MAINTENANCE THE RIGHT AFT EMERGENCY EXIT SIGN WOULD NOT ILLUMINATE. MAINTENANCE REPLACED THE NR 5 EMERGENCY LIGHT INVERTER. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA11CL179 · FAA SDRS
J · 2011-07-03 Matched by certificate designator
ATA 2450

IAH - FLIGHT 4457 THE CREW REPORTED A BACKUP BATTERY OFF BUSS INDICATION IN FLIGHT. THE AIRCRAFT RETURNED TO IAH WHERE IT LANDED WITHOUT INCIDENT. MAINTENANCE REMOVED AND REPLACED THE BACKUP BATTERY PUSHBUTTON SWITCH, AND CONTACTOR K0305, OPERATIONALLY TESTED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA11IA249 · FAA SDRS
J · 2011-06-15 Matched by certificate designator
ATA 2760

CLE FLT 2521 CREW REPORTED THAT THE SPOILERS OPENED ON TAKEOFF ROLL AT APPROXIMATELY 100 KIAS. THE SPOILERS INDICATED OPEN ON THE EICAS SYSTEM. THE CREW THEN ABORTED THE TAKEOFF AND RETURNED TO THE GATE WITHOUT INCIDENT. CLE MAINTENANCE CHECKED ALL SPOILER PROXIMITY SWITCHES AND LANDING GEAR WHEEL HUBS FOR PROPER INSTALLATION AND OPERATIONAL CHECKS. NO DEFECTS WERE NOTED. CLE MAINTENANCE REMOVED AND REPLACED THE SPOILER CONTROL UNIT. OPERATIONAL CHECKS WERE PERFORMED AND THE DISCREPANCY WAS CLEARED.

Source: SDR C2XA11CL144 · FAA SDRS
L · 2011-03-04 Matched by certificate designator
ATA 3350

SECOND FLOOR PROXIMITY EMERGENCY LIGHT STRIP INOP. REMOVED AND REPLACED NR 3 EMERGENCY LIGHT INVERTER IAW EMB 145 AMM 33-50-11.

Source: SDR C2XA11TY022 · FAA SDRS
J · 2011-01-06 Matched by certificate designator
ATA 3610

IAD FLT 3153 THE CREW REPORTED A BLEED NR 1 OVERTEMP INDICATION IN FLIGHT DURING ICING CONDITIONS. THE AIRCRAFT DIVERTED INTO CLE AND LANDED WITHOUT INCIDENT. MAINTENANCE INSPECTED AND REPLACED THE NR 1 FAN AIR CONTROL THERMOSTAT. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XACL006 · FAA SDRS
L · 2010-11-26 Matched by certificate designator
ATA 2611

FLIGHT 2030 - YYZ - FLIGHT CREW REPORTED LAV SMOKE DETECTOR IN GALLEY TEST INOPERATIVE. EWR MX REMOVED AND REPLACED SMOKE DETECTOR PANEL AND PERFORMED OPERATIONAL CHECK SUCCESSFULLY. ACFT WAS APPROVED TO RETURN TO SERVICE.

Source: SDR C2XA10RI0148 · FAA SDRS
O · 2010-11-26 Matched by certificate designator
ATA 2611

FLIGHT 2030 - EWR - FLIGHT CREW REPORTED SMOKE DETECTOR SWITCH IN GALLEY NOT WORKING. EWR MX REMOVED AND REPLACED GALLEY SMOKE DETECTOR PANEL AND PERFORMED OPERATIONAL CHECK SUCCESSFULLY. ACFT WAS APPROVED TO RETURN TO SERVICE.

Source: SDR C2XA10RI0144 · FAA SDRS
O · 2010-02-22 Matched by certificate designator
ATA 5313

SHV - DURING C-CHECK STR 21R HAS CORROSION AT FR 13. REPAIRED STR 21R IAW EC5310-01507. AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH075 · FAA SDRS
O · 2010-02-22 Matched by certificate designator
ATA 5330

SHV - DURING C-CHECK FUSELAGE SKIN HAS CORROSION AT FR 58 POTABLE WATER SUPPORT DOUBLER MATING SURFACE. REPAIRED SKIN IAW EC5330-02079. AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH076 · FAA SDRS
O · 2010-02-21 Matched by certificate designator
ATA 5751

SHV - DURING C-CHECK LEFT AILERON PCA ATTACHMENT BRACKET HAS MIGRATED HAT BUSHING. REMOVED AND REPLACED ATTACHMENT FITTING IAW EC5750-01177. AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH068 · FAA SDRS
O · 2010-02-21 Matched by certificate designator
ATA 5755

SHV - DURING C-CHECK LEFT O/B GROUND SPOILER ATTACHMENT HAS MIGRATED HAT BUSHING. REMOVED AND REPLACED ATTACHMENT FITTING IAW EMB 145 AMM 57-51-02. AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH067 · FAA SDRS
O · 2010-02-21 Matched by certificate designator
ATA 5320

SHV - DURING C-CHECK CARGO DOOR LOWER CUTOUT HAS CORROSION. REPAIRED CARGO DOOR LOWER CUTOUT IAW EMB 145 SRM 51-40-02. AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH072 · FAA SDRS
O · 2010-02-21 Matched by certificate designator
ATA 5320

SHV - DURING C-CHECK LEFT OMEGA BEAM CORROSION FRM 29-34. REPAIRED LEFT OMEGA BEAM IAW EMB 145 SRM 53-00-10. AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH073 · FAA SDRS
O · 2010-02-21 Matched by certificate designator
ATA 3830

SHV - DURING C-CHECK WASTE DRAIN VALVE SUPPORT HAS CORROSION. REMOVED AND REPLACED SUPPORT IAW EMB 145 SRM 51-40-02. AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH069 · FAA SDRS
O · 2010-02-21 Matched by certificate designator
ATA 5320

SHV - DURING C-CHECK SERVICE DOOR CENTER SILL HAS CORROSION. REPAIRED SERVICE DOOR SILL IAW EMB 145 SRM 51-40-02. AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH071 · FAA SDRS
O · 2010-02-21 Matched by certificate designator
ATA 5320

LT OMEGA BEAM PREVIOUS REPAIR AT FR 20 HAS CORROSION (LEVEL 3). MAINTENANCE REMOVED AND REPLACED PREVIOUS REPAIR WITH NEW REPAIR IAW EC5320-01229. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH061 · FAA SDRS
O · 2010-02-21 Matched by certificate designator
ATA 5320

SHV - DURING C-CHECK LT OMEGA BEAM HAS CORROSION BETWEEN FR 35-38. REPAIRED OMEGA BEAM IAW EMB 145 SRM 51-00-10. AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH070 · FAA SDRS
L · 2010-02-10 Matched by certificate designator
ATA 3350

SHV - DURING C-CHECK RT LOWER EXT EMERGENCY LIGHT INOP. REMOVED AND REPLACED EMERGENCY LIGHT BULB IAW EMB 145 AMM 33-50-10. AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH058 · FAA SDRS
L · 2009-12-30 Matched by certificate designator
ATA 3350

A 12BC UPPER SIDEWALL EMERGENCY LIGHT INOP. REMOVED AND REPLACED EXIT MARKING SIGN ASSY IAW EMB 145 AMM 33-50-14. OPS CHECK GOOD.

Source: SDR C2XA10TY005 · FAA SDRS
B J · 2009-10-12 Matched by certificate designator
ATA 3160

CLL - FLIGHT 2593 - DURING FLIGHT THE CREW REPORTED THAT THE PFD1 CIRCUIT BREAKER POPPED WITH A CHECK PFD1 MESSAGE ON EICAS AND SMOKE COMING FROM UNDER THE PFD1. THE AIRCRAFT LANDED AT CLL WITHOUT INCIDENT WHERE MAINTENANCE REMOVED AND REPLACED THE NUMBER ONE PFD, OPERATIONALLY TESTED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA09IA254 · FAA SDRS
B · 2008-09-16 Matched by certificate designator
ATA 2400

FLIGHT 2654 EWR FLIGHT CREW REPORTED STRONG ELECTRICAL BURNING ODOR IN COCKPIT NOTICED AFTER LANDING. EWR MX R&R RELAY KO437 AND PERFORMED OPS CHECK SUCCESSFULLY. ACFT WAS APPROVED TO RETURN TO SERVICE.

Source: SDR C2XA08RI140 · FAA SDRS
B · 2008-02-26 Matched by certificate designator
ATA 2120

IAH - FLIGHT 2656, DURING PREFLIGHT INSPECTION THE CREW REPORTED A FUEL SMELL IN THE COCKPIT. MAINTENANCE INSPECTED THE AIRCRAFT WITH NO DEFECTS NOTED, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA08IA070 · FAA SDRS
O · 2008-02-16 Matched by certificate designator
ATA 5320

SHV - DURING C-CHECK CENTER OMEGA BEAM HAS CORROSION BETWEEN FR 18-23. MX REMOVED AND REPLACED CENTER OMEGA BEAM AT FR18-23 IAW EMB 145 SRM 51-40-02. THE AIRCRAFT WAS APPROVED TO RETURN FOR SERVICE.

Source: SDR C2XA08SH025 · FAA SDRS
L · 2007-03-02 Matched by certificate designator
ATA 3350

602 NR 482585- RT FWD EXTERIOR EMERGENCY LIGHT AND NR 2 AISLE CEILING EMERGENCY LIGHT INOP. REMOVED AND REPLACED NR 2 BATTERY POWER SUPPLY UNIT IAW EMB 145AMM 33-50-04 OPS CK GOOD. AIRCRAFT RELEASED AND RETURNED TO SERVICE.

Source: SDR C2XA07TY010 · FAA SDRS
L · 2007-02-06 Matched by certificate designator
ATA 3350

DURING MAINTENANCE INSPECTION THE RT FORWARD EMERGENCY EXIT LIGHT WAS FOUND TO BE INOPERATIVE. MAINTENANCE REMOVED AND REPLACED A FUSE IN THE AFFECTED EMERGENCY LIGHT POWER SUPPLY, OPERATIONALLY CHECKED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA07IA029 · FAA SDRS
B J · 2006-12-24 Matched by certificate designator
ATA 5610

BRO FLIGHT 3229 - THE CREW REPORTED SMOKE IN THE COCKPIT WHILE ARRIVING AT THE GATE. THE WINDSHIELD LEADS WERE RESECURED. LATER THAT DAY AT IAH, FLIGHT 3295, THE AIRCRAFT DISPLAYED A WINDSHIELD NR 2 HEAT FAIL MESSAGE. THE WINDSHIELD WAS REPLACED AND THE AIRCRAFT RETURNED TO SERVICE.

Source: SDR C2XA06IA198 · FAA SDRS
L · 2006-04-06 Matched by certificate designator
ATA 3350

EWR - DURING ROUTINE MAINTENANCE FOUND THE AISLE EMERGENCY LIGHT AT ROW 1 - 3 NOT WORKING. REMOVED AND REPLACED EMERGENCY LIGHT BATTERY POWER SUPPLY OVER SERVICE DOOR IAW EMB145 AMM 33-50-04. OPS CHECK GOOD.

Source: SDR C2XA06BT018 · FAA SDRS
O · 2006-03-28 Matched by certificate designator
ATA 5320

SHV - DURING C CHECK, THE LOWER BAGGAGE DOOR CUT OUT BEAM WAS FOUND TO BE CORRODED. MAINTENANCE REMOVED AND REPLACED THE AFFECTED BEAM IAW EMB 145 SRM 51-40-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA06SH040 · FAA SDRS
O · 2006-03-28 Matched by certificate designator
ATA 5320

SHV - DURING C CHECK, THE LEFT OMEGA BEAM LOWER FLANGE WAS FOUND TO BE CORRODED. MAINTENANCE REMOVED THE DAMAGED AREA AND COMPLETED THE REPAIR IAW EMB 145 SRM 51-10-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA06SH042 · FAA SDRS
O · 2006-03-28 Matched by certificate designator
ATA 5320

SHV - DURING C CHECK, THE CENTER OMEGA BEAM LOWER FLANGE WAS FOUND TO BE CORRODED AT FRAME 38. MAINTENANCE REMOVED THE DAMAGED AREA AND INSTALLED A SHIM FILLER REPAIR IAW EMB 145 SRM 53-00-10, STEP 4, FIG 203, SHEET 2. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA06SH041 · FAA SDRS
O · 2006-03-22 Matched by certificate designator
ATA 4910

SHV - DURING C CHECK, THE APU FIREWALL WAS FOUND TO BE CHAFED. DAMAGE WAS FOUND TO BE GREATER THAN 50 PERCENT OF MATERIAL THICKNESS. MAINTENANCE REMOVED THE DAMAGED AREA AND INSTALLED A DOUBLER AND FILLER REPAIR IAW EC 5330-01359, SEC 1.3. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA06SH035 · FAA SDRS
L · 2005-07-14 Matched by certificate designator
ATA 3350

ORF - DURING PREFLIGHT INSPECTION, THE FLIGHT CREW REPORTED THE SERVICE DOOR EXIT SIGN NOT ILLUMINATING WHEN TESTED. MAINTENANCE PERFORMED AN OPERATIONAL CHECK OF THE EMERGENCY EXIT LIGHTING SYSTEM AND THE SERVICE DOOR EXIT SIGN OPERATED NORMALLY WITHOUT ANY DEFECTS NOTED. MAINTENANCE THEN CLEARED THE DISCREPANCY.

Source: SDR C2XA05IA089 · FAA SDRS
O · 2004-06-01 Matched by certificate designator
ATA 5320

DURING C CHECK THE CENTER RAMP ANGLE AT FRAME 20 WAS FOUND TO BE CORRODED. MAINTENANCE REMOVED AND REPLACED THE AFFECTED ANGLE IAW EMB 145 SRM 51-40-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH340 · FAA SDRS
O · 2004-06-01 Matched by certificate designator
ATA 5320

SHV-DURING C CHECK THE SERVICE DOOR FORWARD SILL WAS FOUND TO BE CORRODED. MAINTENANCE REMOVED THE DAMAGED AREA AND PERFORMED A DOUBLER REPAIR IAW SRM 53-21-10, STEP 7 FIG 206. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH339 · FAA SDRS
O · 2004-06-01 Matched by certificate designator
ATA 5315

DURING C CHECK THE RT OMEGA BEAM AFT DOUBLER WAS FOUND TO BE CORRODED AT FRAME 22. MAINTENANCE REMOVED AND REPLACED THE AFFECTED DOUBLER IAW EMB 145 SRM 51-40-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH341 · FAA SDRS
O · 2004-05-29 Matched by certificate designator
ATA 5320

DURING C-CHECK, THE SERVICE DOOR FORWARD SILL WAS FOUND TO BE CORRODED. MAINTENANCE REMOVED THE DAMAGED AREA AND PERFORMED A DOUBLER REPAIR IAW EMB 145 SRM 53-21-10. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH333 · FAA SDRS
O · 2004-05-29 Matched by certificate designator
ATA 5320

DURING C CHECK THE T-REINFORCEMENT ON STRINGER 19R WAS FOUND TO BE CHAFED BETWEEN FRAMES 52 AND 53. MAINTENANCE REMOVED THE DAMAGED AREA AND PERFORMED A DOUBLER REPAIR IAW EMB 145 SRM 53-24-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH331 · FAA SDRS
O · 2004-05-29 Matched by certificate designator
ATA 5330

SHV-DURING C CHECK THE EXTERNAL SKIN WAS FOUND TO BE DENTED AT FRAME 19A AND STRINGER 12L. MAINTENANCE PERFORMED A DOUBLER REPAIR TO THE AFFECTED AREA IAW EMB 145 SRM 53-22-01 STEP 6 FIGURE 206. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH332 · FAA SDRS
O · 2004-05-29 Matched by certificate designator
ATA 5320

DURING C-CHECK, THE CARGO DOOR LOWER SILL WAS FOUND TO BE CORRODED. MAINTENANCE REMOVED AND REPLACED THE AFFECTED SILL IAW EMB 145 SRM 51-40-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH334 · FAA SDRS
O · 2004-05-29 Matched by certificate designator
ATA 5315

DURING C CHECK THE CENTER OMEGA BEAM WAS FOUND TO BE CORRODED AT FRAME 20. MAINTENANCE REMOVED AND REPLACED THE AFFECTED BEAM IAW EMB 145 SRM 51-40-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH330 · FAA SDRS
O · 2004-05-27 Matched by certificate designator
ATA 5315

SHV-DURING C CHECK THE SHELL PLATE ON TOP OF THE CENTER OMEGA BEAM AT FRAME 23 WAS FOUND TO BE CORRODED. MAINTENANCE REMOVED AND REPLACED THE SHELL PLATE IAW EMB 145 SRM 51-40-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH325 · FAA SDRS
O · 2004-05-27 Matched by certificate designator
ATA 4910

DURING C-CHECK THE APU FIREWALL WAS FOUND TO BE CRACKED AT THE RT UPPER APU MOUNT. MAINTENANCE REMOVED THE DAMAGED AREA AND PERFORMED A DOUBLER REPAIR IAW EMB 145 SRM 53-32-13 SECTION 4 FIGURE 203. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH324 · FAA SDRS
O · 2004-05-27 Matched by certificate designator
ATA 5210

SHV-DURING C CHECK THE MAIN DOOR FORWARD U-BRACKET WAS FOUND TO BE CORRODED. MAINTENANCE REMOVED AND REPLACED THE AFFECTED BRACKET IAW EMB 145 SRM 51-40-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH327 · FAA SDRS
O · 2004-05-27 Matched by certificate designator
ATA 5210

SHV-DURING C CHECK THE MAIN DOOR AFT U-BRACKET WAS FOUND TO BE CORRODED. MAINTENANCE REMOVED AND REPLACED THE AFFECTED BRACKET IAW EMB 145 SRM 51-40-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH328 · FAA SDRS
O · 2004-05-27 Matched by certificate designator
ATA 5315

SHV-DURING C CHECK THE LT OMEGA BEAM WAS FOUND TO BE CORRODED AT FRAME 20. MAINTENANCE REMOVED THE DAMAGED AREA AND PERFORMED A DOUBLER REPAIR IAW EMB 145 SRM 53-21-10. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH326 · FAA SDRS
O · 2004-05-27 Matched by certificate designator
ATA 5320

SHV-DURING C CHECK THE T REINFORCEMENT ON EXTERNAL STRINGER 19L WAS FOUND TO BE GOUGED. MAINTENANCE REMOVED THE DAMAGED AREA AND PERFORMED A DOUBLER REPAIR IAW EMB 145 SRM 53-24-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH323 · FAA SDRS
O · 2004-05-26 Matched by certificate designator
ATA 7160

DURING C-CHECK THE NR 2 INTAKE WAS FOUND TO BE GOUGED AT 12 O'CLOCK. MAINTENANCE REMOVED THE DAMAGED AREA AND INSTALLED A CHAFE STRIP IAW EC 5410-01067. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH322 · FAA SDRS
O · 2004-05-26 Matched by certificate designator
ATA 5320

SHV - DURING C-CHECK THE SERVICE DOOR CENTER SILL WAS FOUND TO BE CORRODED. MAINTENANCE REMOVED THE DAMAGED AREA AND PERFORMED A DOUBLER REPAIR IAW EMB 145 SRM 53-21-02. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH320 · FAA SDRS
O · 2004-05-26 Matched by certificate designator
ATA 7160

SHV - DURING C-CHECK THE NR 1 ENGINE INTAKE COWLING MOUNTING FLANGE WAS FOUND TO BE GOUGED. MAINTENANCE REMOVED THE DAMAGED AREA AND INSTALLED A CHAFE STRIP IAW EC 5410-01067. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA04SH321 · FAA SDRS
L · 2003-10-22 Matched by certificate designator
ATA 3350

CLE FLIGHT 2317 THE CREW REPORTED THE EMERGENCY LIGHTS WERE INOPERATIVE. MAINTENANCE REPLACED THE INVERTER. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA03CL176 · FAA SDRS
L · 2003-09-10 Matched by certificate designator
ATA 3350

CLE FLIGHT 2058 THE CREW REPORTED 2 EMERGENCY AISLE PATH LIGHT STRIPS WERE INOPERATIVE. MAINTENANCE REPLACED THE NR 3 EMERGENCY LIGHT INVERTER. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA03CL162 · FAA SDRS
L · 2003-08-05 Matched by certificate designator
ATA 3350

CLT FLIGHT NR 2223 THE CREW REPORTED NR 1 FLOOR PROXIMITY STRIP INOP. MAINTENANCE REPLACED THE NR 2 EMERGENCY LIGHT INVERTER,OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA03CL137 · FAA SDRS
L · 2003-07-14 Matched by certificate designator
ATA 3397

THE CREW REPORTED THE FIRST ROW OF EMERGENCY LIGHTS WILL NOT ILLUMINATE. MAINTENANCE RESECURED WIRE, OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA03CL124 · FAA SDRS
L · 2003-05-24 Matched by certificate designator
ATA 3350

CLE FLIGHT 2104 THE CREW REPORTED THE FIRST SECTION OF AISLE PATH LIGHTING WAS INOPERATIVE. MAINTENANCE INSPECTED AND REPLACED THE EMERGENCY LIGHT INVERTER. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA03CL103 · FAA SDRS
F · 2002-08-03 Matched by certificate designator
ATA 2750

CREW REPORTED THAT ON DESCENT THE FLAPS WOULD NOT EXTEND. THE AIRCRAFT ACCOMPLISHED AN EMERGENCY DESCENT AND LANDED AT IAH WITHOUT INCIDENT. MAINTENANCE FOUND THE LEFT FLAP TRANSMISSION BRAKE TO HAVE FAILED. THE AFFECTED FLAP BRAKE WAS REMOVED AND REPLACED, THE SYSTEM OPERATIONALLY CHECKED, AND THE AIRCRAFT RETURNED TO SERVICE.

Source: SDR C2XA02IA155 · FAA SDRS