N116AA

CESSNA 525B · 2007 · Valid Registration

Registered owner: CORSAIR TWO LLC, OR (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AERO AIR LLC (O9IA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

E O · 2022-04-02 Matched by certificate designator
ATA 5280

DURING CRUISE FROM KGEG TO KBFI, PILOT REPORTED A VIBRATION IN THE AIRCRAFT THAT CORRESPONDED TO AIRCRAFT SPEED. NO OTHER ABNORMALITIES DURING FLIGHT. UPON LANDING AND A POST FLIGHT WALK AROUND, IT WAS NOTED THAT THE LH NOSE GEAR DOOR APPEARED TO BE LOOSE. FURTHER INSPECTION REVEALED THE NOSE GEAR DOOR TORQUE TUBE HAD BROKEN FROM ITS WELD AT THE PIVOT POINT ON THE LH CONNECTION. THE TORQUE TUBE WAS REMOVED AND REPLACED WITH THE NEW -10 UNIT PER THE AMM. OPERATIONAL CHECKS WERE GOOD AND NO VIBRATIONS IN FLIGHT. NO FURTHER ACTION REQUIRED.

Source: SDR 2022FA0000187 · FAA SDRS
N · 2019-01-30 Matched by certificate designator
ATA 2611

ON APPROACH INTO ANC FROM BFI, AT ABOUT 8000 FT, THE BAGGAGE SMOKE RED LIGHT ILLUMINATED. THERE WAS NO SIGN OF SMOKE. LANDING WAS UNEVENTFUL. BATTERIES WERE TURNED OFF AND THEN BACK ON. LIGHT WAS NO LONGER ILLUMINATED. MAINT WAS CONTACTED AND INSPECTED THE SYSTEM AND FOUND NO DISCREPANCIES. MAINT TALKED WITH TECH SUPPORT AND THEN PERFORMED A TROUBLESHOOTING CHECKS PER AMM CH 26-11-00. NO FAULTS WERE FOUND. NO SMOKE SMELL WAS NOTED IN THE BAGGAGE COMPARTMENT EITHER. BOTH ENGINES WERE RUN UP FOR ABOUT 10 MINUTES AND LIGHT DID NOT COME BACK ON. AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR O9IA2018013019 · FAA SDRS
O · 1999-02-26 Unresolved
ATA 5320

TUL - FOUND CORROSION INSIDE SIDE STRUT BLOCK ATTACHMENT HOLES. AREA LOCAL BLENDED AND TREATED PER AA ESO 7349 DAGED 2-26-99. (M)

Source: SDR AALA990295 · FAA SDRS
J · 1998-12-18 Unresolved
ATA 3010

HNL - FLT 938 - UPON ENTERING AREA OF POSSIBLE ICING WE TURNED ON WING ANTI-ICE. AFTER ABOUT 30 SECONDS TO 1 MINUTE MANIFOLD NR 1 FAIL LIGHT CAME ON, COMPLETED, CHECKLIST. AIRCRAFT RETURNED TO HNL, WHERE IT MADE AN UNEVENTFUL LANDING. (M)

Source: SDR HALA9800420 · FAA SDRS
B · 1998-10-25 Unresolved
ATA 2510

SFO - FLT 11 - SMOKE IN COCKPIT. REMOVED AND REPLACED FE SEAT, OPS CHECK GOOD. (M)

Source: SDR HALA9800364 · FAA SDRS
J · 1998-05-31 Unresolved
ATA 2131

SEA - FLT 21 - AFTER TAKEOFF FROM SEA TO HNL, AIRCRAFT WAS UNABLE TO PRESSURIZE IN ANY MODE. AIRCRAFT RETURNED TO SEA WHERE AN UNEVENTFUL LANDING WAS MADE. REPLACED AUTOPRESSURE CONTROLLER. OPS CHECK AND LEAK CHECK OK. (X)

Source: SDR HALA9800138 · FAA SDRS
O · 1998-05-07 Unresolved
ATA 5711

LAX - FLT 09 - RIGHT WING CRACKED N THE REAR SPAR CAP WEB NEAR XORS 433/402. INSTALLED FUEL TANK REPAIR DOUBLER PER ES07349, DATED 5-7-98. (X)

Source: SDR HALA9800112 · FAA SDRS
K B · 1997-12-07 Unresolved
ATA 4930

FLT 25 - HNL - HEAVY SMELL OF KEROSENE IN COCKPIT AND CABIN AFTER A/C ARRIVED AT GATE. FOUND FUEL LINE TO APU LEAKING AT 'B' NUT. TIGHTENED 'B' NUT. REPLACED PACKINGS NR 1, NR 2, AND NR 3. RAN ENGINE AT GATE, OK FOR SERVICE. (M)

Source: SDR HALA9700300 · FAA SDRS
O · 1996-11-11 Unresolved
ATA 5320

DURING C-CHECK, FOUND CORROSION ON INTERCOSTAL BETWEEN VERTICAL FRAMES ABOVE THE ACCESS DOOR 115AZ AT STATION 464. INSTALLED ANGLE DOUBLER PER SRM 53-00-01 VOL 1. (M)

Source: SDR HAL960110 · FAA SDRS
O · 1996-11-11 Unresolved
ATA 5720

DURING C-CHECK, FOUND CORROSION ON THE FALSE SPAR AFT INBOARD SIDE AT STATION XORS 164 TO STATION XORS 197. INSTALLED 'L' ANGLE DOUBLERS ON UPPER AND LOWER FALSE SPAR PER ESO 7349, DATED 11-8-96. (M)

Source: SDR HAL960109 · FAA SDRS
O · 1996-11-11 Unresolved
ATA 5320

DURING C-CHECK, FOUND CORROSION AT AFT END OF RIGHT CABLE TRACK. INSTALLED NEW TRACK PER SRM 51-01-00-05. (M)

Source: SDR HAL960105 · FAA SDRS
O · 1996-11-11 Unresolved
ATA 5313

DURING C-CHECK, FOUND CORROSION ON LONGERON 48R AND INTERCOSTAL AT LONGERON 48R. INSTALLED NEW INTERCOSTAL AND LONGERON 48R PER AARD 51-01-00. (M)

Source: SDR HAL960104 · FAA SDRS
O · 1996-11-09 Unresolved
ATA 5751

DURING C-CHECK, FOUND LEFT INBOARD AILERON ACTUATOR CASTING CRACKED AT THE LOWER AFT INBOARD END. REPAIRED PER ESO 7349 DATED 11-1-96. (M)

Source: SDR HAL960103 · FAA SDRS
O · 1996-11-08 Unresolved
ATA 5720

DURING C-CHECK, FOUND CORROSION IN THE AREA FOR BARREL NUTS OF THE TRAPEZOIDAL PANEL RIGHT MLG. INSTALLED INBOARD AND OUTBOARD BARREL NUT BUSHINGS PER SRM 57-20-00. BLENDED AREAS PER ESO 7349 DATED 11/1/96. (M)

Source: SDR HAL960101 · FAA SDRS
O · 1996-11-08 Unresolved
ATA 5320

DURING C-CHECK, FOUND THE 'U' CHANNEL SUPPORT HAS CORROSION FROM LONGERON 51L TO 51R ON THE BELL FRAME AT STATION 1139. SPLICED IN NEW SECTION OF 'U' CHANNEL PER SRM 53-30-00. (M)

Source: SDR HAL960107 · FAA SDRS
O · 1996-11-08 Unresolved
ATA 5320

DURING C-CHECK, FOUND CORROSION ON SHEAR TIE BELOW FRAME 979 ON AFT SIDE. REMOVED AND REPLACED SHEAR TIE PER SRM 51-01-00-5. (M)

Source: SDR HAL960102 · FAA SDRS
O · 1996-11-05 Unresolved
ATA 5311

CORROSION AND CRACKS ON FRAME AT STATION 1278 BETWEEN LONGERONS 52L AND 52R. REMOVED CORROSION PER SRM 51-21-01 AND INSTALLED DOUBLER PER SRM 51-00-01 PAGE 124D. (M)

Source: SDR HAL960099 · FAA SDRS
O · 1996-11-05 Unresolved
ATA 5320

MID LAVATORY FLOOR PAN HAS CORROSION ON FORWARD SIDE. REMOVED AND REPLACED PAN IAW ESO 7349. (M)

Source: SDR HAL960100 · FAA SDRS
O · 1996-11-04 Unresolved
ATA 5320

DURING C-CHECK, FOUND CORROSION ON AFT SIDE OF SHEAR TIE BELOW FRAME AT STATION 939, LONGERON 49 RIGHT TO 49 LEFT. REMOVED CORRODED SECTION OF SHEAR TIE AND INSTALLED NEW SECTION PER SRM 53-30-00. (M)

Source: SDR HAL960097 · FAA SDRS
O · 1996-11-01 Unresolved
ATA 5313

LONGERON 52 FROM STATION 1139 TO 1156 IS CORRODED BEYOND LIMITS. REMOVED AND REPLACED LONGERON PER SRM 51-01-00-05. (M)

Source: SDR HAL960094 · FAA SDRS
O · 1996-10-31 Unresolved
ATA 5720

UNDERSIDE OF LEFT WING JUST OUTBOARD OF MLG STRUT DOOR TAPER LOCK FASTENER HEAD CORRODED. INSTALLED DOUBLER (ESO 7349) CORROSION PROTECT THE RE-WORKED AREA PER SRM VOL 2 CHAPTER 51-21-01. (M)

Source: SDR HAL960095 · FAA SDRS
O · 1996-10-31 Unresolved
ATA 5313

STRINGER 48L CORRODED AT LOWER FLANGE FAST HOLES. CLEANED CORROSION AND ADDED STRAP TO 48L PER SRM 51-00-01 PAGE 10, SRM 51-01-00-03 PAGE 1 FIG 1A (SHEET 1) FIG 80 SHEET 1, FIG 1 SHEET 6. (M)

Source: SDR HAL960096 · FAA SDRS
O · 1996-10-28 Unresolved
ATA 5311

CORROSION ON BELT FRAME STATION 999 AFT SIDE BETWEEN LONGERONS 49R AND 48L. REMOVED CORRODED SECTION OF LOWER FRAME 'J' ANGLE AND INSTALLED SPLICE REPAIR PER SRM 51-22-00 AND 53-30-00. (M)

Source: SDR HAL960092 · FAA SDRS
O · 1996-10-22 Unresolved
ATA 5347

DEEP CORROSION 3.5 INCHES ALONG INBOARD SIDE OF NR 4 SEAT TRACK LOCATED BETWEEN STATION 439 AND STATION 469, A ZONE CABIN FLOOR. REMOVED AND REPLACED NR 4 SEAT TRACK AT LOCATION BETWEEN STATION 439 AND 469 AARD 51-01-00-05. (M)

Source: SDR HAL960091 · FAA SDRS
O · 1996-10-21 Unresolved
ATA 5320

LEFT FLOOR SUPPORT FRAME HAS CORROSION AT STATION 1621 UNDER NR 1 ROLLER TRACK. INSTALLED DOUBLER AT STATION 1621 ON LEFT END OF FLOOR SUPPORT FRAME UNDER ROLLER TRACK REF SRM 53-30-00. (M)

Source: SDR HAL960090 · FAA SDRS
B · 1996-06-24 Unresolved
ATA 2150

HNL - FLT 12 - SMOKE AND OIL SMELL IN CABIN ON GROUND PRIOR TO DEPARTURE. *SUPPLEMENTAL SDR TO SHOW FINAL CLOSING ACTION*. REMOVED NRS 1, 2, 3 AIR CONDITIONER COALESCER BAGS AND PURGED AIRCRAFT SYSTEM PER MM 21-10-00. REPLACED COALESCER BAGS AND THE OPERATIONAL CHECK AND LEAK CHECK GOOD. THE APU OIL SMOKE AND OIL SMELL RETURNED AND THE APU WAS PLACARDED INOPERATIVE. A NEW APU WAS SENT TO SFO AND AN APU CHANGE IS SCHEDULED FOR JUNE 28, 1996. THE APU WAS CHANGED ON JUNE 28 AS SCHEDULED. THE AIRCRAFT IS IN SERVICE. (X)

Source: SDR HAL9679 · FAA SDRS