N116WJ
Operators of this aircraft
Who operated this tail, and how firmly we know it.
No operator established for this aircraft.
Accident & incident history
No NTSB accidents or incidents on file for this aircraft.
Maintenance disclosures
ACFT DEPARTED. NO ISSUES DURING CLIMB. WHILE PASSING THRU FL 240, IT WAS OBSERVED THE ACFT HAD EXCESSIVE NOSE UP TRIM. AUTOPILOT ENGAGED AT THE TIME. THE ACFT, ASIDE FROM TRIM, FLEW NORMALLY. LEVELED OFF AT FL 410. AT CRUISE, AUTOPILOT HELD ACFT LEVEL, BUT TRIM WAS STILL FULL NOSE UP. DURING DESCENT, THE AUTOPILOT DESCENDED THE ACFT, BUT TRIM WENT FULL NOSE DOWN. THE PILOT PULLED BACK ON YOKE SO THE ACFT WOULDN'T NOSE OVER. THE PILOT STATED AT THIS TIME THE FGC COMPUTERS FAILED. CREW WENT TO MANUAL & HAD DIFFICULTY FLYING THE AIRCRAFT WITH FULL AFT TRIM. FULLY CONFIGURED THE TRIM WAS FULL NOSE UP. THE PILOT STATES HAD TO PUT AN EXTREME AMOUNT OF FORCE TO PREVENT THE AIRCRAFT FROM NOSING OVER. MX WAS NOTIFIED AND FOUND THAT FASTENERS SHEARED ON THE LOWER PORTION OF THE TRIM DRIVE SHAFT ASSEMBLY TORQUE TUBE PART NUMBER 43083-818 LOCATED IN THE COCKPIT PEDESTAL.