N119AX

BEECH 1900C · 1988 · Valid Registration

Registered owner: ALASKA CENTRAL EXPRESS INC, AK (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ALASKA CENTRAL EXPRESS INC (YADA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

K · 2023-06-22 Matched by certificate designator
ATA 7314

PILOT REPORTED OIL LEAKING OUT OF RIGHT ENGINE. MAINTENANCE DISCOVER #2 ENGINE OIL SCAVENGE PUMP HAVING A PINHOLE LEAK AND THE HOUSING WAS REPLACED. INSPECTION DETERMINED THAT CAVITATION EROSION OF THE PUMP BODY IN A CORNER OF THE CAVITY HAD CREATED A HOLE. THIS IS FREQUENT ON THESE PUMP HOUSINGS. POST REPLACEMENT OF PUMP HOUSING LEAK CHECK WAS GOOD.

Source: SDR YADA2023071301 · FAA SDRS
O · 2017-12-05 Matched by certificate designator
ATA 5712

WHILE PERFORMING HEAVY MAINTENACE VISUAL INSPECTION FOUND LARGE CRACK ON LEFT HAND WING INBOARD LEADING EDGE RIB P/N: 114-120033-45. MAINTENANCE REMOVED AND REPLACED LEADING EDGE RIB IAW BEECH SRM.

Source: SDR YADA20171205001 · FAA SDRS
O · 2017-09-01 Matched by certificate designator
ATA 2730

PILOT REPORTED THAT THE ELEVATOR (PITCH) FROZE OR BOUND UP WHILE IN CRUISE FLIGHT FROM (ANC) FLYING INTO (SDP). MECHANIC REMOVED FLOOR BOARDS IN TAIL SECTION AND INSPECTED PULLEYS AND CABLES. FOUND PUDDLES OF WATER IN ZONES 5&6 AND ALSO BY ELEVATOR PULLEYS JUST AFT OF AFT PRESSURE BULKHEAD. WATER WAS CLEANED AND REMOVED FROM AREAS, FUNCTIONAL CHECK OF FLIGHT CONTROLS WERE SUCCESSFUL.

Source: SDR YADA20170905001 · FAA SDRS
O · 2017-02-16 Matched by certificate designator
ATA 2750

FLAPS FAILED TO EXTEND.

Source: SDR YADA20170216001 · FAA SDRS
B · 2016-12-31 Matched by certificate designator
ATA 2121

SMELL OF POSSIBLE ELECTRIC ON CLIMB.

Source: SDR YADA20161231001 · FAA SDRS
I · 2015-12-15 Matched by certificate designator
ATA 3421

COPILOT ATTITUDE INDICATOR SHOWING 5 - 10°, BANK TO RIGHT DURING LEVEL FLIGHT. RETURN TO AIRPORT OF DEPARTURE. REPLACED INOPERATIVE ATTITUDE GYRO, CHECKED GOOD.

Source: SDR YADA20151215001 · FAA SDRS
B · 2015-09-04 Matched by certificate designator
ATA 2197

PILOT REPORTED ELEC SMELL IN COCKPIT AFTER DEPARTURE. RETURNED TO ORIGINAL AIRPORT FOR UNEVENTFUL LANDING. LOCATED A PINCHED & SHORTED WIRE ON THE AFT RECIRCULATING FAN AT THE RESISTOR STACK. FAN UNIT REPLACED.

Source: SDR YADA20150904001 · FAA SDRS
K B · 2015-05-22 Matched by certificate designator
ATA 7921

PILOT REPORTED APPEARANCE OF SMOKE IN COCKPIT AT TOUCHDOWN. REPORTED AS POSSIBLY COMING FROM BLEED AIR, OILY SMELL. CORRECTED AN OIL LEAK AT THE LT OIL COOLER INBD FITTING & REPLACED O RING AT FITTING, CLEANED DUCTING AS REQUIRED. OIL LINE AT LEAKING FITTING WITH THIS O RING WAS REMOVED & REINSTALLED 13.3 FLIGHT HOURS PRIOR, FOR OTHER MX.

Source: SDR YADA20150522001 · FAA SDRS
S · 2015-01-23 Matched by certificate designator
ATA 2720

NOSE WHEEL STEERING VERY DIFFICULT TO USE. HARD TO MANIPULATE RUDDER PEDALS WHILE ON GND. FOUND LT RUDDER BELLCRANK MOUNT BRACKET LOOSE WITH ONE CRACKED MOUNT EAR, ALLOWING BELLCRANK TO RUB. REPLACED BRACKET & COMPLIED WITH RECOMMENDED SERVICE BULLETIN SB27-3895. REPLACEMENT OF BRACKET MOUNTING HARDWARE.

Source: SDR YADA20150123001 · FAA SDRS
O · 2014-12-22 Matched by certificate designator
ATA 5210

PILOT REPORTED AIR STAIR DOOR OPERATION VERY STIFF, INSIDE DOOR HANDLE BROKE WHILE TRYING TO OPEN. REPLACED DOOR HANDLE & LUBED DOOR SYS.

Source: SDR YADA20141222001 · FAA SDRS
B · 2014-06-11 Matched by certificate designator
ATA 2121

AFTER TAKEOFF PILOT REPORTED THAT HE SAW SMOKE & COULD SMELL FUMES IN COCKPIT. PILOT DECLARED EMERGENCY & RETURNED TO DEPARTURE AIRPORT ANC WITHOUT INCIDENT. MX IDENTIFIED THE SOURCE OF THE SMELL AS FAILED BEARINGS LOCATED THE FWD VENTILATION BLOWER, NO DAMAGE DISCOVERED. REPLACED THE FAILED BLOWER & THE FLIGHT CREW PERFORMED A SATISFACTORY OPERATIONAL CHECK FLIGHT. THE ACFT WAS THEN RETURNED TO SERVICE.

Source: SDR YADA20140611001 · FAA SDRS
O · 2014-04-11 Matched by certificate designator
ATA 5751

CRACK FOUND IN RT AILERON BALANCE WEIGHT CLIP WHILE PERFORMING BORESCOPE INSPECTION OF CLIP.

Source: SDR YADA2014041461319 · FAA SDRS
N · 2012-12-12 Matched by certificate designator
ATA 5270

AIRCRAFT DEPARTED, ON REACHING AN ALTITUDE OF 20,000 FT THE FORWARD ENTRY DOOR WARNING ANNUNCIATOR ILLUMINATED. THE CREW BURNED OFF EXECESS FUEL AND RETURNED TO BASE. MX PERSONNEL FOUND THE UPPER DOOR AJAR WARNING SWITCH BRACKET WAS BENT. THE BRACKET WAS STRAIGHTENED AND THE SWITCH WAS READJUSTED. THE DOOR WARNING SYSTEM OPERATIONALLY CHECKED GOOD AND THE AIRPLANE WAS RELEASED FOR SERVICE.

Source: SDR 2012F00266 · FAA SDRS
R J · 2012-02-16 Matched by certificate designator
ATA 7210

DURING FLIGHT 765, ENROUTE, THE PILOT OBSERVED TORQUE SURGES OF 400 FT LBS. TO 1,000 FT LBS. ON THE NR 1 ENGINE. THE ENGINE WAS SHUTDOWN AND THE FLIGHT CONTINUED ON TO ANC. ON LANDING, MX FOUND THE OIL FILTER CONTAMINATED WITH METAL DEBRIS AND CHUNKS OF WHAT APPEARS TO BE PARTS OF A BEARING RACE AT THE REDUCTION GEAR BOX SCREEN. THE ENGINE WILL BE REMOVED AND SENT TO THE MFG FOR EVALUATION.

Source: SDR YADA2012F00054 · FAA SDRS