N11QF

EUROCOPTER EC 130 B4 · 2002 · Valid Registration

Registered owner: NEVADA HELICOPTER LEASING LLC, CO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
HELICOPTER CONSULTANTS OF MAUI, LLC. (HCMA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2009-11-17 Matched by certificate designator
ATA 6320

ACFT DEPARTED AIRPORT ON A SIGHT SEEING FLIGHT AT 11:54 AM, SHORTLY BEFORE RETURNING, AT APPROX 12:40 PM AT 1,000 FT AGL THE ENGINE "CHIP" LIGHT ILLUMINATED, THE PILOT REDUCED POWER AND WITHIN 4 TO 5 SECONDS ADDITIONAL CAUTION LIGHTS ILLUMINATED AND THE AURAL WARNING ACTIVATED. PILOT REPORTED ENGINE POWER LOSS AND PROCEDED TO EXECUTE A "POWER OFF" AUTOROTATION LANDING AT APPROX 3/4 OF A MILE FROM AIRPORT WITH NO FURTHER INCIDENT. NO INJURIES OCCURRED TO PILOT OR PASSENGERS. MX WAS DISPATCHED TO SIGHT. INSP REVEALED EXCESSIVE METAL ON THE MODULE 1 ACCESSORY GB MAGNETIC PLUG, THE ENG ELECTRICAL CHIP PLUG AND SMALL AMOUNTS OF METAL ON MODULE 5 MAGNETIC PLUG AND OIL TANK MAG PLUG. INSPECTIONS ALSO REVEALED THAT THE FREE TURBINE AND AXIAL COMPRESSOR ROTATED FREELY BY HAND AND THE ENG OIL LEVEL WAS NORMAL. FURTHER INVESTIGATION REVEALED THAT WHEN THE AXIAL COMPRESSOR WAS ROTATED THE STARTER GEN AND ACCESSORY DRIVES WERE NOT ROTATING, INDICATING A POSSIBLE INTERNAL FAILURE OF THE MODULE 1 ACCESSORY GB. (TSO 1318.1 AT TIME OF INCIDENT.

Source: SDR HCM2009F00001 · FAA SDRS
E J · 2006-03-18 Unresolved
ATA 7320

PRECAUTIONARY LANDING DUE TO BANG HEARD IN FLIGHT BY PILOT. NORMAL LANDING ACCOMPLISHED W/O ACCIDENT, OR INJURIES. AC LANDED ON PRIVATE PROPERTY. UPON LANDING, GOVERNOR WARNING LIGHT ILLUMINATED. SUBSEQUENT INVESTIGATIVE TROUBLESHOOTING REVEALED VEMD TO DISPLAY A CODE (192) HMU FAULT, INDICATING A FAILURE OF EBCAU STEPPER MOTOR. VISUALLY INSPECTED ENG ASSY AND SURGE BLEED VALVE ASSY. NO DEFECTS NOTED, HMU AND EBCAU UNITS WERE REPLACED WITH SERVICABLE UNITS. GROUND AND FLIGHT TESTS PROVED GOOD WITH NO INDICATED ERROR CODES. AC TEST FLOWN BACK TO MAINTENANCE BASE WITH NO FURTHER PROBLEMS NOTED. DETERMINED THE INITIAL BANG HEAR IN FLIGHT WAS MOST LIKELY A COMPRESSOR STALL DUE TO THE MALFUNCTION HMU. (K)

Source: SDR 2006FA0000355 · FAA SDRS