N121KL
Operators of this aircraft
Who operated this tail, and how firmly we know it.
| Operator | Role | Period | Basis |
|---|---|---|---|
| AIRCRAFT CHARTER SERVICES INC (A59A) | Certificate holder | — | Matched by certificate designator |
Accident & incident history
No NTSB accidents or incidents on file for this aircraft.
Maintenance disclosures
RH ENGINE WOULD NOT START (HUNG START) IN AUTO. ENGINE WOULD START IN MANUAL MODE. TROUBLESHOT FOUND MOTIVE FLOW PRESSURE LOW. EMERGENCY FUEL SHUTOFF UNIT WAS RESTRICTING MOTIVE FLOW WHICH REDUCED IDLE FLOW PRESSURE TO THE FCU.
WHILE USING LIFE VEST CERTIFIED 1/16/2018 FOR TRAINING FOUND THAT THE C02 INFLATOR CARTRIDGE WAS TO RIGID TO BE PUNCTURED TO INFLATE THE VEST.
DURING START, THE ANTI-ICE LIGHT WARNING ILLUMINATED. FOUND THE STATOR ICE VALVE FAILED.
PILOTS ATTEMPTED START AND START HUNG AT 16%. SAW ITT RISE HOWEVER ENGINE WOULD NOT ACCELERATE. REMOVED EEC AND INSTALLED ON LT ENGINE PROBLEM FOLLOWED.
PILOTS REPORTED THAT AS FUEL WAS BURNED THE LEFT QUANTITY WOULD STOP SHOWING BURN AT AROUND 2300 AND THE RIGHT SIDE WOULD CONTINUE TO SHOW FUEL BURNED. AS THE RH SIDE SHOWED ABOUT 1100 THE LEFT WOULD DRIFT DOWN TO 1100. SYSTEM FUNCTIONED NORMAL ABOVE AND BELOW THESE PARAMETERS. REMOVED ACCESS PANELS FROM WING. FOUND NR 4 PROBE LAYING IN WING OFF OF MOUNT. FOUND MOUNT TO BE SERVICEABLE AND NOT DEFECTIVE. APPEARS PROBE WAS REMOVED FOM AND NOT REINSTALLED IN MOUNTING. REINSTALLED PROBE AND TESTED SYSTEM. SYSTEM TESTED WITHIN SPECIFICATIONS.