N124AX

BEECH 1900C · 1991 · Valid Registration

Registered owner: ALASKA CENTRAL EXPRESS INC, AK (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ALASKA CENTRAL EXPRESS INC (YADA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2023-03-09 Matched by certificate designator
ATA 2730

WHILE PERFORMING A COMPANY FLEET CAMPAIGN DISCOVERED FORWARD ELEVATOR BELLCRANK CRACKED WEB.

Source: SDR YADA20230313003 · FAA SDRS
S · 2021-12-31 Matched by certificate designator
ATA 3243

PILOT REPORT - CAPTAINS LEFT BRAKE PEDAL LOOSES PRESSURE AND GOES TO FLOOR - NO BRAKE. MAINTENANCE REPLACED THE CAPTAINS LEFT BRAKE MASTER CYLINDER.

Source: SDR YADA2021123101 · FAA SDRS
O · 2019-06-29 Matched by certificate designator
ATA 7603

PILOT REPORTED THAT WHILE ON TAXI OFF THE BLOCK THAT AFTER LIFTING THE LEFT HAND POWER LEVER INTO GROUND FINE, IT BECAME STUCK. THE LEFT POWER LEVER WOULD NOT MOVE AND NEITHER WOULD THE RIGHT POWER LEVER. AIRCRAFT RETURNED TO PARKING BLOCK AND ENGINE WERE SHUT DOWN WITH NO FURTHER DISCREPANCIES. MAINTENANCE FOUND DURING TROUBLESHOOTING THAT THE POWER LEVER DETENT SUPPORT BLOCK WAS MISSING A SCREW THAT HELD IT IN PLACE ON THE CENTER COLUMN AND CAUSED THE THROTTLE GUIDE PINS TO BIND. RESET THROTTLES AND INSTALLED NEW SCREW AND ENGINE OPERATIONAL CHECKS WERE SUCCESSFUL.

Source: SDR YADA20190630001 · FAA SDRS
O · 2019-06-06 Matched by certificate designator
ATA 7600

LEFT HAND CONDITION CABLE ASSEMBLY SUFFERED AN INCREASE IN FRICTION TO POINT OF ROD END FAILURE AT THE CONTROL LEVER WITH IN 30 DAYS OF INSTALL.

Source: SDR YADA2019060600214 · FAA SDRS
E · 2019-03-17 Matched by certificate designator
ATA 7603

PILOT REPORT: UPON DEPARTURE, THE LEFT ENGINE SURGED TO MAX TRANSIENT POWER WHERE WE SHUT DOWN THE ENGINE. IT WAS STARTING TO SHAKE AND DEEMED UNSAFE. TORQUE READING INDICATED 5000 LBS AND 840 ITT FOR ABOUT 13 SECONDS UNTIL MANUALLY SHUT DOWN NR 1 ENGINE. RIGHT ENGINE DID NOT EXCEED ANY LIMITATIONS. AIRCRAFT WAS LANDED OVERWEIGHT BUT WITHOUT FURTHER INCIDENT. MAINTENANCE PERFORMED TROUBLESHOOTING AND FOUND NR 1 ENGINE FUEL CONTROL ROD, AFT ROD END HAD SEPARATED AT BEARING AND CAUSED LOSS OF ENGINE POWER LEVER CONTROL. PILOT SHUT DOWN ENGINE.

Source: SDR YADA20190317001 · FAA SDRS
J · 2018-08-17 Matched by certificate designator
ATA 7930

PILOT REPORTED THE RT ENGINE OIL PRESSURE WAS OBSERVED TO BE SHOWING 65 PSI AFTER TAKEOFF. NO EMERGENCY WAS DECLARED, AIRCRAFT LANDED WITHOUT INCIDENT. REPLACED THE NR 2 ENGINE MAIN OIL FILTER AND THEN CLEANED CONTAMINATION OUT OF THE OIL PRESSURE TRANSMITTER CONNECTOR. GROUND RAN, AND OBSERVED THE CORRECT OIL PRESSURE AND AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR YADA2018082017001 · FAA SDRS
J · 2018-08-03 Matched by certificate designator
ATA 3230

LANDING GEAR WOULD NOT RETRACT. LANDING GEAR RELAY CIRCUIT BREAKER TRIPPED. RESET THE CIRCUIT BREAKER TO ATTEMPT TO RAISE GEAR. NOSE GEAR CAME UP. MAIN REMAINED LOCKED DOWN. PUMPED NOSE GEAR DOWN. AIRCRAFT RETURNED TO ORIGIN AND LANDED UNEVENTFULLY. MAINTENANCE CONFIRMED DISCREPANCY ON FIRST RETRACTION TEST, AND THEN COULD NOT DUPLICATE. AIRCRAFT REMAINS IN MAINTENANCE.

Source: SDR YADA201808063001 · FAA SDRS
O · 2018-07-28 Matched by certificate designator
ATA 2997

MAIN LANDING GEAR WOULD NOT RETRACT & POPPED CIRCUIT BREAKER LANDING GEAR RELAY. MAINTENANCE REPAIRED CHAFED WIRES ON LANDING GEAR POWER PACK AS WELL AS REPLACED OTHER ELECTRICAL COMPONENTS FOR COMPANY CONVENIENCE.

Source: SDR YADA2018073128001 · FAA SDRS
S · 2018-07-26 Matched by certificate designator
ATA 3230

PILOT REPORTED LANDING GEAR DID NOT RETRACT AFTER TAKEOFF, CIRCUIT BREAKER POPPED. RETURNED TO ORIGIN (ANC) AND LANDED WITHOUT INCIDENT.

Source: SDR YADA2018073026001 · FAA SDRS