N125AX

BEECH 1900C · 1988 · Valid Registration

Registered owner: ALASKA CENTRAL EXPRESS INC, AK (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ALASKA CENTRAL EXPRESS INC (YADA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

K · 2025-01-27 Matched by certificate designator
ATA 7261

MAINTENANCE DISCOVERED A LEAKING ENGINE OIL SCAVENGE PUMP - A PINHOLE WAS VERIFIED IN THE PUMP HOUSING OUTER WALL FROM INTERNAL EROSION - REPLACED SAME.

Source: SDR YADA2025012701 · FAA SDRS
O · 2023-03-06 Matched by certificate designator
ATA 2730

WHILE PERFORMING A COMPANY FLEET CAMPAIGN DISCOVERED FORWARD ELEVATOR BELLCRANK CRACKED WEB.

Source: SDR YADA20230313005 · FAA SDRS
K · 2022-10-15 Matched by certificate designator
ATA 7920

DURING UNRELATED MAINTENANCE, AN OIL LEAK WAS DISCOVERED FROM THE LEFT ENGINE. MAINTENANCE IDENTIFIED THE ENGINE OIL SCAVENGE PUMP AS HAVING A PINHOLE LEAK AND THE PUMP HOUSING WAS REPLACED. INSPECTION DETERMINED THAT CAVITATION EROSION OF THE PUMP BODY IN A CORNER OF THE CAVITY HAD CREATED A HOLE. THIS IS A FREQUENT ON THESE PUMP HOUSINGS. POST REPLACEMENT OF PUMP HOUSING LEAK CHECK WAS GOOD.

Source: SDR YADA2022100301 · FAA SDRS
Y · 2020-07-01 Matched by certificate designator
ATA 7321

PILOT REPORT: LEFT ENGINE FAILURE IN FLIGHT. TORQUE ROLLED BACK SLOWLY TO 0 NG INDICATED APPROX 55 FUEL FLOW 100 PPH. ATTEMPTED STARTER ASSIST AIRSTART. PROP FEATHERED AND UNFEATHERED NORMALLY. SAME INDICATIONS FOR RESTART. SECURED ENGINE. 1300 LBS OF FUEL ON BOARD. MAINTENANCE REPORT: THE CAUSE OF THE FAILURE HAS YET TO BE DETERMINED.

Source: SDR YADA20200702001 · FAA SDRS
J · 2018-06-05 Matched by certificate designator
ATA 3020

DURING TAKEOFF ROLL, THE NR 2 ENGINE FIRE LIGHT ILLUMINATED. AFTER RETARDING THE POWER, THE LIGHT DISTINGUISHED. MAINTENANCE PERFORMED INSPECTION OF THE #2 ENGINE AND FOUND THAT THE AIR INTAKE HEATED LIP DUCT WAS DISCONNECTED. MAINTENANCE CONNECTED THE HEATED LIP DUCT.

Source: SDR YADA201806065001 · FAA SDRS