N125AX
Registered owner: ALASKA CENTRAL EXPRESS INC, AK (owner ≠ operator)
Operators of this aircraft
Who operated this tail, and how firmly we know it.
| Operator | Role | Period | Basis |
|---|---|---|---|
| ALASKA CENTRAL EXPRESS INC (YADA) | Certificate holder | — | Matched by certificate designator |
Accident & incident history
No NTSB accidents or incidents on file for this aircraft.
Maintenance disclosures
MAINTENANCE DISCOVERED A LEAKING ENGINE OIL SCAVENGE PUMP - A PINHOLE WAS VERIFIED IN THE PUMP HOUSING OUTER WALL FROM INTERNAL EROSION - REPLACED SAME.
WHILE PERFORMING A COMPANY FLEET CAMPAIGN DISCOVERED FORWARD ELEVATOR BELLCRANK CRACKED WEB.
DURING UNRELATED MAINTENANCE, AN OIL LEAK WAS DISCOVERED FROM THE LEFT ENGINE. MAINTENANCE IDENTIFIED THE ENGINE OIL SCAVENGE PUMP AS HAVING A PINHOLE LEAK AND THE PUMP HOUSING WAS REPLACED. INSPECTION DETERMINED THAT CAVITATION EROSION OF THE PUMP BODY IN A CORNER OF THE CAVITY HAD CREATED A HOLE. THIS IS A FREQUENT ON THESE PUMP HOUSINGS. POST REPLACEMENT OF PUMP HOUSING LEAK CHECK WAS GOOD.
PILOT REPORT: LEFT ENGINE FAILURE IN FLIGHT. TORQUE ROLLED BACK SLOWLY TO 0 NG INDICATED APPROX 55 FUEL FLOW 100 PPH. ATTEMPTED STARTER ASSIST AIRSTART. PROP FEATHERED AND UNFEATHERED NORMALLY. SAME INDICATIONS FOR RESTART. SECURED ENGINE. 1300 LBS OF FUEL ON BOARD. MAINTENANCE REPORT: THE CAUSE OF THE FAILURE HAS YET TO BE DETERMINED.
DURING TAKEOFF ROLL, THE NR 2 ENGINE FIRE LIGHT ILLUMINATED. AFTER RETARDING THE POWER, THE LIGHT DISTINGUISHED. MAINTENANCE PERFORMED INSPECTION OF THE #2 ENGINE AND FOUND THAT THE AIR INTAKE HEATED LIP DUCT WAS DISCONNECTED. MAINTENANCE CONNECTED THE HEATED LIP DUCT.