N126KC

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2018-08-19 Matched by certificate designator
ATA 2130

DURING CRUISE AT FL360, WITH CABIN CONTROLLER SET TO FL380 AND NORMAL PRESSURIZATION. AT TOP OF DESCENT REDUCED POWER SLIGHTLY AND AT THE SAME TIME THE CABIN RATE KNOB TURNED TO MIN AND CABIN CONTROLLER MOVED SLIGHTLY TOWARD FIELD ELEVATION. WITHIN SECONDS THE CABIN RATE INDICATED APPROXIMATELY 2,000 FPM CLIMB. A FEW SECONDS LATER THE CABIN ALT MASTER WARNING ILLUMINATED AND THE WARNING HORN SOUNDED. THE CABIN ALTITUDE INDICATION CLIMBED INTO THE RED ARC, NEVER SAW IT EXCEED 10,000 FT. REMAINED BETWEEN 9,000 AND 10,000 FT DURING THE ENTIRE EVENT. THRUST LEVERS WERE REDUCED TO IDLE AND A 4,000 FPM DESCENT WAS INITIATED. WHILE DESCENDING, CLEARED FOR THE APPROACH, AND A CONTINUOUS DESCENT WAS MAINTAINED UNTIL LANDING. 20 SECONDS INTO THE DESCENT WHILE STILL INDICATING A RAPID CABIN CLIMB, THE CABIN OXYGEN MASKS WERE DEPLOYED MANUALLY. AT THE SAME TIME, DIALED SEA LEVEL ON THE CABIN CONTROLLER, THE AIRCRAFT DESCENDED THROUGH 17,000 FT, AND THE CABIN BEGAN TO TRANSITION FROM A HIGH RATE OF CLIMB TO A NORMAL DESCENT. SHORTLY AFTER THE CABIN ALT MASTER WARNING EXTINGUISHED. PASSING THROUGH 10,000 FT ALL SYSTEMS AND INDICATIONS WERE NORMAL. PERFORMED PRESSURIZATION CHECKS WITH NO DISCREPANCIES NOTED, COULD NOT DUPLICATE ON GROUND, TOOK AIRPLANE FOR A FLIGHT CHECK, PERFORMED PRESSURIZATION CHECKS IN FLIGHT WITH NO DISCREPANCIES NOTED, COULD NOT DUPLICATE.

Source: SDR G73R201808225587 · FAA SDRS
E · 2018-05-03 Matched by certificate designator
ATA 2435

DURING ARRIVAL, AFTER LEVELLING OFF AT 10,000 FT AN ABNORMAL VIBRATION WAS NOTICED. MOVING EACH THRUST LEVER INDEPENDENTLY INDICATED THAT THE VIBRATION WAS ASSOCIATED WITH THE NR 2 THRUST LEVER MOVEMENT. NR 2 ENGINE WAS REDUCED TO IDLE UNTIL LANDING, AND THEN SHUT DOWN AFTER LANDING. THERE WERE NO COCKPIT INDICATIONS AND NO GEN LIGHTS AT ANY TIME DURING THE EVENT. FROM THE FIRST DETECTED ABNORMAL VIBRATION UNTIL LANDING WAS 5-10 MINUTES. ONCE ON THE GROUND IT WAS DETERMINED THE NR 2 ENGINE STARTER GENERATOR WAS THE CAUSE OF THE INFLIGHT VIBRATION. REMOVED AND REPLACED THE STARTER GENERATOR. THE FAULTY STARTER GENERATOR HAD TSO: 305.7 HOURS AND CSO: 219 CYCLES SINCE THE LAST OVERHAUL. DISASSEMBLED AND FOUND THIS UNIT HAD A COM SIDE BEARING FAILURE. THIS CAUSED THE FAN TO START RUBBING ON THE FAN COVER. CLEANED AND INSPECTED. FOUND WORN BRUSHES AND WORN DAMPENER PLATE. VISUALLY AND DIMENSIONALLY INSPECTED. FOUND A WORN DRIVE END BEARING LINER.

Source: SDR G73R20180515445 · FAA SDRS
M J · 2016-07-22 Matched by certificate designator
ATA 3040

RIGHT WINDSCREEN GOES INTO OVERHEAT.

Source: SDR G73R2016080400001 · FAA SDRS
N · 2016-05-26 Matched by certificate designator
ATA 2610

APU FIRE BELL AND LIGHT SOUNDED AND ILLUMINATED DURING AIRCRAFT ROLL OUT ON LANDING WITH APU OFF.

Source: SDR G73R2016060300001 · FAA SDRS