N134AE

BELL HELICOPTER TEXTRON 206L-1 · 1981 · Valid Registration

Registered owner: AIR EVAC EMS INC, MO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AIR EVAC EMS, INC. (EVCA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

B · 2024-01-14 Matched by certificate designator
ATA 2120

ELECTRICAL BURNING SMELL IN CABIN DURING FLIGHT. THIS COULD NOT BE DUPLICATED.

Source: SDR EVCA202401140001 · FAA SDRS
B · 2022-08-14 Matched by certificate designator
ATA 2120

CREW SAID THERE WAS A SLIGHT FUEL SMELL. AIRCRAFT INSPECTED AND NO FUEL LEAK DETECTED. AIRCRAFT RETURNED TO SERVICE.

Source: SDR EVCA20220816001 · FAA SDRS
B · 2019-03-18 Matched by certificate designator
ATA 2197

ELECTRICAL SMELL AND VISIBLE SMOKE IN CABIN AFTER AIR CONDITIONER WAS TURNED ON, WENT AWAY WHEN AIR CONDITIONER WAS TURNED OFF. REMOVED TAIL BOOM ACCESS AND BAGGAGE COMPARTMENT ACCESS PANELS, INSPECTED AIR CONDITIONER AFT BLOWER ASSEMBLY AND FOUND WIRING TO THE BLOWER FAN IN THE 2 PIN CONNECTOR OVERHEATED. REINSTALLED TAIL BOOM AND BAGGAGE COMPARTMENT ACCESS PANEL. PERFORMED GROUND RUN WITH NO DEFECTS NOTED. WORK PERFORMED IAW BHT206L1-MM CHAPTER 53 AND CABIN AIR CONDITIONING SYSTEM MAINTENANCE INSTRUCTIONS – DOC. NO. ICA-206EC270M-1.

Source: SDR EVCA2019031800000 · FAA SDRS
B · 2017-08-10 Matched by certificate designator
ATA 3397

PILOT REPORTED SEARCH LIGHT BECAME INOPERATIVE AND CIRCUIT BREAKER POPPED WHILE IN FLIGHT. CREW REPORTED FAINT ELECTRICAL BURNING ODOR AND REPORTED CABIN LIGHTS FLICKERING. UPON MAINTENANCE INSPECTION FOUND THE SEARCH LIGHT DIODE AND JUMPER TO HAVE INDICATIONS OF BURNING AND FAILURE.

Source: SDR EVCA201708101 · FAA SDRS
O · 2017-04-18 Matched by certificate designator
ATA 6220

DURING PREFLIGHT INSPECTION PILOT FOUND ONE OF THE MAIN ROTOR HUB PILLOW BLOCK EARS TO BE CRACKED.

Source: SDR EVCA201704181 · FAA SDRS
O · 1999-08-12 Matched by certificate designator
ATA 3421

ARTIFICIAL HORIZON HAS FOGGED GLASS.

Source: SDR HEEA063462 · FAA SDRS
O · 1999-07-13 Matched by certificate designator
ATA 3457

BENCH CHECK REQUIRED. FOUND SELECTOR KNOBS INTERMITTENT WHEN TURNED.

Source: SDR HEEA062914 · FAA SDRS
O · 1999-04-05 Matched by certificate designator
ATA 2312

TRANSCEIVER HAD INTERMITTENT OPERATION. PERFORMED PRELIMINARY INSPECTION AND FOUND UNIT HAS NO TONE DEVIATION AND NO CTCSS TONES.

Source: SDR HEEA061787 · FAA SDRS
O · 1999-04-05 Matched by certificate designator
ATA 2312

DIGITS OF LED DISPLAY CHANGE WITH VIBRATION IF FACE PLATE IS PRESSED. PERFORMED PRELIMINARY INSPECTION AND FOUND BROKEN WIRE, REPAIRED WIRE, CLEANED THUMBWHEEL NO HELP. UNIT AUDIO CUTTING OUT ON ALL CHANNELS.

Source: SDR HEEA061786 · FAA SDRS
D · 1999-01-28 Matched by certificate designator
ATA 7110

IN CRUISE FLIGHT, PILOT NOTICED A CHANGE IN SOUND. CONTINUED FLIGHT (7 MILES AWAY) TO DESTINATION. POST-FLIGHT INSPECTION REVEALED RT ENGINE COWL SIDE DOOR MISSING. COWLING HAD MADE MINOR CONTACT WITH ONE M/R BLADE. REF: BK-117 IPC, FIGURE 221, ITEM 10.

Source: SDR 99ZZZX1712 · FAA SDRS
O · 1999-01-25 Matched by certificate designator
ATA 6220

ROTOR STAR HAS WEAR IN ZONES 3-4. WEAR IN ZONE 2, DUE TO BEARING P/N F32827 AND BEARING P/N F32828 SPINNING IN BORE.

Source: SDR HEEA060439 · FAA SDRS
K · 1998-11-06 Matched by certificate designator
ATA 2913

HYDRAULIC PUMP CASE DRAIN LEAKING.

Source: SDR HEEA0016703 · FAA SDRS
O · 1998-11-05 Matched by certificate designator
ATA 2810

FILLER VALVE HAS SEAL TORN, LEAKS.

Source: SDR HEEA0016680 · FAA SDRS
O · 1998-07-27 Matched by certificate designator
ATA 3451

TRANSCEIVER INOPERATIVE. NO DISPLAY OR RECEIVE.

Source: SDR HEEA0015265 · FAA SDRS
O · 1998-06-17 Matched by certificate designator
ATA 6720

BEARING HAS EXCESSIVE WEAR TO THE POINT OF NEAR FAILURE AND POSSIBLE LOSS OF TAIL ROTOR CONTROL. REPLACED WITH SERVICEABLE LINK.

Source: SDR HEEA0014808 · FAA SDRS
O · 1998-06-08 Matched by certificate designator
ATA 2312

POWER OUT, HESITATING AND UNIT WOULD NOT RECEIVE 138-139 MHZ RANGE.

Source: SDR HEEA0014663 · FAA SDRS
O · 1998-04-22 Matched by certificate designator
ATA 3420

ARTIFICIAL HORIZ INDICATOR INTERNAL LIGHTS SHORTED.

Source: SDR HEEA0014032 · FAA SDRS
O · 1998-04-02 Matched by certificate designator
ATA 2210

TRANSDUCER CAUSES ERRATIC READINGS.

Source: SDR HEEA0013827 · FAA SDRS
O · 1998-03-19 Matched by certificate designator
ATA 3422

FAILED TEST 1.1 ON SST NO VALID.

Source: SDR HEEA0013469 · FAA SDRS
F · 1998-02-06 Matched by certificate designator
ATA 2211

CSAS COMPUTER DEFECTIVE. CONTROL KICKS IN FLIGHT.

Source: SDR HEEA0012860 · FAA SDRS
K · 1998-02-05 Matched by certificate designator
ATA 3423

MAG COMPASS FLUID LEAKING.

Source: SDR HEEA0012840 · FAA SDRS
O · 1998-02-05 Matched by certificate designator
ATA 7310

FUEL LEAK FROM TUBE BETWEEN TWO NOZZLES. FUEL LEAKS OUT ALONG BRAZE AT NOZZLE.

Source: SDR HEEA0012769 · FAA SDRS
K · 1997-12-31 Matched by certificate designator
ATA 7310

AFTER LEAK CHECK PER SB LT101-73-10-0124, PART II A IT WAS DISCOVERED THAT THE FUEL MANIFOLD WAS LEAKING AT ONE OF THE FUEL NOZZLES WHERE THE RIDGED TUBE IS BRAZED TO THE NOZZLE.

Source: SDR HEEA0012407 · FAA SDRS
O · 1997-12-05 Matched by certificate designator
ATA 2210

YAW SYSTEM SENSITIVE TO INPUT GYRO IS DEFECTIVE

Source: SDR HEEA0012244 · FAA SDRS
O · 1997-12-03 Matched by certificate designator
ATA 3422

DIR GYRO SLOW TO ENGAGE AND INTERMITTENTLY INOPERATIVE.

Source: SDR HEEA0012216 · FAA SDRS
O · 1997-11-13 Matched by certificate designator
ATA 2210

CONTROL UNIT DROPPED OFF LINE SEVERAL TIMES, WOULD NOT COME ON ONE TIME.

Source: SDR HEEA0011995 · FAA SDRS
O · 1997-11-05 Matched by certificate designator
ATA 2422

STATIC INVERTER BROKEN SCREWS ON MOUNT.

Source: SDR HEEA0011775 · FAA SDRS
O · 1997-10-21 Matched by certificate designator
ATA 3421

UNIT ROLLED TO THE INVERTED POSITION AND STAYED THERE FOR GROUND RUN AND POWER CHECK. AIRCRAFT WAS HOVERED AND TEST FLOWN FOR FURTHER OBSERVATION. GYRO ROLLED UPRIGHT BUT DID NOT REFLECT PROPER ALTITUDE.

Source: SDR HEEA0011607 · FAA SDRS
O · 1997-10-21 Matched by certificate designator
ATA 6420

T/R BUSHING RING STAKING CAME LOOSE. REPLACED WITH SERVICEABLE PART.

Source: SDR HEEA0011585 · FAA SDRS
O · 1997-10-10 Matched by certificate designator
ATA 3421

HORIZON GYRO FRONT GLASS FOGGED, SLOW OPERATION.

Source: SDR HEEA0011428 · FAA SDRS
O · 1997-10-10 Matched by certificate designator
ATA 3421

ARTIFICAL GYRO +5 TO 10 DEGREE CONSTANT LEFT BANK.

Source: SDR HEEA0011429 · FAA SDRS
O · 1997-10-02 Matched by certificate designator
ATA 3610

NO. 1 ENGINE HAD HIGH TOT. BLEED AIR VALVE FAILED.

Source: SDR HEEA0011192 · FAA SDRS
O · 1997-08-19 Matched by certificate designator
ATA 3414

AIRSPEED INDICATOR FAILED TO "0".

Source: SDR HEEA0010769 · FAA SDRS
O · 1997-06-26 Matched by certificate designator
ATA 7931

CANNOT ADJUST SENSOR ALWAYS REACHES .-13VDC.

Source: SDR HEEA0010291 · FAA SDRS
O · 1997-06-26 Matched by certificate designator
ATA 3340

POWER SUPPLY BLOWS FUSE AFTER 5 SECONDS.

Source: SDR HEEA0010298 · FAA SDRS
O · 1997-05-07 Matched by certificate designator
ATA 2211

PITCH SYSTEM INOPERATIVE, WILL NOT CENTER UP, ACTUATOR GOES FULL, AND PITCH ACTUATOR KEEPS RUNNING.

Source: SDR HAIHEEA9775 · FAA SDRS
O · 1997-04-23 Matched by certificate designator
ATA 2841

FUEL QTY #2 SUPPLY INTERMITTENTLY DROPS TO ZERO. MAIN TANK DROPPED TO ZERO ALSO.

Source: SDR HAIHEEA9550 · FAA SDRS
O · 1997-04-23 Matched by certificate designator
ATA 6210

M/R BLADE HAS HOLE IN THE LEADING EDGE ABRASION STRIP NEAR THE TIP.

Source: SDR HAIHEEA9490 · FAA SDRS
O · 1997-02-10 Matched by certificate designator
ATA 6730

ACTUATOR RATCHETY AND SLOW. WOULD SOMETIMES STICK TO ONE SIDE.

Source: SDR HEEA978987 · FAA SDRS
O · 1996-10-11 Matched by certificate designator
ATA 7310

AIRCRAFT ENGINE LEAK CHECK REVEALED: FUEL LEAKING FROM FUEL MANIFOLD TUBING. INSTALLED A SERVICEABLE MANIFOLD.

Source: SDR HEEA968221 · FAA SDRS
O · 1996-05-31 Matched by certificate designator
ATA 2822

FUEL PUMP SEAL LEAKAGE.

Source: SDR HEEA967305 · FAA SDRS
O · 1996-03-13 Matched by certificate designator
ATA 2312

WILL NOT TRANSMIT. FOUND NO 29V ON POWER SUPPLY. REPLACED U2 (IC), U1 (IC),VR1 (DIODE) AND REPAIRED POWER SUPPLY. SYNTHESIZER BOARD HAS BAD TUNING VOLTAGE. REPLACED U11 (IC), U12 (IC), U13 (IC), U9 (IC), U10 (IC). REPAIRED. FOUND WEAK RECEIVER SENSE AT 406MHZ.ALIGNED THE RECEIVER AND ADJUSTED SYNTHESIZER PRESELECTOR VOLTAGE TO SPECS, REPAIRED. FOUND TRANSMIT TONE SET A CODE 11 FOR A TONE OF 91.5HZ DRIFTING OFF FREQUENCY. REPLACED U14 (IC) ON AUDIO BOARD. REPAIRED. BENCH CHECK GOOD.

Source: SDR HEEA966854 · FAA SDRS
O · 1995-11-22 Matched by certificate designator
ATA 5302

CRACKS WERE FOUND ON THE FRAME WHERE IT RIVETED TO THE TAIL CONE SKIN. CRACKS WERE ALSO FOUND UNDER THE UPPER AFT ECU MOUNT. INSTALLED REPAIR KIT P/N 117-SB20-101-3.1 ACCORDING TO SB BK117-20-101. INSTALLED A REPAIR DOUBLER ON TAIL CONE. SHIMMED ECU TO AVOID ANY PRELOADS ON MOUNTS.

Source: SDR HEEA956139 · FAA SDRS
O · 1995-11-01 Matched by certificate designator
ATA 3454

COMPASS FLAG WILL NOT PULL.

Source: SDR HEEA955953 · FAA SDRS
B · 1995-10-12 Matched by certificate designator
ATA 2312

UNIT SHORTED. SMOKE CAME FROM UNIT WHEN TURNED ON.

Source: SDR HEEA955870 · FAA SDRS
O · 1995-05-18 Matched by certificate designator
ATA 7931

SWITCH WILL NOT CLOSE.

Source: SDR HEEA955018 · FAA SDRS
O · 1995-03-28 Matched by certificate designator
ATA 5210

BROKEN EJECTION SPRING OF LATCH REQUIRES TWO HANDS TO OPERATE LATCH ASSY. REPLACED WITH SERVICEABLE LATCH ASSY AND RETURNED TO SERVICE.

Source: SDR HEEA954649 · FAA SDRS
O · 1995-03-22 Matched by certificate designator
ATA 3310

TRANSFORMER LOOSE IN BOX, INOPERATIVE, 35A CIRCUIT BREAKER LUG STRIPPED. TIME SINCE REPAIR 0:00.

Source: SDR HEEA954568 · FAA SDRS
K · 1995-03-22 Matched by certificate designator
ATA 6720

LEAKING LOWER SEAL AND PILOT VALVE AND EHA SEAL.

Source: SDR HEEA954577 · FAA SDRS
O · 1995-02-09 Matched by certificate designator
ATA 3310

LIGHTS INTERMITTENTLY.

Source: SDR HEEA954325 · FAA SDRS
O · 1995-02-06 Matched by certificate designator
ATA 3452

REPLY LIGHT WILL NOT COME ON; INTERMITTENT. REPLACED PHOTOCELL V301. REPAIRED.

Source: SDR HEEA954320 · FAA SDRS
O · 1995-01-10 Matched by certificate designator
ATA 2312

NO DISPLAY/WEAK TRANSMITT. VERIFIED PROBLEM. REPLACED F401 (FUSE), REPAIRED. ADJUSTED FREQUENCY AND SIDETONES. BENCH CHECK GOOD.

Source: SDR HEEA954235 · FAA SDRS