N14562

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2023-01-29 Matched by certificate designator
ATA 5100

CREW REPORTED-PASSENGER DESCRIBED A WHOMPING SOUND FOLLOWED BY A “BUCKET DRAGGING ACROSS THE PLANE”. NO EICAS INDICATIONS SHOWN OR ANYTHING ABNORMAL FROM THE FLIGHT DECK. THE SOUND FROM THE FLIGHT DECK SOUNDED LIKE A LOW RUMBLE. CORR ACTION- MX PERFORMED GVI OF INTERIOR AND EXTERIOR OF A/C, OPERATED PACKS AND PRESSURED CABIN AND COULD IDENTIFY NO ABNORMAL SOUNDS OR RUMBLING AT THIS TIME. SUSPECT IT WAS ICE COMING OFF THE AIRCRAFT.

Source: SDR 4DPA2023012900001 · FAA SDRS
L · 2020-06-18 Matched by certificate designator
ATA 3350

DURING MX INSPECTION THE #3 EMERGENCY LIGHT BATTERY PACK WILL NOT ILLUMINATE LIGHTS. MX R&R #3 EMERGENCY LIGHT BATTERY WITH OPERATIONAL CHECK GOOD.

Source: SDR ASOA2020062685019 · FAA SDRS
L · 2020-06-18 Matched by certificate designator
ATA 3350

DURING MX INSPECTION THE #1 EMERGENCY LIGHT BATTERY PACK WILL NOT ILLUMINATE LIGHTS. MX R&R #1 EMERGENCY LIGHT BATTERY WITH OPERATIONAL CHECK GOOD.

Source: SDR ASOA2020062685020 · FAA SDRS
L · 2019-12-24 Matched by certificate designator
ATA 3350

IAH - FLIGHT 4309 MX REPORTED THAT THE EMERGENCY LIGHT CEILING PANEL AISLE LIGHT #2 ND R/H FWD EXTERIOR LIGHT WAS FOUND TO BE INOPERATIVE. MAINTENANCE REMOVED AND REPLACED THE NUMBER TWO BATTERY CHARGER, OPERATIONALLY TESTED WITH NO DEFECTS NOTED, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA2020010224467 · FAA SDRS
O · 2019-05-07 Matched by certificate designator
ATA 5230

DURING C CHECK INSPECTION A CRACK WAS FOUND ON CARGO DOOR SKIN AT HANDLE HOUSING CUT-OUT. MAINTENANCE REPAIRED CRACK IAW 52-30-01.

Source: SDR ASOA201905073032 · FAA SDRS
O · 2019-05-05 Matched by certificate designator
ATA 5753

RIGHT INBOARD FLAP FAIRING INBOARD SUPPORT CORRODED. MAINTENANCE REPAIRED INBOARD FLAP SUPPORT IAW SRM 51-70-06. ITEM 3 REPAIR OF EXPANDED COPPER FOIL.

Source: SDR ASOA201905053031 · FAA SDRS
O · 2019-05-05 Matched by certificate designator
ATA 5753

CORRECTION: RIGHT INBOARD FLAP DELAMINATED. MAINTENANCE REPAIRED INBOARD FLAP IAW SRM 51-72-09. ITEM 3 TYPE B ROOM TEMPERATURE REPAIR.

Source: SDR ASOA201905053030 · FAA SDRS
O · 2019-05-04 Matched by certificate designator
ATA 5753

RIGHT INBOARD FLAP LOWER SURFACE DELAMINATED. MAINTENANCE REPAIRED RIGHT INBOARD FLAP SURFACE I/A/W SRM 51-72-09.ITEM 3 REPAIR OF EXPANDED COPPER FOIL

Source: SDR ASOA2019053143030 · FAA SDRS
L · 2018-04-04 Matched by certificate designator
ATA 3350

IAH - DURING MAINTENANCE INSPECTION THE NUMBER FLOUR EMERGENCY LIGHT BATTERY PACK WAS FOUND TO BE INOPERATIVE. MAINTENANCE REMOVED AND REPLACED THE AFFECTED BATTERY PACK, OPERATIONALLY TESTED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA201804044019 · FAA SDRS
B · 2018-03-18 Matched by certificate designator
ATA 3320

STRONG ELECTRICAL BURNING ODOR IN THE CABIN. FOUND A SOCKET FOR A LIGHT AT A4 BURNED. REMOVED AND REPLACED THE CEILING LIGHT ASSY. OPS CHECKED GOOD. RETURNED TO SERVICE.

Source: SDR ASOA201803197034 · FAA SDRS
B · 2016-06-18 Matched by certificate designator
ATA 3320

THE CREW REPORTED A BURNING ODOR NEAR ROWS 2 & 3, AND WERE UNABLE TO TURN THE CABIN LIGHTS OFF. THE ACFT WAS FERRIED WHERE MAINTENANCE INSPECTED THE ACFT. R & R THE CABIN LIGHT CONTROL MODULE, OPERATIONALLY TESTED WITH NO DFECTS OR OTHER DISCREPANCIES NOTED, AND THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20160618055 · FAA SDRS
B · 2015-11-05 Matched by certificate designator
ATA 3420

PILOT REPORTED F/O'S PFD BLANK AND ELECTRIC ODOR PRESENT WITH POWER ON ACFT. ITEM INTIALLY PLACED ON MEL. MAINTENANCE R & R NR 4 PFD WITH OPS CHECK GOOD. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20151105057 · FAA SDRS
O · 2015-02-09 Matched by certificate designator
ATA 5311

DURING C-CHECK, FRAME 10 CRACKED JUST UNDER LT DV WINDOW. R & R THE FRAME IAW SRM 51-40-02. THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20150209045 · FAA SDRS
O · 2015-02-09 Matched by certificate designator
ATA 5330

DURING C-CHECK, INNER SKIN FOUND CORRODED FRAMES 38-39, STRINGER 21L-21R. MAINTENANCE REPAIRED THE SKIN IAW SRM 53-23-01. THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20150209051 · FAA SDRS
O · 2015-02-09 Matched by certificate designator
ATA 5330

FUSELAGE SKIN FOUND CORRODED FRAMES 37-38, STRINGER 21L-21R. REPAIRED THE SKIN IAW SRM 53-23-01.. THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20150209050 · FAA SDRS
O · 2015-02-09 Matched by certificate designator
ATA 5330

DURING C-CHECK, RT FUSELAGE SKIN AT FRAME 75 STRINGER 1R-2R CRACKED AT RIVET HOLE VERIFIED WITH EDDY CURRENT. REPAIRED THE SKIN IAW EC5330-02976. THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20150209049V · FAA SDRS
O · 2015-02-09 Matched by certificate designator
ATA 5330

DURING C-CHECK, LT FUSELAGE SKIN AT FRAME 75 AT STRINGER 1L-2L CRACKED, VERIFIED WITH EDDY CURRENT. REPAIR THE SKIN IAW EC5330-02976. THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20150209048 · FAA SDRS
O · 2015-02-09 Matched by certificate designator
ATA 5310

DURING C-CHECK, RT EMERGENCY EXIT DOOR FOUND CORRODED ON LOWER STRUCTURE. REPAIRED THE EMERGENCY EXIT LOWER FRAME IAW EC5220-01063. THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20150209047 · FAA SDRS
O · 2015-02-09 Matched by certificate designator
ATA 5310

DURING C-CHECK, CARGO DOOR CUTOUT LOWER BEAM CORRODED BETWEEN FRAMES 65-68. R & R THE CUTOUT LOWER BEAM IAW SRM 51-40-02. THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20150209046 · FAA SDRS
O · 2015-02-09 Matched by certificate designator
ATA 5311

DURING C-CHECK, FRAME 65 HAS CORROSION AT LOWER CARGI DOOR GUIDE. MAINTENANCE REPAIRED THE FRAME BETWEEN STRINGERS 15-16L IAW EC5330-02975. THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20150209044 · FAA SDRS
O · 2015-01-27 Matched by certificate designator
ATA 5320

SERVICE DOOR CENTER SILL CORRODED. R & R SERVICE DOOR CENTER SILL IAW SRM 51-40-02. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20150127015V · FAA SDRS
B · 2014-12-22 Matched by certificate designator
ATA 2121

THE CREW REPORTED AN ELECTRICAL ODOR IN THE FORWARD CABIN. THE ACFT DIVERTED AND LANDED WITHOUT INCIDENT. R & R THE NR 2 EXHAUST FAN, OPERATIONALLY TESTED WITH NO DEFECTS NOTED. THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20141222155 · FAA SDRS
N · 2014-10-11 Matched by certificate designator
ATA 2611

THE CREW REPORTED A SMOKE INDICATION IN THE CARGO AREA. THE ACFT RETURNED TO DEPARTURE AND LANDED WITHOUT INCIDENT. MAINTENANCE INSPECTED AND REPLACED BOTH CARGO SMOKE DETECTORS. OPS CHECKED GOOD.

Source: SDR ASOA20141011084 · FAA SDRS
J · 2014-08-31 Matched by certificate designator
ATA 2612

THE CREW REPORTED NR 1 ENGINE FIRE DETECTOR FAIL MESSAGE IN FLIGHT. MAINTENANCE INSPECTED AND REPLACED THE NR 1 ENGINE PYLON FIRE LOOP. OPS CHECKED GOOD.

Source: SDR ASOA20140831075 · FAA SDRS
O · 2014-03-22 Matched by certificate designator
ATA 5330

TWO DENTS AND A CREASE WERE FOUND ON THE LT FUSELAGE BETWEEN FRAME 20 AND 22. MAINTENANCE RECONTOURED DENTS FROM FRAME 20 THRU FRAME 22. INSTALL A FILLER AND DOUBLER ON THE CREASE AREA. PERFORMED A NDT AND NO CRACKS WERE NOTED. WORK WAS DONE IAW ETD 2014-145-023920. ALL WORK ACCOMPLISHED AND WAS RELEASED BACK TO SERVICE.

Source: SDR ASOA20140322068 · FAA SDRS
K J · 2013-06-05 Matched by certificate designator
ATA 2810

THE CREW REPORTED A FUEL LEAK FROM THE RIGHT WING. MX INSPECTED AND REPLACED THE RT WING FLAP VALVE. OPS CHECKED GOOD.

Source: SDR ASOA20130605047C · FAA SDRS
O · 2013-03-09 Matched by certificate designator
ATA 7120

ACFT IS IN FOR A C-CHECK WHEN INSPECTION FOUND THE NR 1 ENGINE LOWER YOKE FWD KNUCKLE CRACKED. MX R & R THE FWD LOWER YOKE IAW EC 5450-01028, REV A. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED AT THE END OF ALL CHECKS.

Source: SDR ASOA20130309288T · FAA SDRS
O · 2013-03-06 Matched by certificate designator
ATA 5751

RT AILERON MOST OTBD PCA ATTACHMENT POINT HAS NO INTERFERANCE FIT BETWEEN HAT BUSHING AND HOLE. R & R AILERON PCA BRACKET.

Source: SDR ASOA20130306285T · FAA SDRS
O · 2012-10-11 Matched by certificate designator
ATA 5330

TWO GOUGES AFT OF MAIN CABIN DOOR. CUT OUT DAMAGED SKIN, FABRICATED, PRIMED, PAINTED AND INSTALLED PATCH. LEAK CHECKED GOOD.

Source: SDR ASOA20121012147 · FAA SDRS
K J · 2012-08-15 Matched by certificate designator
ATA 3240

THE CREW REPORTED THE NR 1 HYDRAULIC SYS WENT INTO THE AMBER RANGE IN FLIGHT. THE ACFT DIVERTED AND LANDED WITHOUT INCIDENT. MX INSPECTED AND REPLACED THE NR 1 BRAKE SHUTTLE VALVE AND THE NR 4 BRAKE ASSY. OPS CHECKED GOOD. THE ACFT WAS RELEASED FOR SERVICE.

Source: SDR ASOA20120815069C · FAA SDRS
N · 2011-10-22 Unresolved
ATA 2612

FLT 4401, REPORTED E2 FIRE DET FAIL MESSAGE ON EICAS. MX REMOVED AND REPLACED NR 2 ENGINE FIRE DETECTION LOOP IAW AMM 26-11-01 WITH OPS CHECKED SUCCESSFUL. ACFT RETURNED TO SERVICE.

Source: SDR C2XA20111022172 · FAA SDRS
B · 2011-05-03 Unresolved
ATA 3040

FLIGHT 3073 - FLIGHT CREW REPORTED ELECTRICAL BURNING SMELL IN COCKPIT. EWR MX REMOVED AND REPLACED NR 2 W/S HEAT CONTROLLER AND PERFORMED OPERATIONAL CHECK SUCCESSFULLY. ACFT WAS APPROVED TO RETURN TO SERVICE.

Source: SDR C2XA11RI069 · FAA SDRS
F · 2011-04-28 Unresolved
ATA 2710

TYS - A/C WAS ON APPROACH WHEN THE CREW REPORTED THAT THE AILERONS FELT HEAVY. MAINTENANCE PERFORMED A DVI ON FORWARD AILERON QUADRANTS AT BOTH LEFT AND RIGHT PCA'S IAW EMB 145AMM-57-11-00. NO DEFECTS NOTED AND WAS RELEASED.

Source: SDR C2XA11TY051 · FAA SDRS
O · 2011-04-07 Unresolved
ATA 5751

LT AILERON PCA OUTBOARD FITTING OUTBOARD HAT BUSHING FITTING DAMAGE (ELONGATED). REMOVED AND REPLACED PCA FITTING IAW EC5750-01177.

Source: SDR C2XA11TY043 · FAA SDRS
O · 2011-04-05 Unresolved
ATA 5311

RT FRAME 10 IS CRACKED AT DV WINDOW. REMOVED AND REPLACED FRAME 10 IAW EMB 145 SRM 51-40-02.

Source: SDR C2XA11TY041 · FAA SDRS
B · 2011-02-06 Unresolved
ATA 2120

ORD FLT 6023 - THE CREW REPORTED AN ELECTRICAL BURNING SMELL FROM THE CLOSET AREA WHILE SITTING AT THE GATE. MAINTENANCE INSPECTED AND COULD NOT DUPLICATE OR SMELL ANY ELECTRICAL BURNING SMELL. NO DEFECTS WERE NOTED AND THE AIRCRAFT WAS RELEASED FOR SERVICE.

Source: SDR C2XA11CL041 · FAA SDRS
B · 2010-12-04 Unresolved
ATA 2120

THE CREW REPORTED NR 2 ENGINE HAD A SLIGHT FUEL SMELL. MAINTENANCE INSPECTED AND RAN NR 2 ENGINE. NO FUEL ODORS OR LEAKS WERE NOTED.

Source: SDR C2XA10CL194 · FAA SDRS
L · 2010-11-23 Unresolved
ATA 2560

ORD FLT 5991 - THE CREW REPORTED THE EMERGENCY FLASHLIGHT BEHIND THE CAPTAIN SEAT WAS INOPERATIVE. MAINTENANCE INSPECTED AND REPLACED THE FLASHLIGHT BULB. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA10CL178 · FAA SDRS
M J · 2010-06-11 Unresolved
ATA 2432

BHM FLT 6992 THE CREW REPORTED A BATTERY 2 OVERTEMP INDICATION. AIRCRAFT WAS DIVERTED AND LANDED WITHOUT INCIDENT. MAINTENANCE INSPECTED AND REPLACED THE NR 2 BATTERY AND OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA10CL090 · FAA SDRS
O · 2010-06-02 Unresolved
ATA 2131

IND FLT 5686 THE CREW REPORTED A LOSS OF CABIN PRESSURIZATION INDICATIONS IN FLIGHT. MAINTENANCE INSPECTED AND REPLACED THE DIGITAL PRESSURIZATION CONTROLLER. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA10CL083 · FAA SDRS
O · 2010-04-13 Unresolved
ATA 2133

PRESSURIZATION CABIN RATE ERRATIC FROM 10000FT TO SURFACE AUTO MODE PRESSURIZING BELOW FIELD ELEVATION AND MANUAL PRESSURIZATION MODE INOP. REMOVED AND REPLACED PNEUMATIC OUTFLOW VALVE IAW EMB 145AMM 21-31-04, OPS CHECK GOOD.

Source: SDR C2XA10TY055 · FAA SDRS
L · 2010-03-28 Unresolved
ATA 3350

DURING ROUTINE MAINTENANCE THE AFT OVERWING EMERGENCY EXIT LIGHT WOULD NOT TEST. MAINTENANCE REPLACED THE NR 4 EMERGENCY LIGHT INVERTER. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA10CL051 · FAA SDRS
L · 2010-02-10 Unresolved
ATA 3350

OVERWING EMERGENCY LIGHTS INOP. REMOVED AND REPLACED FUSE ON NR 4 EMERGENCY BATTERY TRAY IAW RADIANT POWER CORP CMM25-60-83, OPS CHECK GOOD.

Source: SDR C2XA10TY026 · FAA SDRS
L · 2009-08-06 Unresolved
ATA 3397

IAH - DURING MAINTENANCE INSPECTION, THE AISLE PATH LIGHT STRIP AT ROW 19 WAS FOUND TO BE INOPERATIVE. MAINTENANCE REPAIRED A BROKEN WIRE ON THE LIGHT STRIP, OPERATIONALLY TESTED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA09IA197 · FAA SDRS
O · 2008-01-26 Unresolved
ATA 5751

SHV - DURING C-CHECK LEFT AILERON UPPER SHROUD BONDING PLATE CORRODED. MX REPAIRED LT AILERON UPPER SHROUD BONDING PLATE IAW EC5750-01315. THE AIRCRAFT WAS APPROVED TO RETURN FOR SERVICE.

Source: SDR C2XA08SH013 · FAA SDRS
N · 2006-11-01 Unresolved
ATA 2611

EWR LOG SQUAWK LAV SMOKE INFLIGHT. REMOVED AND REPLACED LAV SMOKE DETECTOR IAW EMB145 AMM26-14-01. OPS CHECK GOOD.

Source: SDR C2XA06BT047 · FAA SDRS
L · 2003-07-18 Unresolved
ATA 3350

DURING ROUTINE MAINTENANCE THE RT AND LT OVERWING EMERGENCY LIGHTS WERE INOPERATIVE. MAINTENANCE REPLACED THE NR 4 EMERGENCY LIGHT BATTERY CHARGER. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA03CL125 · FAA SDRS