N145JW

SIKORSKY S-92A · 2016 · Valid Registration

Registered owner: BRISTOW LLC, LA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
BRISTOW LLC (U0GA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

N · 2024-09-13 Matched by certificate designator
ATA 2697

FIRE LIGHT FLASHES INTERMITTENTLY WITH NO AUDIO OR CAPTION LIGHT. : REMOVED AND REPLACED #2 ENGINE OUTBOARD FLAME DETECTOR HARNESS. OPERATIONAL CHECK GOOD.

Source: SDR U0GA2024091314429 · FAA SDRS
N · 2024-09-12 Matched by certificate designator
ATA 2697

FIRE LIGHT FLASHES INTERMITTENTLY WITH NO AUDIO OR CAPTION LIGHT. DURING SHUTDOWN FIRE TEST OUTBOARD CIRCUIT BREAKER POPS WHEN TESTING. DRIED WATER FROM CONNECTOR PLUG. OPS CHECKED GOOD.

Source: SDR U0GA2024091314425 · FAA SDRS
N · 2024-09-10 Matched by certificate designator
ATA 2612

FIRE #2 ENG CAUTION AND AUDIO ACTIVATED DURING HEAVY RAIN AND STAYED "ON". FOUND WATER ON JUNCTION OF #2 INBOARD FIRE DETECTOR CONNECTOR HARNESS. CLEANED AND DRIED OUT CONNECTOR. OPS CHECK GOOD ON GROUND AT THIS TIME. ALL WORK PERFORMED IAW REF. S92 WIRING SYSTEM MANUAL CHAPTER 26-11-00.

Source: SDR U0GA2024091314412 · FAA SDRS
N · 2024-09-08 Matched by certificate designator
ATA 2697

FIRE #2 ENGINE CAUTION LIGHT AND AUDIO WARNING ON FOR ONE MINUTE IN RAIN. INSPECTED #2 FIRE DETECTOR WIRE HARNESS AND DRIED CONNECTORS. TESTED SATISFACTORY. TL-265449-2024

Source: SDR U0GA2024090914391 · FAA SDRS
N · 2024-09-07 Matched by certificate designator
ATA 2697

NO #2 ENGINE FIRE LIGHT ILLUMINATED IN FLIGHT 10 MINUTES AFTER TAKE-OFF. CLEANED ALL ELECTRICAL CONNECTORS ON FLAME DETECTOR AND UPPER DECK. FIRE LIGHT WENT OFF, TESTED SATISFACTORY. TL-265393-2024

Source: SDR U0GA 202409014384 · FAA SDRS
J · 2023-06-20 Matched by certificate designator
ATA 7900

DEPARTED HOUMA ENROUTE TO MC726 WITH 19 PASSENGERS. LEVELED OFF AT 3,000 FEET RECEIVED CAUTION LIGHT. THE PM NOTED IT WAS FOR LOSS OF PRESSURE IN THE #1 ENGINE DOWN TO 9PSI. PF CALLED FOR THE EMERGENCY CHECKLIST. WHILE THE PM WAS GOING THROUGH THE EMERGENCY CHECKLIST. THE PF MADE THE RADIO CALLS. INFORMED NEW ORLEANS APPROACH OF THE SITUATION AND NEEDED TO RETURN TO HOUMA. AS PER THE EMERGENCY CHECKLIST THE ENGINE WAS BROUGHT BACK TO IDLE. WHILE CONTINUING THROUGH THE CHECKLIST THE CAPTAIN DECIDED TO DECLARE THE EMERGENCY. READING THROUGH THE CHECKLIST, NOTED NO INCREASE IN OIL TEMPERATURE. PER THE EMERGENCY CHECKLIST THE ENGINE WAS LEFT AT IDLE AND USED FOR LANDING. AFTER LANDING ON RUNWAY 36 TAXIED CLEAR ONTO RUNWAY 30/12. SECURED THE ENGINE PER THE EMERGENCY CHECKLIST. TAXIED BACK INTO BASE AND PARKED AT A8. DURING THE WALK AROUND NOTED OIL WAS COMING DOWN THE LEFT SIDE OF THE AIRCRAFT. MAINTENANCE DETERMINED ISSUE CAUSED BY CUT O-RING ON OIL PRESSURE TRANSDUCER. TRANSDUCER HAD BEEN REPLACED 2 DAYS PRIOR.

Source: SDR U0GA202306210001 · FAA SDRS