N148SA

DEHAVILLAND DHC-6-300 · Valid Registration

Registered owner: ZUNI LLC, WA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
GRAND CANYON AIRLINES INC (GCNA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2014-07-02 Matched by certificate designator
ATA 7210

MFG INSTALLED NEW FIRST STAGE SUN GEAR, WITH NEW 1ST STAGE PLANET GEAR SET ASSY. ONE OF THE GEARS, HAD A BUSHING FAILURE, CAUSING THE GEAR TO SPIN AROUND. CAUSING CONTAMINATION OF THE OIL SYSTEM. GEAR HAD FOUR HRS OF TEST TIME ONLY SINCE NEW. REPAIR STATION INSTALLED THE GEARS DURING O/H AND DID NOT NOTICE ANY DEFECT IN THE GEAR AT THE TIME OF INSTALLATION. BUSHING FAILURE OCCURRED AFTER CUSTOMER INSTALLED THE ENGINE AND WAS PERFORMING A GROUND PERFORMANCE RUN. DURING THE PERFORMANCE RUN, THE OIL PRESSURE DROPPED TO 80 PSI. SHUTDOWN THE ENGINE AND REMOVED THE FILTER HOUSING TO ADJUST THE OIL PRESSURE. AT THIS TIME THEY NOTICED BRONZE-LIKE FLAKES IN THE OIL FILTER. THE CHIP DETECTOR WAS PULLED AND A SIGNIFICANT AMOUNT OF DEBRIS WAS NOTED. THE ENGINE WAS RETURNED TO THIS REPAIR STATION AND AN INVESTIGATION REVEALED THE BUSHING HAD SPUN IN THE GEAR CAUSING OIL CONTAMINATION. NO OIL STARVATION WAS OBSERVED IN ANY OF THE GEARS WITHIN THE RGB/AGB, ELIMINATING THE POSSIBILITY OF GROUND CREW NOT PUTTING OIL IN THE ENGINE PRIOR TO START.

Source: SDR QOWR2014071800446 · FAA SDRS
B · 2012-04-27 Matched by certificate designator
ATA 2300

UPON LANDING PILOT WAS INFORMED BY PASSENGER THAT TOUR STATION SEAT 6B HAD LOUD POPPING AND SMOKE WAS OBSERVED. MAINTENANCE INSPECTED AND FOUND NO SMOKE BUT ITEM DID SMELL HOT. TOUR STATION REPLACED. INSPECTED REMOVED TOUR STATION AND FOUND VOLUME CONTROL SWITCH LOOSE AND SHORTED AGAINST METAL REINFORCING PLATE. SOME HOW PASSENGER LOOSENED SWITCH ENOUGH FOR SWITCH TO BACK OUT ENOUGH TO BYPASS THE ANTI-ROTATION PIN AND CONNECTORS TO TOUCH THE METAL BACKING PLATE.

Source: SDR GCNA20120427035 · FAA SDRS
N · 1995-04-19 Matched by certificate designator
ATA 3418

STALL WARNING OCCURRED AFER TAKEOFF FROM GEN AIRPORT. CREW PULLED APPLICABLE CIRCUIT BREAKER AND REMAINDER OF FLIGHT FLOWN FLAPS UP. MAINTENANCE REPLACED FAILED INBOARD STALL WARNING SWITCH. THIS AIRCRAFT WAS FLOWN THROUGH MOIST WEATHER ON THIS DATE. THIS SWITCH WAS REPAIRED BY THE MANUFACTURER 82.1 FLIGHT HRS TO THIS FAILURE.

Source: SDR 95ZZZX2514 · FAA SDRS