N154C

GULFSTREAM AEROSPACE G-IV · 2002 · Valid Registration

Registered owner: RED RIVER AIRCRAFT LEASING LLC, AK (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CORPORATE AIR LLC (XCGA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

F J · 2024-01-15 Matched by certificate designator
ATA 2750

DURING INITIAL CLIMB FLAPS WERE SELECTED UP. FLAPS RETRACTED TO APPROXIMATELY 10 DEGREES AND STOPPED, AT WHICH TIME THE CREW RECEIVED THE "FLAP INPUT INVALID" EICAS MESSAGE. FLIGHT CREW DIVERTED TO AN ALTERNATE AIRPORT AND LANDED WITHOUT INCIDENT. THE AIRPLANE WAS TURNED OVER TO MAINTENANCE, WHO CLEANED AND LUBRICATED LEFT AND RIGHT FLAPS AND TRAVEL NUTS. MAINTENANCE ALSO VISUALLY INSPECTED EXTERNAL PORTIONS OF FLAP SYSTEM, AND PERFORMED FLAP CONTROL SYSTEM AND FLAP SYSTEM AND EMERGENCY FLAP SYSTEM OPERATIONAL TESTS PER THE GIV AMM WITH NO DEFECTS NOTED. AIRPLANE WAS RETURNED TO SERVICE. AIRPLANE WAS TEST FLOWN TO VALIDATE FIX.

Source: SDR XCGA202401171 · FAA SDRS
O · 2020-05-15 Matched by certificate designator
ATA 7230

DURING ENGINE CALENDAR LIFE / OVERHAUL AT ROLLS ROYCE CANADA THE #10 HIGH PRESSURE COMPRESSOR DISK WAS FOUND TO HAVE 3 CRACKS IN THE DOVE TAILS AT THE 2, 4, AND 7 O'CLOCK POSITIONS.

Source: SDR XCGA2020051500001 · FAA SDRS
B · 2000-08-01 Matched by certificate designator
ATA 3340

WHILE PERFORMING A ROUTINE POST-FLIGHT INSPECTION, SMOKE WAS FOUND COMING FROM BEHIND THE VALANCE PANEL AREA NEAR FWD LT EMERG EXIT WINDOW. FOUND PROTECTED POWER SUPPLY (PPU) FOR ONE OF THE UPWASH FLUORESCENT LIGHT BULBS HAD BEEN DEFECTIVE. SIMILAR OCCCURRENCE ON 9-99 ON SAME ACFT WITH SAME P/N PPU (AL-5112), SN 2526. (X)

Source: SDR 20000828SH024 · FAA SDRS
O · 1999-09-29 Matched by certificate designator
ATA 3320

WHILE THE AIRCRAFT WAS POWERED UP ON THE GROUND, PRIOR TO A TRIP, FLIGHT MECHANIC NOTICED A LARGE AMOUNT OF WHITE SMOKE COMING FROM UNDER THE VALANCE PANEL ON LEFT SIDE OF CABIN AND ONE OF THE FLUORESCENT BULBS NOT ILLUMINATING. CIRCUIT BREAKERS FOR ALL FLUORESCENT LIGHTS WERE PULLED AS A PRECAUTION.

Source: SDR 99ZZZX3984 · FAA SDRS
O · 1999-09-08 Matched by certificate designator
ATA 2434

LEFT DC GENERATOR WOULD OCCASSIONALLY TRIP OFF-LINE DURING A GROUND RUN-UP. FOUND THE LEFT GENERATOR SHUNT GROUND PAD MELTED AND BURNT. GROUND PAD HAD RECENTLY BEEN REMOVED BY AN OUTSIDE MAINT FACILITY (AT CUSTOMER REQUEST) TO CHECK IT AND SHUNT FOR CORROSION. BOTH SHUNT AND GROUND PAD WERE IN GOOD CONDITION. IT APPEARS EITHER THE BOLT SECURING THE GROUND PAD TO THE SHUNT WAS NOT TORQUED OR THE GROUND PAD WAS NOT MATED FLUSH WITH THE SHUNT BEFORE ALL SECURING HARDWARE FOR THE SHUNT AND GROUND PAD WERE TIGHTENED.

Source: SDR 99ZZZX3629 · FAA SDRS