N16510

EMBRAER EMB-135ER · 2000 · Valid Registration

Registered owner: CORPORATE FLIGHT MANAGEMENT INC, TN (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CORPORATE FLIGHT MANAGEMENT, INC. (FJTA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

L · 2007-02-02 Matched by certificate designator
ATA 3350

DURING ROUTINE MAINTENANCE THE RIGHT FORWARD EMERGENCY LIGHT AND THE FORWARD AISLE PATH LIGHT STRIP WERE INOPERATIVE. MAINTENANCE REPLACED THE NR 2 EMERGENCY LIGHT BATTERY POWER SUPPLY. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA07CL018 · FAA SDRS
O · 2006-10-21 Matched by certificate designator
ATA 4910

SHV - MAJOR - DURING C-CHECK THE APU FIREWALL WAS FOUND TO BE CHAFED. MAINTENANCE CLEANED UP THE DAMAGED AREA AND INSTALLED A SHIM IAW EC5310-01359. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA06SH104 · FAA SDRS
B · 2006-05-01 Matched by certificate designator
ATA 3030

CREW REPORTED, PITOT 3 INOPERATIVE CAUTION LIGHT ON EICAS AND STRONG BURNING SMELL ON CABIN AND COCKPIT. FOUND PITOT NR 3 CURRENT SENSOR MELTED. REMOVED AND REPLACED PITOT NR 3 CURRENT SENSOR K0057 IAW EMB135 AMM 30-31-00, OPS CHECKED GOOD. NO BURNING SMELL NOTED. AIRCRAFT RETURNED TO SERVICE.

Source: SDR C2XA06BT019 · FAA SDRS
B · 2006-04-21 Matched by certificate designator
ATA 5610

CLE FLIGHT 2805, THE CREW REPORTED UPON ENTERING ICING CONDITIONS, WINDSHIELD HEAT SELECTED, A STRONG ELECTRICAL SMELL WAS DETECTED. THE AIRCRAFT DIVERTED INTO EWR AND LANDED WITHOUT INCIDENT. MAINTENANCE INSPECTED AND REPLACED THE CAPTAINS WINDSHIELD. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA06CL047 · FAA SDRS
O · 2004-03-13 Matched by certificate designator
ATA 5320

TYS, DURING A SCHEDULED INSPECTION THE CARGO DOOR CUTOUT LOWER SILL WAS FOUND CORRODED. MAINTENANCE REMOVED AND REPLACED THE CARGO DOOR CUTOUT LOWER SILL IAW EMB-135 SRM 51-40-02.

Source: SDR C2XA04TY051 · FAA SDRS
O · 2004-03-12 Matched by certificate designator
ATA 5320

TYS DURING A SCHEDULED 2C INSPECTION THE SERVICE DOOR FWD SILL WAS FOUND CORRODED. MAINT BLENDED AND MEASURED AREA, FAB AND INSTALL DOUBLER IAW EMB 135/145 SRM 53-21-10. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED UPON COMPLETION OF ALL WORK.

Source: SDR C2XA04TY048 · FAA SDRS
O · 2004-03-12 Matched by certificate designator
ATA 5320

TYS DURING A SCHEDULED 2C INSPECTION A GOUGE WAS FOUND AT FR 15, STR 16L. MAINT REPAIRED CENTER FUSELAGE 1 AT LT FLOOR CROSSBEAM. ALODINED, PRIMED AND PAINTED IAW IC 2004-145/0816 AND CPM 51-21-04;05;06. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED UPON COMPLETION OF ALL WORK.

Source: SDR C2XA04TY049 · FAA SDRS
O · 2004-03-12 Matched by certificate designator
ATA 5315

TYS DURING A SCHEDULED 2C INSPECTION CORROSION WAS FOUND ON THE RAMP ANGLE AT THE GALLEY AREA. MAINT REMOVED AND REPLACED THE RAMP ANGLE IAW EMB 135/145 SRM 51-40-02. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED UPON COMPLETION OF ALL WORK.

Source: SDR C2XA04TY047 · FAA SDRS
O · 2004-03-04 Matched by certificate designator
ATA 5320

TYS DURING A SCHEDULED 2C INSPECTION THE PAX DOOR SILL BRACKETS WERE FOUND CORRODED. MAINT REMOVED AND REPLACED THE FORWARD AND AFT PAX DOOR SILL BRACKETS IAW EMB 135/145 SRM 51-40-02. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED UPON COMPLETION OF ALL WORK.

Source: SDR C2XA04TY041 · FAA SDRS
O · 2004-03-04 Matched by certificate designator
ATA 5320

TYS DURING A SCHEDULED 2C INSPECTION THE LT WALL FLOOR SILL WAS FOUND CORRODED. MAINT REMOVED AND REPLACED THE LT FLOOR SILL AFT OF PAX DOOR IAW EMB 135/145 SRM 51-40-02. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED UPON COMPLETION OF ALL WORK.

Source: SDR C2XA04TY040 · FAA SDRS
O · 2004-01-19 Matched by certificate designator
ATA 3350

DURING SERVICE CHECK MAINTENANCE FOUND NR 3 EMERGENCY LIGHT BATTERY WILL NOT CHARGE. REMOVED AND REPLACED NR 3 EMERGENCY LIGHT BATTERY IAW EMB135 33-50-04. OPS CHECKED GOOD.

Source: SDR C2XA04BT008 · FAA SDRS
O · 2004-01-18 Matched by certificate designator
ATA 3350

DURING RON CHECK MAINTENANCE FOUND THE FORWARD RIGHTHAND OVERWING EMERGENCY LIGHT DOES NOT WORK AND FLOOR PROXIMITY LIGHTS ARE NOT WORKING. MAINTENANCE REMOVED AND REPLACED BATTERY PACK NR 1 IAW EMB135 AMM 33-50-04. EMERGENCY LIGHTS OPS. CHECKED GOOD IAW EMB135 AMM 33-50-00. AIRCRAFT RETURNED TO SERVICE.

Source: SDR C2XA04BT006 · FAA SDRS
O · 2003-12-28 Matched by certificate designator
ATA 3350

CREW REPORTED, (VARIOUS EMERGENCY LIGHTS IN FORWARD CABIN ARE INOPERATIVE.) MAINTENANCE REMOVED AND REPLACED NR 2 EMERGENCY LIGHT BATTERY IAW EMB135 AMM NR 33-50-04. OPS. CHECKED GOOD.

Source: SDR C2XA03BT123 · FAA SDRS
O · 2003-12-26 Matched by certificate designator
ATA 3350

CLE FLIGHT 2026 THE CREW REPORTED THE EMERGENCY LIGHT AT THE SERVICE DOOR WAS INOPERATIVE. MAINTENANCE REPLACED THE NR 2 EMERGENCY LIGHT BATTERY. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA03CL212 · FAA SDRS
L · 2003-12-25 Matched by certificate designator
ATA 3350

THE CREW REPORTED THE EMERGENCY EXIT LIGHTING WOULD NOT REMAIN ILLUMINATED DURING TESTING. MAINTENANCE RECHARGED THE EMERGENCY EXIT LIGHTING BATTERIES. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA03CL217 · FAA SDRS
L · 2003-12-18 Matched by certificate designator
ATA 3350

DURING ROUTINE MAINTENANCE THE SECOND AND THIRD EMERGENCY AISLE PATH LIGHT STRIPS WERE FOUND INOPERATIVE. MAINTENANCE REPLACED THE NR 2 EMERGENCY LIGHT BATTERY PACK. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA03CL203 · FAA SDRS
J · 2003-11-22 Matched by certificate designator
ATA 2810

CREW REPORTED, FUEL NR 1 LOW LEVEL MESSAGE CAME ON INFLIGHT ON ARRIVAL INTO EWR. NR 1 FUEL QTY INDICATOR SHOWS ZERO FUEL. DECLARED EMERGENCY AND LANDED UNEVENTFULLY IN EWR. MAINTENANCE FOUND REFUELING SWITCH TO BE IN THE OPEN POSITION ON THE REFUELING PANEL. CLOSED SWITCH OPS, CHECKED GOOD IAW EMB135 AMM 28-11-00, INDICATION CHECKS GOOD.

Source: SDR C2XA03BT111 · FAA SDRS
B · 2002-10-01 Matched by certificate designator
ATA 2120

CLE FLIGHT NR 3160 THE CREW REPORTED THE CABIN SMELLS OF FUMES WITH THE APU BLEED ON. MAINTENANCE INSPECTED AND RAN APU WITH BLEED ON AND OPERATIONAL CHECKS WERE GOOD. NO DEFECTS WERE FOUND. THE AIRCRAFT WAS RELEASED FOR SERVICE.

Source: SDR C2XA02CL191 · FAA SDRS
Y J · 2002-01-29 Matched by certificate designator
ATA 7200

CLE FLIGHT 3052 THE CREW REPORTED THE NR 2 ENGINE SHUT DOWN IN FLIGHT UNCOMMANDED. THEY REPORTED A LOUD BANG AND HIGH ITT. THE AIRCRAFT LANDED IN CLEVELAND WITHOUT FURTHER INCIDENT. MAINTENANCE REPLACED THE NR 2 ENGINE.OPERATIONAL CHECKS WERE GOOD. THE AIRCRAFT WAS RELEASED FOR SERVICE.

Source: SDR C2XA02CL027 · FAA SDRS
P · 2002-01-18 Matched by certificate designator
ATA 5270

DURING A 2A INSPECTION MAINTENANCE FOUND THE RIGHT HAND OVERWING EMERGENCY EXIT DID NOT PRODUCE A MESSAGE ON THE EICAS WHEN THE DOOR WAS OPEN. MAINTENANCE ADJUSTED THE MICROSWITCH ON THE RIGHT HAND EMERGENCY EXIT DOOR. OPERATIONAL CHECKS WERE GOOD. THE AIRCRAFT WAS RELEASED FOR SERVICE.

Source: SDR C2XA02CL012 · FAA SDRS
O · 2001-10-29 Matched by certificate designator
ATA 5230

TYS DURING A SCHEDULED 1C INSPECTION,THE CARGO DOOR SKIN WAS FOUND CHAFED AROUND THE HANDLE CUTOUT. MAINTENANCE BLENDED OUT THE AREA IAW EC5230-01068--5120-04--5120-05 AND 5120-06. ALL WORK WAS ACCOMPLISH AND WILL BE RELEASED UPON COMPLETION OF THE SCHEDULED MAINTENANCE.

Source: SDR C2XA01TY · FAA SDRS
O · 2001-10-29 Matched by certificate designator
ATA 5230

TYS DURING A SCHEDULED 1C INSPECTION,THE CARGO DOOR SKIN WAS FOUND CHAFED AROUND THE HANDLE CUTOUT. MAINTENANCE BLENDED OUT THE AREA IAW EC5230-01068--5120-04--5120-05 AND 5120-06. ALL WORK WAS ACCOMPLISH AND WILL BE RELEASED UPON COMPLETION OF THE SCHEDULED MAINTENANCE.

Source: SDR C2XA01TY171 · FAA SDRS
O · 2001-10-29 Matched by certificate designator
ATA 5312

TYS DURING A SCHEDULE 1-C INSPECTION,MAINTENANCE FOUND A HOLE RUBBED INTO THE FIREWALL BLANKET. MAINTENANCE USED EC5330-01166 FOR THE REPAIR. ALL WORK WAS DONE IAW THE EC AND AIRCRAFT WILL BE RELEASED UPON COMPLETION OF ALL SCHEDULE MAINTENANCE.

Source: SDR C2XA01TY170 · FAA SDRS
O · 2001-10-29 Matched by certificate designator
ATA 5320

TYS DURING A SCHEDULED INSPECTION A FAIRLEAD FLOOR SUPPORT AT THE CENTER OMEGA BEAM WAS FOUND BROKEN AT FR21. MAINTENANCE R/R THE FAIRLEAD FLOOR SUPPORT AND THE WORK WAS FOUND SATISFACTORY AND THE AIRCRAFT WILL BE RELEASED UPON COMPLETION OF ALL SCHEDULED MAINTENANCE.

Source: SDR C2XA01TY169 · FAA SDRS
O · 2001-10-28 Matched by certificate designator
ATA 3445

TYS During a scheduled inspection the lower TCAS antenna was found with corrosion on the base. Maintenance removed and replaced the antenna, operational checked good. I.A.W.-EMB-AMM-34-43-03. Repair procedure was satisfactory and the aircraft will be released upon complection of inspection.

Source: SDR C2XA01TY164 · FAA SDRS
O · 2001-10-28 Matched by certificate designator
ATA 5320

TYS DURING A SCHEDULED INSPECTION, SEVERAL AREAS OF CORROSION WAS FOUND ON THE CENTER FLOORBEAM GUSSET BETWEEN FRAMES 18-22. MAINTENANCE REMOVED AND REPLACED GUSSET TOP CAP. IAW-EMB-135/145-SRM-51-40-02. REPAIR PROCEDURES WERE SATISFACTORY, AIRCRAFT WILL BE RELEASED UPON COMPLETION OF INSPECTION.

Source: SDR C2XA01TY167 · FAA SDRS
O · 2001-10-28 Matched by certificate designator
ATA 5210

TYS DURING A SCHEDULED INSPECTION THE PAX-DOOR HOLD OPEN PIN LOWER BUSHING WAS FOUND TO BE MIGRATING OUT. MAINTENANCE INSTALLED BUSHING FROM THE BOTTOM IN REFERENCE TO GST-1662/01. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED ON COMPLETION OF AIRCRAFT MAINTENANCE INSPECTION.

Source: SDR C2XA01TY162 · FAA SDRS
O · 2001-10-28 Matched by certificate designator
ATA 3500

TYS During a scheduled inspection, When doing inspection task card # 35-20-00-720-001-A00, the cabin oxygen masks did not deploy in auto mode. Maintenance removed and replaced the altitude sensing switch. I.A.W.-EMB-135-AMM-51-40-02. operational checked good. Repair procedures where satisfactory, aircraft will be released upon complection of inspection.

Source: SDR C2XA01TY168 · FAA SDRS
O · 2001-10-28 Matched by certificate designator
ATA 5320

TYS During a scheduled inspection, corrosion was found on the floor gussets at the entrance to the cockpit, between frames 15 and 18. Maintenance removed and replaced gusset and center section of forward digital plate (fabricated doubler, shims and cockpit step bracket),alodined, primed and painted. I.A.W.-EMB135/145-SRM-51-40-02 and CMP-51-21-04,05 and 06., and EC5320-01059. Repair procedure was satisfactory and the aircraft will be released upon complection of inspection.

Source: SDR C2XA01TY166 · FAA SDRS
O · 2001-10-28 Matched by certificate designator
ATA 5315

TYS Several areas of corrosion were found on the aft side of service door aft of frame 22.Maintenance removed floor support and replaced it with a new part IAW emb135/145 SRM 51-40-02 and 51-10-02-Work was satisfactory and aircraft will be released upon completion of scheduled maintenance.

Source: SDR C2XA01TY163 · FAA SDRS
O · 2001-10-28 Matched by certificate designator
ATA 5321

TYS During a scheduled inspection, corrosion was found on the right floor seal at frame 18. Maintenance removed surface corrosion, alodined, primed and painted. I.A.W.-EMB135/145-CMP-51-21-04,05 and 06. Repair procedure was satisfactory and the aircraft will be released upon complection of inspection.

Source: SDR C2XA01TY165 · FAA SDRS
J · 2000-09-24 Matched by certificate designator
ATA 7530

MDW-EWR - FLT 3620 - THE CREW REPORTED THE LEFT ENGINE ITT WAS HIGHTER THAN THE RIGHT (APPROX 100 DEGREES) WHILE IN CRUISE. THE AIRCRAFT DIVERTED INTO CLEVELAND AND LANDED WITHOUT INCIDENT. MAINTENANCE INSPECTED AND REPLACED THE LEFT ENGINE AIR TUBE ASSY FOR THE DIFFUSER TO THE START BLEED CONTROL VALVE. OPERATIONAL CHECKS WERE GOOD IAW ROLLS ROYCE MM 75-31-15 AND 77-00-00. THE AIRCRAFT WAS RELEASED FOR SERVICE. (M)

Source: SDR C2XA00CL072 · FAA SDRS