N16511

EMBRAER EMB-135ER · 2000 · Valid Registration

Registered owner: CORPORATE FLIGHT MANAGEMENT INC, TN (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CORPORATE FLIGHT MANAGEMENT, INC. (FJTA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2024-07-24 Matched by certificate designator
ATA 5610

7/24/2024 - FLT VTE3348 - CREW REPORTED THAT CAPT WINDSHIELD BROKE UPON LEVELING AT FL290. RETURNED TO KPHX. MAITNENANCE REMOVED AND REPLACED THE WINDSHIELD IAW EMB135 AMM PROCEDURES. OPS CHECKED GOOD.

Source: SDR FJTA202407265111 · FAA SDRS
B · 2008-07-16 Matched by certificate designator
ATA 3320

FLIGHT 2513 -EWR- FLIGHT CREW REPORTED ELECTRICAL BURNING ODOR IN FORWARD CABIN. EWR MX REMOVED AND REPLACED PASSENGER CABIN LIGHT AT ROW 1A AND PERFORMED OPERATIONAL CHECK SUCCESSFULLY. ACFT WAS APPROVED TO RETURN TO SERVICE. (S)

Source: SDR C2XA08RI103 · FAA SDRS
O · 2006-12-17 Matched by certificate designator
ATA 5210

FLIGHT NR 3176 THE CREW REPORTED THE MAIN CABIN DOOR WAS VERY DIFFICULT TO CLOSE. MAINTENANCE INSPECTED AND ADJUSTED THE MAIN CABIN DOOR TOP AFT FRAME ROLLER. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA06CL099 · FAA SDRS
K B J · 2006-03-24 Matched by certificate designator
ATA 4930

CLE FLIGHT NR 2592, THE CREW REPORTED A STRONG FUEL SMELL WHEN STARTING THE APU. MAINTENANCE INSPECTED AND PLACED THE APU ON MEL IAW 49-00-00. CLE FLIGHT NR 3235 MAINTENANCE ENTRY FOR CLEARING MEL. MAINTENANCE REMOVED AND REPLACED THE APU FUEL CONTROL UNIT. ALL OPS CHECKS WERE REPORTED GOOD ENTRY DATED 27 MAR 06.

Source: SDR C2XA06CL034 · FAA SDRS
L · 2006-01-26 Matched by certificate designator
ATA 3397

DURING ROUTINE MAINTENANCE THE SERVICE DOOR EMERGENCY LIGHT WAS FOUND INOPERATIVE. MAINTENANCE INSPECTED AND REPLACED THE SPLICE SP9043 AT THE EXIT IDENTIFIER SIGN AT THE SERVICE DOOR. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA06CL012 · FAA SDRS
B · 2005-02-12 Matched by certificate designator
ATA 7230

CLE FLIGHT NR 2153, AFTER TAKEOFF, THE CREW SAW AND SMELLED SMOKE AND THE LAV SMOKE ALARM SOUNDED. THE AIRCRAFT RETURNED TO CLE WITHOUT INCIDENT. MAINTEANCE FOUND THE NR 1 ENGINE BLOWING SMOKE INTO THE AIRCRAFT. THE NR 1 ENGINE WAS REMOVED AND REPLACED. THE AIRCRAFT RETURNED TO SERVICE.

Source: SDR C2XA05CL007 · FAA SDRS
O · 2004-04-28 Matched by certificate designator
ATA 5751

TYS - DURING A SCHEDULED 2C INSPECTION THE RIGHT PCS AILERON O/B BRACKET BUSHING WAS FOUND MIGRATING. MAINT REMOVED AND REPLACED THE RIGHT AILERON PCA ATTACH BRACKET IAW EA-2710-01017 AND 51-20-03; 51-40-02. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED UPON COMPLETION OF ALL WORK.

Source: SDR C2XA04TY073 · FAA SDRS
O · 2004-04-28 Matched by certificate designator
ATA 5751

TYS - DURING A SCHEDULED 2C INSPECTION THE RT AILERON PCA ATTACH BRACKET WAS FOUND GOUGED. MAINT REMOVED AND REPLACED THE AILERON PCA BRACKET PRIMED AND PAINTED IAW SRM 51-20-03 AND EA 2710-01017. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED UPON COMPLETION OF ALL WORK.

Source: SDR C2XA04TY072 · FAA SDRS
O · 2001-11-23 Matched by certificate designator
ATA 5315

TYS DURING A SCHEDULED INSPECTION THE CENTER FLOORBEAM TOP CAP WAS FOUND CORRODED BETWEEN FRAMES 19 AND 22. MAINTENANCE REMOVED AND REPLACED THE TOP CAP IAW EMB135 SRM 51-40-02, THE REPAIR WAS SATISFACTORY. THE AIRCRAFT WILL BE RELEASED UPON COMPLETION OF INSPECTION.

Source: SDR C2XA01TY184 · FAA SDRS
O · 2001-11-23 Matched by certificate designator
ATA 2612

TYS DURING A SCHEDULE INSPECTION THE LEFT HAND ENGINE FIRE DETECTION LOOP WAS FOUND TO BE CHAFED BEYOND MANUFACTURES LIMITS. MAINTENANCE REMOVED AND REPLACED THE FIRE DETECTION LOOP IAW EMB135 MM 26-11-01, OPERATIONAL CHECKS WERE SATISFACTORY. THE AIRCRAFT WILL BE RELEASED UPON COMPLETION OF INSPECTION.

Source: SDR C2XA01TY183 · FAA SDRS
O · 2001-11-23 Matched by certificate designator
ATA 5313

TYS DURING A SCHEDULED INSPECTION THE EXTERNAL STRINGER 19L WAS FOUND CHAFED JUST AFT OF HYDRAULIC PUMP. MAINTENANCE ACCOMPLISHED A BLEND OUT REPAIR OF STRINGER 19L IAW CONTINENTAL EXPRESS ENGINEERING CHANGE/REPAIR AUTHORIZATION 5310-01207, THE REPAIR WAS SATISFACTORY. THE AIRCRAFT WILL BE RELEASED UPON COMPLETION OF INSPECTION.

Source: SDR C2XA01TY185 · FAA SDRS
O · 2001-11-23 Matched by certificate designator
ATA 5315

TYS DURING A SCHEDULED INSPECTION THE FORWARD DIGITAL PLATE LOCATED JUST AFT OF THE COCKPIT ENTRANCE DOOR WAS FOUND TO BE CORRODED. MAINTENANCE REMOVED AND REPLACED THE FORWARD DIGITAL PLATE IAW EMB 135 SRM 51-40-02 AND EC 35320-01059, THE REPAIR WAS FOUND TO BE SATISFACTORY. THE AIRCRAFT WILL BE RELEASED UPON COMPLETION OF INSPECTION.

Source: SDR C2XA01TY186 · FAA SDRS
L · 2001-11-19 Matched by certificate designator
ATA 3350

TYS DURING A SCHEDULED 1-C INSPECTION, PANEL 251 HF EMERGENCY LIGHT STRIP, WAS INOPERATIVE, DUE TO A BROKEN CONNECTOR. MAINTENANCE INSTALLED A NEW CONNECTOR ON PANEL 251 HF IAW EMB 135/145 AMM AND PERFORM A OPS CHECK, EVERYTHING WAS ACCOMPLISH AND WILL BE RELEASED UPON COMPLETION OF ALL MAINTENANCE.

Source: SDR C2XA01TY182 · FAA SDRS
O · 2001-11-18 Matched by certificate designator
ATA 5320

TYS DURING A SCHEDULED 1-C INSPECTION THE LEFT FLOOR SUPPORT PLATE FWD OF SERVICE DOOR WAS FOUND CORRODED AROUND SCREW HOLES. MAINTENANCE REMOVED AND REPLACED THE NUT PLATE, CLEAN THE CORROSION, REFINISH THE AREA IAW EMB 135/145 SRM 51-40-02, CPM 51-21-17-00 AND 51-21-04, 05 AND 06. ALL WORK WAS ACCOMPLISH AND WILL BE RELEASED UPON COMPLETION OF ALL MAINTENANCE.

Source: SDR C2XA01TY181 · FAA SDRS
O · 2001-11-18 Matched by certificate designator
ATA 5320

TYS DURING A SCHEDULED 1-C INSPECTION CORROSION WAS FOUND UNDER THE SERVICE DOOR SILL AND SCREW HOLES. MAINTENANCE REMOVED AND REPLACED ONE NUT PLATE, CLEAN THE CORROSION, REFINISH THE AREA IAW EMB 135/145 SRM 51-40-02 AND CPM 51-17-04--51-21-07, ALL WORK WAS ACCOMPLISH AND WILL BE RELEASED UPON COMPLETION OF ALL MAINTENANCE.

Source: SDR C2XA01TY180 · FAA SDRS
O · 2001-11-18 Matched by certificate designator
ATA 5315

TYS DURING A SCHEDULED 1C INSPECTION THE FLOORBEAM SPLICE CAP OVER FRAME 20 ON RIGHT SIDE WAS FOUND CORRODED AROUND THE RIVETS. MAINTENANCE REMOVED AND REPLACED THE RIVETS, CLEAN THE CORROSION, REWORKED THE AREA IAW EMB 135/145 SRM 51-40-02 AND CPM 51-17-00--51-21-07. ALL WORK WAS ACCOMPLISH AND WILL BE RELEASED UPON COMPLETION OF ALL MAINTENANCE.

Source: SDR C2XA01TY179 · FAA SDRS
K B J · 2001-09-17 Matched by certificate designator
ATA 4990

CLE FLIGHT 3864 THE CREW REPORTED A LAV SMOKE WARNING INDICATION ON TAXI OUT WITH A SMELL OF SMOKE IN LAV. THE AIRCRAFT RETURNED TO THE GATE WITHOUT FURTHER INCIDENT. MAINTENANCE INSPECTED AND FOUND THE APU OIL SERVICE CAP WAS OFF AND OIL LEAKING OUT OF RESERVOIR. THE APU WAS SERVICED TO PROPER LEVEL AND THE CAP WAS INSTALLED. THE SPILLED OIL WAS CLEANED UP. THE OPERATIONAL CHECKS WERE GOOD AND THE AIRCRAFT WAS RELEASED FOR SERVICE.

Source: SDR C2XA01CL204 · FAA SDRS
N · 2000-07-28 Matched by certificate designator
ATA 2611

LGA - FLT 3698 - CREW REPORTED AFTER TAKEOFF, RECEIVED A ''LAV SMOKE'' EICAS MESSAGE AND SMELLED SMOKE IN THE COCKPIT. MAINTENANCE INSPECTED LAV SMOKE DETECTION SYSTEM IAW EMB MM 26-14-00. NO FAULT OR DEFECTS NOTED. REMOVED FROM MEL AND THE AIRCRAFT WAS RELEASED FOR SERVICE. (M)

Source: SDR C2XA00CL059 · FAA SDRS
B J · 2000-07-26 Matched by certificate designator
ATA 2611

LGA - FLT 3698 - THE CREW REPORTED AFTER TAKEOFF, RECEIVED A LAV SMOKE EICAS MESSAGE AND SMELLED SMOKE IN THE COCKPIT. THE AIRCRAFT RETURNED TO LAGUARDIA WITH NO INCIDENT. MAINTENANCE INSPECTED ENGINES AND APU FOR ANY OIL FUEL LEAKS. PERFORMED GROUND RUN OF BOTH ENGINES. RAN APU ADN LEFT AND RIGHT PACKS. NO DEFECTS WERE FOUND. PLACED LAV SMOKE DETECTOR ON MEL AND RELEASED AIRCRAFT BACK TO SERVICE. (M)

Source: SDR C2XA00CL1057 · FAA SDRS