N171AA

CESSNA 510 · 2012 · Valid Registration

Registered owner: CORSAIR TWO LLC, OR (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
AERO AIR LLC (O9IA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 1999-11-23 Unresolved
ATA 2430

LAX - (ATB) APPROXIMATELY ONE HOUR AFTER TAKEOFF LAX, LOST DC BUS 1 AND L EMERGENCY DC BUS. RESET T/R 1 OUTPUT AND T/R 1 INPUT. OPS BACK TO NORMAL. NR 1 T/R. UNIT OPS CHECKED NORMAL. SYSTEM OK FOR SERVICE. (X)

Source: SDR HALA9900241 · FAA SDRS
O · 1999-04-06 Unresolved
ATA 3230

SEA - FLT 21 - AIR RETURN - CAN'T RAISE GEAR AFTER TAKEOFF UNABLE TO RAISE GEAR HANDLE. THUS GEAR WOULD NOT COME UP. ATTEMPTED GEAR HANDLE RELEASE BUTTON. INSPECTED MAIN GEAR AND FOUND RIGHT MAIN TRIM CYLINDER SUPPLY HOSE RUPTURED AT AFT END OF RT MAIN TRUCK. REPLACED HOSE ASSY WITH REF TO MM TRIM CYLINDER REPLACEMENT, LEAK CHECK GOOD. SERVICED NR 3 HYD RES TO FULL. OK FOR SERVICE. (M)

Source: SDR HALA9900091 · FAA SDRS
J · 1999-03-19 Unresolved
ATA 7200

GEN 3 OFF AND GEN FAIL LIGHTS BOTH ILLUMINATED AND NR 3 AC LOAD INDICATED ZERO. NR 3 CSD OIL PRESS LOW LIGHT ILLUMINATED CSD OIL OUTLET TEMP NORMAL AND RISE TEMP NORMAL FOLLOWED BY INCREASE IN OUTLET TEMP AFTER SEVERAL MINUTES. OUTLET TEMP REDUCED AFTER CSD DISCONNECT. CSD NR 3 DISCONNECTED AS PER FCOM. NR 3 ENGINE OIL PRESS IN YELLOW BAND JUST AFTER GEN OFF. 20 PSI PRECAUTIONARY SHUT DOWN ENGINE NR 3 AS PER THE FCOM. ENGINE NR 3 OIL QTY INDICATES ZERO AFTER GEN FAILURE. OIL PRESS 15 PSI AFTER SHUTDOWN. CHANGED ENGINE PER DR719401 CARD AND ACCOMPLISHED POWER ASSURANCE CHECK PER DR 71951 CARD. (M)

Source: SDR HALA9900079 · FAA SDRS
Y · 1999-02-04 Unresolved
ATA 7200

HNL - FLT 21 - (LOG PAGE NR 4821636). DURING CRUISE, NR 1 ENGINE EXHIBITED CHARACTERISTICS OF COMPRESSOR STALLS. (RAISING EGT, AUDIBLE RUMBLES, AND N2 DECREASING). COMPLETED APPROPRIATE CHECKLIST AND SHUT DOWN ENGINE. (X)

Source: SDR HALA9900039 · FAA SDRS
O · 1998-09-13 Unresolved
ATA 2330

SEA - FLT 23 - STATIC INTERFERENCE HEARD FROM OVERHEAD SPEAKER/HEADSET AT WHICH TIME THE NR 1 F/D, NR 1 FMA, AND NR 1 GPS WENT BLANK. AFTER STATIC STOPS, F/D, GPS RETURN TO NORMAL, FMA STAYS BLANK. WHEN MODE TEST SWITCH IS DEPRESSED, FMA RETURNS TO NORMAL. OCCURRED 3 TIMES ON FINAL. UNABLE TO DUPLICATE STATIC ON NR 1 OVERHEAD SPEAKER/HEADSET. OPS CHECK OK ON GROUND. OK FOR SERVICE. (M)

Source: SDR HALA9800321 · FAA SDRS
O · 1998-06-24 Unresolved
ATA 5320

TULE - (LOG PAGE NR 0116521). CORROSION ON RT FORWARD LAVATORY FLOOR SUPPORT. INSTALLED NEW FLOOR SUPPORT FOR FORWARD LAVATORY PER AARD 51-00-00-05. (X)

Source: SDR HALA9800182 · FAA SDRS
O · 1998-06-19 Unresolved
ATA 5753

TULE - (NR 116312) - INBOARD FLAP TRACK POST HAS CORROSION IN VARIOUS HOLES ON INBOARD FLAP ON RIGHT-HAND WING. STA 118 XORS. REAMED HOLES TO REMOVE CORROSION AND INSTALLED BUSHINGS PER AARD 57-20-00-10. (X)

Source: SDR HALA9800180 · FAA SDRS
J · 1998-06-04 Unresolved
ATA 2612

SFO - FLT 15 - (LOG PAGE NR 4620938) - NR 1 ENGINE FIRE DETECTION LOOP 'A' LIGHT ON AFTER TAKEOFF. WENT OUT AFTER CLIMB POWER. REPLACED NR 1 ENGINE CONTROL BOX. (X)

Source: SDR HALA9800141 · FAA SDRS
J · 1998-05-26 Unresolved
ATA 3610

FLT 10 - LAX - DURING CRUISE NR 3 MANIFOLD FAIL LIGHT CAME ON TEMP ABOUT 190 DEGRESS PSI AT 10 AFTER SHUT OFF. REPLACED MANIFOLD FAIL DET CONTROLLER, THE PNEU MANIFOLD FAULT INDICATOR, NO FAULT NOTED, OPS CHECKED OK. ON ENG RUN. (M)

Source: SDR HALA9800137 · FAA SDRS
O · 1998-05-20 Unresolved
ATA 7603

SFO - FLT 12 - NR 3 THROTTLE STIFF WHEN RETARDED. RE-TORQUED CLUTCH SHAFT RETAINING NUT AND ADJUSTED NR 3 THROTTLE CLUTCH TENSION PUSH/PULL FORCE CHECKS OK AT 4 POUNDS. THROTTLE FORCE WITHIN LIMITS PER MM 76-11-00. (X)

Source: SDR HALA9800126 · FAA SDRS
J · 1998-02-08 Unresolved
ATA 3610

HNL - FLT 03 - NR 1 ENGINE MANIFOLD FAIL (RED) LAMP ILLUMINATED AT TOP OF DESCENT WHEN THROTTLES WERE CLOSED TO IDLE. TEMP 210 DEGREES CELSIUS LIGHT EXTINGUISHED IN ABOUT 5 SECONDS AFTER NR 1 BLEED SWITCH TURNED OFF. (M)

Source: SDR HALA9800039 · FAA SDRS
G · 1997-11-19 Unresolved
ATA 2430

FLT 2 - HNL - ON FINAL TO LAX WITH 35 DEGREES FLAPS SELECTED AND GPWS SW OFF, STICK SHAKER ACTUATED APPROX 15-20 KNOTS ABOVE VREF. ON DESCENT, TURNED NAV LIGHT SWITCH ON AC BUSS TIE '1' ISOL LIGHT CAME ON AND LOST ALL ASSOCIATED INSTRUMENTS. AIRCRAFT DIVERTED TO 'ONT' WHERE AN UNEVENTFUL LANDING WAS MADE. (M)

Source: SDR HALA9700233 · FAA SDRS
L · 1997-07-07 Unresolved
ATA 3397

FLT 2 - HNL - 'C' CABIN EMERGENCY FLOOR LIGHTS ON IN CRUISE. SECURED WIRES. (M)

Source: SDR HALA9700136 · FAA SDRS
B · 1995-11-12 Unresolved
ATA 3820

HNL - FLT 22 - INFORMATION TAKEN FROM LOG PAGE 3657248 - REAR LAVATORIES, DENSE SMOKE, STEAM, AND ODOR. FOUND HOSE, PN 159445, PUNCTURED IN NR 3 AFT LAVATORY, REMOVED AND REPLACED HOSE. OPS CHECK, LEAK CHECK OK. (X)

Source: SDR HAL95150 · FAA SDRS