N189K

HAWKER BEECHCRAFT CORP 390 · 2008 · Valid Registration

Registered owner: BIBG2 LLC, KY (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

N · 2026-05-22 Matched by certificate designator
ATA 2612

WHILE CRUISING AT 38,000 FEET IN AND OUT OF CLOUDS NO PRECIPITATION OR TURBULENCE. RIGHT ENGINE FIRE INDICATION PUSH BUTTON ILLUMINATED AND "FIRE" ANNUNCIATOR IN THE N1 INDICATION CAME ON. THE FLIGHT CREW PERFORMED MEMORY ITEMS OF: THROTTLE TO IDLE AND WAIT FOR THE LIGHTS TO EXTINGUISH - THEY DID NOT. THE CREW MOVED THE THROTTLE TO CUT OFF AND THE LIGHTS EXTINGUISHED. COMMUNICATED TO CENTER THEY WANTED TO START A DECENT AND CHANGED THEIR ARRIVAL AIRPORT FROM 27K TO KLEX FOR GROUND AND SAFETY SUPPORT REASONS. THE ARM BUTTON WAS PRESSED THAT TURNED FUEL AND HYDRAULICS OFF AND ARMED THE SQUIB IF THEY NEEDED TO BLOW THE BOTTLE. FIRE BOTTLE WAS NOT BLOWN AS THE FIRE INDICATION WAS NO LONGER PRESENT. RIGHT ENGINE REMAINED SHUT DOWN FOR THE REMAINDER OF THE FLIGHT. THE CREW RAN THE "ONE ENGINE INOPERATIVE" APPROACH CHECK LIST IN ITS ENTIRETY. LANDED AT KLEX AND WAS ALERTED THAT BOTH ENGINES SEEMED NORMAL. FIRE CAME TO THE AIRCRAFT TO PERFORM THERMAL SCANNING AND A VISUAL INSPECTION WITH NO INDICATIONS OF A CURRENT OR HISTORY OF FIRE TAKING PLACE. WE BELIEVE THIS TO BE A FALSE FIRE INDICATION.

Source: SDR HBKA202605260587 · FAA SDRS
R J · 2026-04-11 Matched by certificate designator
ATA 7230

SHORTLY AFTER TAKE OFF, CREW WITNESSED THE LT ENGINE INDICATIONS STARTING TO ROLL BACK. THIS INDICATION HAPPENED BETWEEN 500 & 1000 FOR AGL. FELT THE DECELERATION OF THE ACFT. THE FLIGHT CREW REPORTED THERE WERE NO CAUTION OR WARNING LIGHTS PRESENT DURING THIS EVENT. THE ENGINE STOPPED ROLLING BACK AT IDLE SPEED WHERE IT REMAINED FOR THE REST OF THE FLIGHT. THERE WAS NO CONTROL OF THE THRUST ON THE LEFT ENGINE AFTER THE ENGINE STARTED ROLLING BACK FROM THE TAKE OFF THRUST SETTING. THE FLIGHT CREW AFTER ATTEMPTING TO REGAIN THRUST INPUT TO THE ENGINE LEFT THE THRUST LEVER AT IDLE FOR A LEFT TURN DOWNWIND AND LANDING AT THE SAME AIRPORT THEY DEPARTED FROM KCHA. THERE WAS NO ABNORMAL NOISE OR VIBRATIONS.

Source: SDR HBKA202604160001 · FAA SDRS