N19554

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

L · 2020-05-01 Matched by certificate designator
ATA 3350

IAH- FLIGHT 4289 DURING MAINTENANCE INSPECTION THE R/H EMERGENCY LIGHT WAS FOUND TO BE INOPERATIVE. MAINTENANCE REMOVED AND REPLACED THE #2 EMERGENCY LIGHT POWERSUPPLY BATTERY PACK, OPERATIONALLY TESTED WITH NO DEFECTS NOTED, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA2020050414017 · FAA SDRS
B · 2020-02-01 Matched by certificate designator
ATA 3350

PILOT REPORTED ELECTRICAL SMELL BY SEAT 4CD AND 5CD. ITEM PLACED ON MEL. ON 2/3/20 MX REMOVED AND REPLACED SIDEWALL LAMP AND RESEATED CONNECTOR WITH OPERATIONAL CHECK GOOD. A/C WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20200205004 · FAA SDRS
O · 2018-09-14 Matched by certificate designator
ATA 3350

PILOT REPORTED "FLOOR PATH EMERG LIGHT A/C LEFT AT WINDOW EXIT AND EXIT CEILING BACK SIDE OF LIGHT CAME ON IN FLIGHT" MX REMOVED AND REPLACED THE NR 5 INVERTER AND BATTERY CHARGER ASSEMBLY WITH OPERATIONAL CHECK GOOD. A/C WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA2018091845203 · FAA SDRS
O · 2018-07-25 Matched by certificate designator
ATA 5530

TYS A/C IS IN C-CHECK WHEN INSPECTION FOUND EVIDENCE OF SOME WEAR ON THE VERTICAL STAB BORES OR SPHERICAL BEARINGS. MAINTENANCE PERFORMED OPS CHECKS OF BOTH DIHEDRAL AND FOUND TO BE GOOD IAW AMM 51-50-01. ALL WORK ACCOMPLISHED AND WILL BE RELEASED AT THE END OF THE CHECK.

Source: SDR ASOA201807257141 · FAA SDRS
O · 2018-07-25 Matched by certificate designator
ATA 3210

TYS A/C IS IN C-CHECK WHEN INSPECTION FOUND THE RT MLG SIDE BRACE FWD AFT FITTING BEARING BORE SCORED AND HAD A SMALL AREA OF CORROSION. ALL WORK WAS ACCOMPLISHED BY MAINTENANCE IAW ETD 2018-145-076914. CORROSION WAS A LEVEL ONE IN SIZE AND WAS CLEANED. A/C WILL BE RELEASED AT THE END OF THE CHECK.

Source: SDR ASOA201807257142 · FAA SDRS
O · 2018-07-21 Matched by certificate designator
ATA 3211

LT AND RT MLG AFT TRUNNION FITTINGS INTERNAL DIAMETER HAS CORROSION. COMPLETED REWORK OF THE MLG TRUNNION IN ACCORDANCE WITH ETD 2018-145-079169.

Source: SDR ASOA201807237139 · FAA SDRS
O · 2018-07-17 Matched by certificate designator
ATA 5522

TYS A/C IS IN C-CHECK WHEN INSPECTION FOUND THE RIGHT ELEVATOR LOWER OUTBOARD FLANGE AT SCREW HOLE DAMAGED. MAINTENANCE REPAIRED DAMAGED AREA BY CUTTING OUT DAMAGE AND FABRICATING AND INSTALLING A REPAIR IAW ETD 2018-145-073219. ALL WORK ACCOMPLISHED AND WILL BE RELEASED AT THE END OF THE CHECK.

Source: SDR ASOA201807177131 · FAA SDRS
O · 2018-07-17 Matched by certificate designator
ATA 5313

TYS A/C IS IN FOR A C-CHECK WHEN INSPECTION FOUND A CRACK AT STRINGER 2L AND FRAME 75. MAINTENANCE REPAIRED AREA IAW ETD 2018-145-077021. ALL WORK ACCOMPLISHED AND WILL BE RELEASED AT THE END OF THE CHECK.

Source: SDR ASOA201807177128 · FAA SDRS
O · 2018-07-17 Matched by certificate designator
ATA 5330

TYS A/C IS IN FOR A C-CHECK WHEN INSPECTION FOUND THE LEFT REAR EXTERNAL FUSELAGE BETWEEN FRAME 75 AND 76,STRINGER 2L TO 4L CRACKED. MAINTENANCE PERFORMED A REPAIR AT THIS AREA IAW SRM 53-31-01. ALL WORK ACCOMPLISHED AND WILL BE RELEASED AT THE END OF THE CHECK.

Source: SDR ASOA201807177129 · FAA SDRS
O · 2018-07-17 Matched by certificate designator
ATA 5730

TYS A/C IS IN FOR A C-CHECK WHEN INSPECTION FOUND A DENT IN THE NR 2 LEADING EDGE LEFT WING. MAINTENANCE REPAIRED AREA BY CUTTING OUT THE DENT AND FABRICATED A DOUBLER AND REPAIRED AREA IAW SRM 57-40-00 FIGURE 201, SHEET 2. ALL WORK ACCOMPLISHED AND WILL BE RELEASED AT THE END OF THE CHECK.

Source: SDR ASOA201807177130 · FAA SDRS
O · 2018-07-09 Matched by certificate designator
ATA 5540

A/C IS IN C-CHECK WHEN INSPECTION FOUND RUDDER 1 UPPER ACTUATOR ATTACH POINT UPPER LUG HAT BUSHING MISSING AND FELL OUT. MAINTENANCE FOUND THE ATTACH POINT ELONGATED, THEY REAM HOLE AND PLACED AN OVERSIZED BUSHING IAW SRM 55-00-00. ALL WORK ACCOMPLISHED AND WILL BE RELEASED AT THE END OF THE CHECK.

Source: SDR ASOA201807097122 · FAA SDRS
O · 2018-06-29 Matched by certificate designator
ATA 5311

CP SIDE FRAME ABOVE WS SIDE POST CRACKED. SPLICED IN NEW SECTION OF FRAME ABOVE WS SIDE POST IN ACCORDANCE WITH ETD 2018-145-072956.

Source: SDR ASOA201807257140 · FAA SDRS
L · 2016-05-22 Matched by certificate designator
ATA 3350

FLIGHT CREW REPORTED THAT THE EMERGENCY LIGHT ON THE BULKHEAD AT SEAT 3D WAS INOPERATIVE. THE ACFT WAS FERRIED WHERE MAINTENANCE R & R THE NR 3 EMERGENCY LIGHT INVERTER, OPERATIONALLY TESTED WITH NO DEFECTS NOTED, AND THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20160522050 · FAA SDRS
L · 2016-03-24 Matched by certificate designator
ATA 3350

EMERGENCY FLOOR LIGHTS AT ROW 8-11 AND EXIT LIGHT AT OVERWING EXITS WERE FOUND INOPERATIVE. MAINTENANCE REPLACED THE NR 3 EMERGENCY LIGHT BATTERY. OPS CHECKS WERE GOOD.

Source: SDR ASOA20160324019 · FAA SDRS
O · 2015-12-01 Matched by certificate designator
ATA 3350

THE CREW REPORTED EMERGENCY LIGHTS REMAIN ON AT ROW 5-18. MAINTENANCE INSPECTED AND REPLACED THE NR 3 EMERGENCY LIGHT BATTERY POWER SUPPLY. OPS CHECKS WERE GOOD.

Source: SDR ASOA20151201068C · FAA SDRS
N · 2014-11-21 Matched by certificate designator
ATA 2611

THE CREW REPORTED A BAGGAGE SMOKE INDICATION IN FLIGHT ON EICAS AND EXT/BAGG PUSHBUTTON. THE ACFT RETURNED TO DEPARTURE WHERE IT LANDED WITHOUT INCIDENT. MAINTENANCE INSPECTED THE ACFT AND RESECURED A LOOSE WIRE ON THE SMOKE DETECTOR PANEL, AND R & R RELAYS K0629 AND K0625. OPS CHECKS WERE COMPLETED WITH NO DEFECTS NOTED AND THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20141121135 · FAA SDRS
N · 2014-11-21 Matched by certificate designator
ATA 2611

THE CREW REPORTED A BAGGAGE SMOKE INDICATION IN FLIGHT ON EICAS AND EXT/BAG PUSHBUTTON. THE ACFT RETURNED TO DEPARTURE WHERE IT LANDED WITHOUT INCIDENT. MAINTENANCE INSPECTED THE ACFT AND RESECURED A LOOSE WIRE ON THE SMOKE DETECTOR PANEL, AND R & R RELAYS K0629 AND K0625. OPS CHECKS WERE COMPLETED WITH NO DEFECTS NOTED AND THE ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20141121134 · FAA SDRS
L · 2014-11-12 Matched by certificate designator
ATA 3350

EMERGENCY LIGHT INOPERATIVE. R & R LIGHT. OPS CHECKED GOOD. ACFT RELEASED AND RETURNED TO SERVICE.

Source: SDR ASOA20141113115 · FAA SDRS
L · 2014-06-16 Matched by certificate designator
ATA 3350

DURING MX INSPECTION THE EMERGENCY LIGHT BELOW THE COCKPIT STEP WAS DISCOVERED INOPERATIVE. MX R & R THE NR 1 EMERGENCY LIGHT SYS INVERTER AND LIGHT ASSY WITH OPS CHECKED GOOD. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20140616071 · FAA SDRS
L · 2014-04-23 Matched by certificate designator
ATA 3350

LEFT AND RT OVERWING EMERGENCY LIGHTS INOPERATIVE. R & R NR 4 BATTERY POWER SUPPLY. OPS CHECKED GOOD.

Source: SDR ASOA20140424082 · FAA SDRS
M Y J · 2014-04-19 Matched by certificate designator
ATA 7200

DURING FLIGHT, AFTER A SERIES OF BUMPS OR WHAT SOUNDED LIKE A BACKFIRE. NR 2 ENGINE ITT SPIKED INTO THE RED FOLLOWED BY NR 2 ENGINE OUT. RESTART WAS SUCCESSFUL, FOLLOWED SHORTLY BY REPEAT OF UNCOMMANDED ENGINE SHUTDOWN. THE ACFT LANDED WITHOUT FURTHER INCIDENT. MAINTENANCE INSPECTED AND REPLACED THE NR 2 ENGINE. OPS CHECKED GOOD. DURING TEARDOWN FOUND THE BOLT THAT ATTACHES THE CVG ACTUATOR TO THE TORQUE TUBE WAS SHEARED OFF.

Source: SDR ASOA20140419036 · FAA SDRS
O · 2014-02-07 Matched by certificate designator
ATA 5751

DURING C CHECK, INSPECTION FOUND RT AILERON PCA ATTACHMENT BRACKET BEARING MIGRATED. MAINTENANCE R & R THE RT PCA BRACKET IAW EC 5750-01177.

Source: SDR ASOA20140207022 · FAA SDRS
O · 2013-06-12 Matched by certificate designator
ATA 5210

PILOT REPORTED THE MAIN CABIN DOOR WAS DIFFICULT TO OPEN. MX ADJUSTED THE MAIN CABIN DOOR ROLLERS WITH OPS CHECK SUCCESSFUL. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20130612059 · FAA SDRS
L · 2013-04-27 Matched by certificate designator
ATA 3350

CREW REPORTED SECTIONS OF THE FLOOR EMERGENCY LIGHTS TURNING ON AND OFF INTERMITTENTLY. MX R & R THE NR 3 BATTERY CHARGER ASSY AND BATTERY PACK WITH OPS CHECKS SUCCESSFUL. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR ASOA20130427043R · FAA SDRS
B · 2012-10-09 Matched by certificate designator
ATA 3397

F/A SMELLED ELECTRIC BURNING ODOR AFTER LANDING. MX INSPECTED AND REPLACED NOSE LANDING LIGHT CONTACTOR K0237. OPS CHECKED WERE GOOD.

Source: SDR ASOA20121009080 · FAA SDRS
H J · 2011-12-12 Matched by certificate designator
ATA 2421

DURING CLIMB THE CREW REPORTED THAT THE NR 3 GENERATOR DROPPED OFF LINE. THE ACFT WAS OPERATING WITH THE NR1 GENERATOR ON MEL AND WITH THE NR 3 DROPPING OFF LINE ELECTED TO RETURN TO DEPARTURE WHERE THE ACFT LANDED WITHOUT INCIDENT. MX REPLACED THE NR3 GENERATOR, PERFORMED OPS CHECKS AND CLEARED THE DISCREPANCY.

Source: SDR ASOA20111212014 · FAA SDRS
O · 2011-10-24 Unresolved
ATA 5730

AIRCRAFT STRUCK BY LIGHTNING. PERFORMED LIGHTNING STRIKE INSPECTION IAW EMB 145 5-50-01. REMOVED AND REPLACED DAMAGE RIVET AT FRAME 8 STRINGER 16L-17L. REPAIRED TOP AFT OF RT WING TIP. REMOVED AND REPLACED RT ELEVATOR TIP FAIRING. REPAIRED O/B FLAP TRAILING EDGE AND LEADING EDGE. AIRCRAFT RELEASED AND RETURNED TO SERVICE.

Source: SDR C2XA11TY163 · FAA SDRS
O · 2011-10-13 Unresolved
ATA 3350

THE CREW REPORTED THE AILE PATH EMERGENCY LIGHTS AT ROW 8 THRU 12 WILL NOT GO OFF. MAINTENANCE INSPECTED AND REPLACED THE NR 3 EMERGENCY LIGHT BATTERY CHARGER AND BATTERY. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA11CL230 · FAA SDRS
L · 2011-10-13 Unresolved
ATA 3350

FLT 6145 IAD SECTION OF AISLE PATH LIGHTING INOP AROUND EMERGENCY EXIT ROW 12 NOTED. IAD MX REMOVED AND REPLACED NR 3 EMERGENCY LIGHT BATTERY POWER SUPPLY IAW EMB145 AMM 33-50-04 WITH OPERATION CHECK SUCCESSFUL. ACFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA11RI166 · FAA SDRS
L · 2011-10-04 Unresolved
ATA 3397

MCI - DURING MAINTENANCE INSPECTION THE EMERGENCY EXIT LIGHTS OVER BOTH EXITS AND THE AISLE PATH LIGHTS FROM RO 8 TO 12 WERE FOUND TO BE INOPERATIVE. MAINTENANCE CLEANED THE CONNECTORS ON INVERTERS NUMBER 4 AND 5, OPERATIONALLY TESTED WITH NO DEFECTS AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA11IA231 · FAA SDRS
L · 2011-07-31 Unresolved
ATA 3350

DURING ROUTINE MAINTENANCE THE EMERGENCY AISLE PATH LIGHTING WAS FOUND INOPERATIVE AT THE EXIT ROW. MAINTENANCE REPLACED THE NR 3 EMERGENCY LIGHT BATTERY. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA11CL178 · FAA SDRS
B J · 2011-03-23 Unresolved
ATA 2611

LAV SMOKE INDICATION ON THE EICAS SHORTLY AFTER TAKEOFF. FOGGY CABIN/POSSIBLY DE-ICING FLUID IN AIR CONDITIONING SYSTEM. PERFORMED ENGINE RUNS IAW RR MM71-00-80 AND COULD NOT DUPLICATE AND LEAK CHECK WAS GOOD. AIRCRAFT RELEASED AND RETURNED TO SERVICE

Source: SDR C2XA11TY038 · FAA SDRS
O · 2010-06-24 Unresolved
ATA 2740

FLIGHT 2476 - EWR - FLIGHT CREW REPORTED BACK UP PITCH TRIM SWITCH INOPERATIVE. CREW PERFORMED AIR RETURN UNEVENTFULLY. EWR MX REMOVED AND REPLACED SWITCH AND PERFORMED OPERATIONAL CHECK SUCCESSFULLY. ACFT WAS APPROVED TO RETURN TO SERVICE.

Source: SDR C2XA10RI087 · FAA SDRS
O · 2010-06-13 Unresolved
ATA 3350

THE CREW REPORTED THAT WHEN THE EMERGENCY LIGHT SWITCH WAS PLACED IN THE ARMED POSITION THE CABIN EMERGENCY LIGHTS WOULD COME ON. MAINTENANCE REMOVED AND REPLACED THE FLIGHT ATTENDANT'S LIGHT CONTROL MODULE, OPERATIONALLY TESTED THE SYSTEM AND CLEARED THE DISCREPANCY.

Source: SDR C2XA10IA173 · FAA SDRS
O · 2010-05-20 Unresolved
ATA 5330

SHV - DURING C-CHECK THE AFT RT SKIN WAS FOUND TO BE CRACKED AT A RIVET AT FRAME 79 AND STRINGER 4R. MAINTENANCE PERFORMED A BUSHING REPAIR IAW EC5330-02130. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH179 · FAA SDRS
O · 2010-05-20 Unresolved
ATA 5751

SHV - DURING C-CHECK THE RT AILERON PCA ATTACHMENT BRACKET WAS FOUND TO BE WORN AND WOULD NOT RETAIN THE HAT BUSHINGS. MAINTENANCE REMOVED AND REPLACED THE AFFECTED BRACKET IAW EC5750-01177. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA10SH180 · FAA SDRS
J · 2009-10-28 Unresolved
ATA 3610

CLE FLT 2580 - THE CREW REPORTED A BLEED 1 VALVE CLOSED MESSAGE AFTER TAKEOFF. COULD NOT GET THE NR 1 BLEED VALVE TO OPEN. MAINTENANCE INSPECTED AND REPLACED THE NR 1 BLEED VALVE PUSH BUTTON SWITCH. OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA09CL139 · FAA SDRS
M · 2009-04-03 Unresolved
ATA 7500

AIRCRAFT ON CLIMBOUT FROM EWR TO TYS REACH A HIGH ITT. MAINTENANCE REPLACED THE RT COMPRESSOR AIR TUBE ON THE E1 IAW ROLLS ROYCE MM 75-00-00, OPS AND LEAK CHECKS WERE GOOD AND RETURN TO SERVICE.

Source: SDR C2XA09TY058 · FAA SDRS
O · 2007-12-21 Unresolved
ATA 2120

FLT 421 - SMF TO GEG - FLIGHT CREW REPORTED PACK 1 VALVE FAILED TO CLOSED NUMEROUS TIMES ON CLIMB. MX PERSONNEL REMOVED AND REPLACED NR 1 PACK VALVE, OPERATIONALLY CHECKED SATISFACTORY AND A/C WAS RELEASED TO RETURN FOR SERVICE.

Source: SDR C2XA07ON050 · FAA SDRS
O · 2007-09-03 Unresolved
ATA 3397

FLT 524 - MCI TO RDU - DURING PREFLIGHT CK, FLIGHT CREW DISCOVERED THE EMERGENCY LIGHTS WILL NOT SHUT OFF. MX PERSONNEL INSPECTED AND FOUND CONNECTOR ON NR 3 EMERGENCY BATTERY NOT PROPERLY SECURED. MX PERSONNEL RESECURED AND OPERATIONALLY CHECK EMERGENCY LIGHTING SYS AGAIN AND ALL CHECKED GOOD. AIRCRAFT WAS RELEASED TO RETURN FOR SERVICE IN AIRWORTHY CONDITIONS.

Source: SDR C2XA07ON021 · FAA SDRS
L · 2007-09-02 Unresolved
ATA 3350

MCI - DURING MAINTENANCE INSPECTION THE NUMBER 5 & 6 AISLE PATH EMERGENCY LIGHTS WERE FOUND TO BE INOPERATIVE. MAINTENANCE REMOVED AND REPLACED THE NUMBER THREE EMERGENCY LIGHT BATTERY PACK, OPERATIONALLY CHECKED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA07IA195 · FAA SDRS
L · 2007-08-09 Unresolved
ATA 3350

AUS - FLIGHT 308, DURING PREFLIGHT INSPECTION AN EMERGENCY EXIT LIGHT WAS FOUND TO BE INOPERATIVE. MAINTENANCE REMOVED AND REPLACED THE EMERGENCY LIGHT POWER SUPPLY FOR THE EMERGENCY EXIT ROWS, OPERATIONALLY CHECKED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA07IA185 · FAA SDRS
L · 2007-08-02 Unresolved
ATA 3350

AUS - DURING MAINTENANCE INSPECTION, THE FORWARD THREE AISLE PATH LIGHT STRIPS WERE FOUND TO BE INOPERATIVE. MAINTENANCE REMOVED AND REPLACED THE AFFECTED EMERGENCY LIGHT BATTERY PACK, OPERATIONALLY CHECKED WITH NO DEFECTS, AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA07IA182 · FAA SDRS
L · 2007-02-19 Unresolved
ATA 3350

EWR LOG SQUAWK FLT 2665 EMERGENCY LIGHTS INOP. REMOVED AND REPLACED BATTERY IAW EMB145 AMM 37-50-04. OPS CHECK GOOD.

Source: SDR C2XA07BT019 · FAA SDRS
O · 2006-01-28 Unresolved
ATA 5230

SHV - DURING C-CHECK THE CARGO DOOR INTERNAL FRAME WAS FOUND TO BE CORRODED AROUND A NUT PLATE. MAINTENANCE PERFORMED A DOUBLER REPAIR IAW CONTINENTAL EXPRESS EC5230-01131. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA06SH008 · FAA SDRS
O · 2006-01-28 Unresolved
ATA 4910

SHV - DURING C-CHECK THE APU FIREWALL WAS FOUND TO BE CHAFED AT THE 6 O`CLOCK POSITION. MAINTENANCE BLENDED OUT THE DAMAGED AREA AND PERFORMED A SHIM REPAIR IAW CONTINENTAL EXPRESS EC5310-01359. THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA06SH007 · FAA SDRS
O · 2005-11-19 Unresolved
ATA 3350

DURING SERVICE AND ROUTINE INSPECTION CHECK, MAINTENANCE FOUND THAT THE LEFT OVERWING EMERGENCY LIGHT WAS NOT WORKING. REMOVED AND REPLACED BULB IN LEFT OVERWING EMERGENCY LIGHT ASSEMBLY IAW EMB145 MM 33-50-10, OPS CHECKED GOOD.

Source: SDR C2XA05BT082 · FAA SDRS
O · 2004-03-04 Unresolved
ATA 5320

TYS DURING A SCHEDULED 1C INSPECTION THE SERVICE DOOR FWD SILL HAS AREAS OF CORROSION. MAINT BLENDED AFT AREA AND FOUND TO BE WITHIN LIMITS; ALODINED, PRIMED, PAINTED, BLENDED FWD AND FOUND TO BE OUT OF LIMITS, FABBED DOUBLER, ALODINED, PRIMED, PAINTED AND INSTALL IAW EMB 135/145 SRM 51-40-02. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED UPON COMPLETION OF ALL WORK.

Source: SDR C2XA04TY044 · FAA SDRS
O · 2004-03-04 Unresolved
ATA 5320

TYS DURING A SCHEDULED 1C INSPECTION THE FWD DIGITAL PLATE HAD AREAS OF CORROSION. MAINT CUT THE DAMAGED AREA OUT, FAB DOUBLERS AND DRILLED HOLES ON NEW FWD DIGITAL, INSTALL AND PRIMED DOUBLERS AND NEW DOUBLER IAW EMB 135/145 SRM 53-21-10. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED UPON COMPLETION OF ALL WORK.

Source: SDR C2XA04TY043 · FAA SDRS
O · 2004-03-04 Unresolved
ATA 4910

TYS DURING A SCHEDULED 1C INSPECTION THE RT UPPER STIFFENER ON THE APU FIREWALL WAS FOUND CRACKED. MAINT FABBED A DOUBLER AND STOPPED DRILL CRACK. INSTALL DOUBLER AT RT UPPER STIFFENER ON THE APU FIREWALL IAW EMB 135/145 SRM 55-32-13. ALL WORK WAS ACCOMPLISHED AND WILL BE RELEASED UPON COMPLETION OF ALL WORK.

Source: SDR C2XA04TY042 · FAA SDRS
B · 2003-11-06 Unresolved
ATA 3040

FLIGHT 2959, PILOT REPORTED THAT THE NR 1 WINDSHIELD WAS SPARKING ALONG THE SIDE DURING FLIGHT. THE AIRCRAFT LANDED AT IAH WITHOUT INCIDENT WHERE MAINTENANCE REMOVED AND REPLACED THE AFFECTED WINDSHIELD.

Source: SDR C2XA03IA104 · FAA SDRS
L · 2003-09-21 Unresolved
ATA 3350

THE CREW NOTED THAT THE EMERGENCY LIGHTS WOULD NOT TURN OFF. MAINTENANCE RESET THE ELECTRICAL POWER, PERFORMED A OPERATIONAL CHECK OF THE EMERGENCY LIGHTING SYSTEM, NO DEFECTS NOTED, AND, THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA03IA099 · FAA SDRS
J · 2003-05-29 Unresolved
ATA 3234

IAH- FLIGHT 2548, THE CREW NOTED INTERMITTENT LANDING GEAR LEVER DISAGREE IN FLIGHT. HANDLE IN THE UP POSITION ALL GEAR INDICATORS SHOW UP, BUT BOXED IN RED. IAH- MAINTENANCE REMOVED AND REPLACED THE LANDING GEAR LEVER, IAW ERJ 145-MM-32-32-02 AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA03IA055 · FAA SDRS
J · 2003-05-29 Unresolved
ATA 3230

FLIGHT 2548, THE CREW NOTED INTERMITTENT LANDING GEAR LEVER DISAGREE IN FLIGHT. HANDLE IN THE UP POSITION ALL GEAR INDICATORS SHOW UP, BUT BOXED IN RED. MAINTENANCE REMOVED AND REPLACED THE LANDING GEAR ELECTRONIC UNIT, IAW ERJ 145 MM- 32-32-01 AND THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA03IA056 · FAA SDRS
J · 2003-05-27 Unresolved
ATA 3210

IAH - FLT 2857 - PILOT REPORTED THAT THE UPON CLIMBOUT FROM STL THE GEAR HANDLE HAD TO BE CYCLED TWICE TO GET THE LANDING GEAR TO RETRACT. THE AIRCRAFT CONTINUED ON TO IAH AND LANDED WITHOUT INCIDENT. MAINTENANCE PERFORMED AN OPERATIONAL CHECK OF THE LANDING GEAR AND FOUND THE LANDING GEAR SYSTEM TO BE OPERATING NORMALLY. THE AIRCRAFT WAS THEN APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA03IA054 · FAA SDRS
L · 2003-05-02 Unresolved
ATA 3350

DURING "A" CHECK THE MECHANIC NOTED THAT THE GALLEY OVERHEAD EMERGENCY LIGHT FAILED TO ILLUMINATE. MAINTENANCE REMOVED AND REPLACED THE EMERGENCY LIGHT BULB, PERFORMED A OPERATIONAL CHECK OF THE EMERGENCY LIGHTING SYSTEM, NO DEFECTS NOTED, AND, THE AIRCRAFT WAS APPROVED FOR RETURN TO SERVICE.

Source: SDR C2XA03IA043 · FAA SDRS
O · 2003-03-17 Unresolved
ATA 3350

EMERGENCY EXIT SIGN ON THE STEP INTO COCKPIT INOP. REPAIRED BROKEN WIRE. OPS CHECK GOOD IAW EMB145AMM 20-00-00.

Source: SDR C2XA03BT042 · FAA SDRS
J · 2002-10-16 Unresolved
ATA 3600

CLE FLIGHT#3296 THE CREW REPORTED AFTER TAKEOFF THEY RECEIVED A #1 BLEED LEAK MESSAGE ON THE EICAS AND THE OVERHEAD PANEL.THE AIRCRAFT RETURNED TO CLE AND LANDED WITHOUT FURTHER INCIDENT.MAINTENANCE INSPECTED AND REPLACED THE #1 ENGINE DIRRERENTIAL PRESSURE SENSOR LINE.OPERATIONAL CHECKS WERE GOOD.

Source: SDR C2XA02CL204 · FAA SDRS