N212QS

BOMBARDIER INC CL-600-2B16 · 2016 · Valid Registration

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
NETJETS AVIATION, INC. (DXTA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

B · 2026-03-17 Matched by certificate designator
ATA 2120

WHILE ON VISUAL APPROACH CAVU DAY WE HAD THE SMELL OF SMOKE THROUGH THE AIRPLANE. WE COULD NOT IDENTIFY THE SOURCE. PERFORMED A BREAKAWAY TORQUE CHECK OF THE LEFT AND RIGHT ACM TURBINES IAW AMM PART II TASK 21-51-00-720-801. BREAKAWAY TORQUE WITHIN LIMITS AT THIS TIME. NO DEFECTS NOTED. REMOVED THE WATER SEPARATOR COALESCER BAGS, CHECKED BAGS FOR OIL IMPREGNATION, AND REINSTALLED IAW AMM PART II TASK 21-51-13-400-801. NO OIL WAS NOTED IN THE COALESCERS AT THIS TIME. REMOVED THE APU INLET DUCT AT THE CONNECTION POINT TO THE APU ENCLOSURE & CHECKED THE APU COMPRESSOR FOR OIL WITH A BORESCOPE, NOTED NO OIL PRESENT AT THIS TIME. REINSTALLED THE APU INLET DUCT IAW AMM PART II TASK 49-14-01-400-801. PER MCC'S REQUEST PERFORMED THE BOMBARDIER ECS BURN-OFF PROCEDURE. NO OIL SMELL WAS NOTED DURING THE BURN-OFF PROCEDURE. PER DOM REQUEST, TECHS OPERATED EACH INDIVIDUAL CABIN APPLIANCE AND CHECKED FOR SMOKE EMISSION, NO SMOKE EMISSIONS NOTED. MCC & DOM ELECT NO FURTHER ACTION AT THIS TIME. NO DEFECTS NOTED, ALL LEAK CHECKS SATISFACTORY.

Source: SDR DXTA2026033007300 · FAA SDRS
J · 2025-10-24 Matched by certificate designator
ATA 3230

WHILE APPROACHING THE AIRPORT WE GOT A RED CAS GEAR DISAGREE MESSAGE AND A MOMENTARY RED CAS NOSE DOOR OPEN MESSAGE THAT WENT OUT WHILE RUNNING THE GEAR DISAGREE CHECKLIST. HAD UP INDICATIONS FOR THE 3 GEAR. WHILE RUNNING THE QRH FOR GEAR DISAGREE GOT TO WHERE THE GEAR DISAGREE LIGHT WENT OUT & THREE GREEN DN INDICATIONS WERE DISPLAYED FOR THE GEAR. CHECKLIST SAID NO FURTHER ACTION REQUIRED. END OF PROCEDURE. WE LANDED WITH NO FURTHER ISSUES. REMOVED SUSPECTED DEFECTIVE NLG SELECTOR VALVE AND INSTALLED CUSTOMER SUPPLIED INSPECTED AND TESTED NLG SELECTOR VALVE IAW AMM 32-22-16 ,OPS CHECKED NORMAL

Source: SDR DXTA2025102705423 · FAA SDRS
B · 2025-10-01 Matched by certificate designator
ATA 2150

PUNGENT ODOR IN ENTIRE ACFT AFTER TURNING PACKS ON WITH APU RUNNING. ODOR DID NOT IMPROVE OVER TIME. EVEN WITH MAIN DOOR & CARGO DOORS OPEN, ODOR REMAINS STRONG & WAS IRRITATING TO NOSTRILS. REPEAT WRITE UP. REMOVED LT & RT WATER SEPARATORS & PERFORMED LT & RT ACM TORQUE CHECK & BOTH ACMS TOOK 30 IN OZ IAW AMM 21-51-00. REMOVED RT ACM & INSTALLED OVERHAULED ACM, REMOVED DAMAGED RUBBER HOSES & INSTALLED NEW RUBBER HOSES. REMOVED WATER SEPARATOR TO DISCARD COALESCER SOCK. REMOVED LT SUSPECTED DAMAGED ACM & INSTALLED REPAIRED ACM IAW AMM 21-51-16, REMOVED LT WATER SEPARATOR TO DISCARD COALESCER SOCK & INSTALLED NEW COALESCER SOCK, INSTALLED WATER SEPARATOR IAW AMM 21-51-13 OPS CHKD GOOD NO DEFECTS NOTED.

Source: SDR DXTA2025100305160 · FAA SDRS
E J · 2025-07-10 Matched by certificate designator
ATA 7200

IN FLIGHT, AT CRUISE, THE RIGHT ENGINE AMBER VIBRATION DISPAYED AT 2.7. PER QRH, AFTER PULLING BACK POWER, VIBRATION INDICATOR REDUCED BACK TO GREEN BUT AT AN ELEVATED READING OF 2.5 TO 2.6. A SLIGHTLY SLOWER CRUISE SPEED WAS REQUIRED TO KEEP INDICATOR IN GREEN. NO OTHER ABNORMAL ENGINE INDICATIONS. HOWEVER, THERE WAS A SLIGHT VIBRATION SOUND THAT COULD BE HEARD BUT NOT FELT IN THE AIRPLANE. THE 2.5 TO 2.6 RANGE DIDN'T CHANGE WITH MAJOR VARIANCE IN THROTTLE. RANGE STAYED BETWEEN 2.4 TO 2.6. ANY POWER INCREASE WOULD END UP IN AMBER OF 2.7 TO 2.8 SO THUS WAS AVOIDED. CORRECTIVE: ACTION: PERFORMED AN ENGINE RUN ON LEFT AND RIGHT ENGINES AT IDLE AND FOUND ENGINE VIBERATION TO BE 0.1 LEFT AND 0.3 RIGHT. DOWNLOADED ENGINE DATA AND FORWARDED TO GE ENGINEERING. PER NJ MCC WE WILL CONTINUE TROUBLE SHOOTING PERFORMING HIGHER POWER ENGINE RUNS TOMORROW MORNING. EZ 7/11. RAN BOTH ENGINES TO ~80 NL FOUND LEFT ENGINE VIBES STEADY AT .2.WITH A BRIEF PEAK OF .4 DURING ACCELERATION. RIGHT ENGINE WAS STEADY AT 1.4 WITH A BRIEF PEAK OF 1.5 DURING ACCELERATION. TRANSPOSED ENGINE VIBRATION MONITOR ACCELEEROMETERS LEFT AND RIGHT PER CHALLENGER 650 AMM 77-31-01. ANOTHER RUN REVEALED VERY SIMILAR RESULTS, THE FAULT DID NOT FOLLOW THE ACCELEROMETER, RETURNED ACCELEROMETERS TO THEIR ORIGINAL LOCATIONS. DISCUSSED FINDINGS WITH DAVID ROWE FROM GE, HE SUGGESTED LUBING THE FAN BLADES. LUBE ON ORDER. BR 07/12. PERFORMED FAN BLADE LUBE PER GE CF34 SERVICE MANUAL SEI-780 MAINTENANCE PRACTICE 36. T THE DISASSEMBLY AND REASSEMBLY OF THE FAN BLADES IS AN RU ITEM SEE FF1 T2.PLD00CW8F7 FOR RH DOCUMENTATION BREAKDOWN. AFTER THE LUBE WAS COMPLETED ENGINE RUNS WERE AGAIN PERFORMED. THE ENGINE VIBES ON THE RIGHT SIDE AT ~80NL WERE STEAY AT .6 WITH A PEAK OF .7 DURING ACCELERATION. WAITING ON GE ENGINEERING TO TELL US IF THIS IS ACCEPTABLE. PER CF34BJ INCREMENTAL CHANGE, SM 72-00-00, ENGINE (INSTALLED ON-AIRCRAFT) -TESTING - PARAGRAPH 4.A. €“ N1 VIBRATION LEVELS LESS THAN 2..7 MILS IS ACCEPTABLE

Source: SDR DXTA2025071404204 · FAA SDRS
B · 2025-06-02 Matched by certificate designator
ATA 3240

ON POST FLIGHT NOTICED THE INBOARD BRAKE ON THE RIGHT MLG WAS SMOKING AND EXTREMELY HOT. WE WERE VERY LIGHT ON LANDING AND DID NOT USE ANY ABNORMAL BRAKING. REMOVED AND REPLACED THE RIGHT MAIN LANDING GEAR BRAKE ASSEMBLY WITH OVERHAULED. REPLACED BRAKE BOLTS WITH NEW. COMPLIED WITH BLEEDING AND LEAK CHECK. NO LEAKS NOTED. GAINED ACCESS TO THE BRAKE PRESSURES IN THE MDC. FOUND BRAKE PRESSURES TO BE WITHIN LIMITS. INSTALLED WHEEL ASSEMBLY. IAW CL 650 MM 32-43-19, 32-43-00, 32-42-01 TORQUE WRENCH: TL-105363 SN 0423902302 NEXT CAL DUE DATE AUG 2025, TL-103772 SN 1021121206 NEXT CAL DUE DATE DEC 2025

Source: SDR DXTA2025060503738 · FAA SDRS
J · 2025-05-10 Matched by certificate designator
ATA 3230

URING OCF FOR GEAR DISAGREE, AFTER THE 1ST COMPLETE CYCLE OF THE LANDING GEAR THE NOSE LANDING GEAR DID NOT EXTEND. WE DECLARED AN EMERGENCY, AND PROC ENDED TO OUR ALTERNATE AIRPORT KACT. WE PROCEEDED TO RUN QRH PROCEDURE 10-17 MANUAL GEAR EXTENSION. THE MAIN LANDING GEAR EXTENDED NORMALLY BUT THE NOSE GEAR NOT PRODUCING A GEAR DISAGREE CAS MESSAGE AND A RED GEAR FLAG. WE DECIDED TO RUN THE LANDING GEAR JAMMED CHECKLIST WHICH PRODUCED 3 GREEN AFTER TURNING OFF 3 AND 3 B HYDRAULIC PUMPS. WE COMPLETED A FLYBY FOR GEAR VERIFICATION, THEN LANDING SAFELY AT KDAL. CORRECTIVE ACTION: REMOVED THE NLG SELECTOR VALVE P/N: 750006000 S/N: 1810T AND INSTALLED CUSTOMER SUPPLIED NEW NLG SELECTOR VALVE P/N: 750006000 S/N: 2322T, INSTALLED ALL NEW PACKINGS P/N: NAS1612-4 S/N: NSN. PERFORMED FUCTIONAL TEST, FUNCTIONAL TEST GOOD NO DEFECTS/FAULTS NOTED. WORK IN REF. CL650 AMM 32-33-07, 33-30-00 AND 07-10-01. TQ ID: TL-103779 CAL DATE: 30NOV25

Source: SDR DXTA2025051003436 · FAA SDRS
J · 2025-04-20 Matched by certificate designator
ATA 3230

GEAR DISAGREE RED CAS: DURING LANDING WHEN GEAR WAS SELECTED DOWN BOTH MAIN GEAR SHOWED GREEN DN AND NOSE GEAR SHOWED A WHITE UP. AFTER A FEW SECONDS WE HAD A RED GEAR DISAGREE CAS. CREW DID A GO AROUND AFTER CLEANING UP THE PLANE CREW REQUEATED VECTORS FOR ANOTHER APPROACH AND CONFIGURED THE PLANE AGAIN. THE SAME THING HAPPENED: RED GEAR DISAGREE. CREW PERFORMED THE GEAR DISAGREE CHECKLIST AND THE NOSE GEAR CONTINUED TO INDICATE UP. PER THE CHECKLIST CREW PERFORMED A MANUAL GEAR EXTENSION AND FINALLY GOT THREE GREEN. CREW WAS ABLE TO LAND NORMALLY AFTER THE MANUAL GEAR EXTENSION. INSPECTED MLG AND NLG WITH NO DEFECTS NOTED. POWER UP AIRCRAFT INTERROGATED MDC AND NO FAULT CODE RELATED TO GEAR DISAGREE NOTED. PERFORMED MDC DOWNLOAD, GAINED ACCESS TO TO PSEU, RETRIEVED RECORDED FAULTS AND SENT TO BOMBARDIER, DUE TO HANGER AVAILABILITY MCC ELECTED TO FERRY AIRCRAFT TO ANOTHER MAINTENANCE FACILITY. PERFORMED RFTS-113704 REV. 0. ALL WORK DONE YA/W CL-650 AMM 32-00-00.

Source: SDR DXTA2025042203153 · FAA SDRS
J · 2024-10-19 Matched by certificate designator
ATA 3241

ANTI SKID: GETTING READY TO TAXI FOR DEPARTURE WITH ENGINES RUNNING NO ANTISKID LIGHT SOON AS PARKING BRAKE WAS RELEASED BOTH THE ANTISKID INBOARD AND OUTBOARD LIGHT ILLUMINTED SEVERAL ATTEMPTS WITH SETTING AND RELEASING PARKING BRAKE RESULTED IN THE AMBER CAS MESSAGES UNABLE TO TAXI WITHOUT AMBER CAS MESSAGES ILLUMINATED REPEAT WRITE UP CORRECTIVE ACTION; REPLACED ANTISKID CONTROL UNIT IAW CL650 AMM 32-44-04. OPS CHECK GOOD.

Source: SDR DXTA2024102300906 · FAA SDRS
J · 2023-11-11 Matched by certificate designator
ATA 3260

SELECTING LDG GEAR DOWN RESULTED IN A RED GEAR DISAGREE CAS LIGHT & AUDIBLE 'GEAR DISAGREE' OVER THE SPEAKER. IT WAS NLG POSITION THAT WAS NOT DOWN & LOCKED. NLG WAS ACTUALLY DOWN, BUT NLG DOORS WERE OPEN DUE TO THE LOUD WINDSTREAM NOISE. GEAR DISAGREE QRH COMPLETED THROUGH STEP (8) WITH THREE DN INDICATIONS DISPLAYED. LANDED WITHOUT INCIDENT. NO DAMAGE TO GEAR OBSERVED. FOUND NLG DOWN LOCK PROX SENSORS BELOW THE MINIMUM 0.06" GAP. ADJUSTED GAP TO 0,064". WORK PERFORMED IAW AMM 32-61-20. PERFORMEO IAW AMM 32-61-20. COMPLIED WITH OPS CHKS OF NLG EXTENSION & RETRACTION SYS GOOD IAW AMM 32-30-00-720-801.

Source: SDR DXTA2023111610067 · FAA SDRS
J · 2023-06-12 Matched by certificate designator
ATA 2600

R JETPIPE OVHT RED CAS: DURING LEVEL FLIGHT AT 40,000' THE RIGHT JETPIPE OVERHEAT CAS MESSAGE ILLUMINATED. CREW PERFORMED JETPIPR OVRHT QRC CHECKLIST. CAS MESSAGE WENT AWAY AS WE RETARDED / REDUCED THE RIGHT POWER LEVER/ THRUST LEVER. PRIOR TO FLIGHT FIRE MONITOR AND FIRE DETECT SYSTEMS TESTED NORMALLY. AFTER DIVERSION, SYSTEMS STILL TESTED NOTMALLY. LIGHT HAS REMAINED OUT. WE WERE IN VISUAL CONDITIONS.//CORRECTICVE ACTION// OPENED RIGHT ENGINE COWLS TO ACCESS JET PIPE FIRE LOOP. INSPECTED FIRE LOOP CONNECTIONS AND FOUND A BROKEN PIN ON FIRE LOOP. REMOVED JET PIPE FIRE LOOP ON RIGHT HAND ENGINE. REF. CHALLENGER 650 MM 26-11-04. REPLACED RIGHT EXHAUST NOZZLE ASSEMBLY SENSING ELEMENT. REF. CHALLENGER 650 MM 26-11-04. OPS CHECK GOOD.PN ON 744-11645 SN ON 191203-191209

Source: SDR DXTA2023061288220 · FAA SDRS
J · 2018-06-01 Matched by certificate designator
ATA 2750

AT FL380, FLAP DISPLAY CAME ON AND INDICATED BETWEEN 2 AND 3 DEGREES. THE F/A CONFIRMED THAT THE FLAPS APPEARED TO BE EXTENDED SLIGHTLY. A FEW MINUTES LATER, FELT THE FLAPS MOVE AND THEY INDICATED 5 DEGREES. THE AUTO THROTTLES FAILED AND NEVER REENGAGED. HYD 1B, 2B, 3B AMBER CAS MESSAGES DISPLAYED FOR APPROXIMATELY THREE MINUTES. FLAP AND HYDRAULIC FUNCTION WAS NORMAL THROUGHOUT THE REST OF THE EMERGENCY DIVERTION AND LANDING.

Source: SDR DXTA201806041023 · FAA SDRS
J · 2018-06-01 Matched by certificate designator
ATA 2751

LEVEL AT FL380, FLAP DISPLAY ILLUMINATED AND INDICATED BETWEEN 2 AND 3 DEGREES. THE F/A CONFIRMED THAT THE FLAPS APPEARED TO BE EXTENDED SLIGHTLY. A FEW MINUTES LATER FELT THE FLAPS MOVE AND THEY INDICATED 5 DEGREES. THE AUTO THROTTLES FAILED AND NEVER RE-ENGAGED. HYD 1B, 2B, 3B AMBER CAS MESSAGES DISPLAYED FOR APPROXIMATELY THREE MINUTES. FLAP AND HYDRAULIC FUNCTION WAS NORMAL THROUGHOUT THE REST OF THE EMERGENCY DIVERTION AND LANDING. REMOVED AND REPLACED THE FLAP CONTROL PANEL AND FLAP POSITION TRANSMITTER. OPS CHECKED SATISFACTORY.

Source: SDR DXTA2018060741023 · FAA SDRS