N223PB

CESSNA 402C · 1979 · Valid Registration

Registered owner: HYANNIS AIR SERVICE INC, MA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
HYANNIS AIR SERVICE INC. (HYIA)Certificate holderMatched by certificate designator
HYANNIS AIR SERVICE INC. (HYIA)Operator2015-02-10 – 2015-02-10Operator named in NTSB report

Accident & incident history

Acc · 2015-02-10 Operator named in NTSB report
CESSNA 402C None injury Part 135HYANNIS AIR SERVICE INC.
Source: NTSB case ERA15LA125
Accident · 2006-03-27 Matched by aircraft (N-number)
Cessna 402C Serious injuryHYANNIS AIR SERVICE INC.
Source: NTSB case MIA06LA071

Maintenance disclosures

O · 2025-11-12 Matched by certificate designator
ATA 6111

DURING DISASSEMBLY FOR SCHEDULED OVERHAUL A CRACK WAS IDENTIFIED AT A SINGLE BLADE ROOT. MULTIPLE BEARING RACES WERE FOUND TO BE CORRODED AND FAILED.

Source: SDR HYIA20251113001 · FAA SDRS
B · 2025-10-08 Matched by certificate designator
ATA 2197

PILOT REPORTED THE AUXILIARY CABIN FAN SWITCH FELT HOT WITH A BURNING SMELL AND NOTED SPARKS. COMPANY MAINTENANCE INSPECTED AND FOUND A BURNT WIRE TERMINAL. THE TERMINAL WAS REPLACED WITH NO FURTHER DEFECTS NOTED.

Source: SDR HYIA20251010001 · FAA SDRS
O · 2023-04-12 Matched by certificate designator
ATA 5712

DURING MAINTENANCE A CRACK WAS DISCOVERED ON THE RIGHT HAND CLOSEOUT RIB (P/N: 5122115-56) AT R.W.S. 106.79. THIS CRACK ORIGINATES FROM A HOLE IN THE FORWARD ROW OF FASTENERS COMMON TO THE AFT MAIN LANDING GEAR TRUNNION SUPPORT PLATE AND TRAVELS FORWARD AN APPROXIMATE LENGTH OF .625 INCHES. THE CRACK IS CONSISTENT WITH OTHERS VISUALLY IDENTIFIED IN THIS SAME AREA. THIS RIB WILL BE REPLACED.

Source: SDR HYIA20230413001 · FAA SDRS
O · 2022-11-22 Matched by certificate designator
ATA 5711

DURING MAINTENANCE A CRACK WAS VISUALLY IDENTIFIED ON THE RH UPPER FWD SPAR CAP PN: 5122031-6. THIS CRACK IS LOCATED NEAR THE FORWARD RADIUS OF THE SPAR CAP AT APPROXIMATE RWS 70.94. THIS CRACK WAS CONFIRMED BY SURFACE EDDY CURRENT, MEASURES APPROXIMATELY 1 INCH LONG, AND IS CONSISTENT WITH OTHER CRACKS VISUALLY IDENTIFIED IN THIS AREA. THE CAP WILL BE REMOVED AND REPLACED USING NEW PARTS.

Source: SDR HYIA20221128001 · FAA SDRS
O · 2022-11-10 Matched by certificate designator
ATA 5410

DURING MAINTENANCE ON N223PB, A MULTIPLE CRACKS WERE VISUALLY IDENTIFIED ON THE RH NACELLE CROSSOVER BEAM (P/N: 5654104-2). ONE CRACK ON THE FRONT FACE OF THE BEAM AT APPROXIMATE RWS 87.44 WITH AN APPROXIMATE LENGTH OF 3.780 INCHES. A SECOND CRACK WAS IDENTIFIED ON THE LOWER CHANNEL PERPENDICULAR TO THE LENGTH OF THE CHANNEL ALSO AT THE SAME WING STATION, EXTENDING FROM THE FRONT FACE ACROSS THE TOP OF THE CHANNEL AND DOWN THE REAR FACE. A THIRD CRACK WAS VISUALLY IDENTIFIED ON THE AFT FACE OF THE BEAM AT THE SAME WING STATION STARTING FROM THE BOTTOM EDGE TRAVELING UP APPROXIMATELY 1.704 INCHES BEFORE TRAVELING UP 2.262 INCHES FURTHER AT AN APPROXIMATE ANGLE OF 30 DEGREES. THIS NACELLE HAD SPECIAL INSPECTION 402-4 COMPLIED WITH 238.5 HOURS AGO, AND SPECIAL INSPECTION 402-1 COMPLIED WITH 60.7 HOURS AGO. THIS BEAM WILL BE REPLACED USING NEW PARTS.

Source: SDR HYIA20221114002 · FAA SDRS
O · 2022-02-08 Matched by certificate designator
ATA 5415

WHILE PERFORMING THE LIGHTED BOROSCOPE INSPECTION PROCEDURE AS OUTLINED IN TEXTRON MEL-54-02R2 TO SATISFY AD2017-10-19, A CRACK WAS IDENTIFIED ON THE OUTBOARD RADIUS OR THE LEFT HAND OUTBOARD NACELLE FITTING. THIS CRACK MEASURES APPROXIMATELY .119 INCHES LONG AND IT'S LOCATION IS CONSISTENT WITH OTHERS FOUND USING THIS SAME METHOD. THIS FITTING HAS BEEN REMOVED AND WILL BE REPLACED USING NEW SUPERSEDED P/N: 5292029-31.

Source: SDR HYIA20220216001 · FAA SDRS
B · 2021-12-19 Matched by certificate designator
ATA 2140

THE PILOT REPORTED A BURNING SMELL DURING CLIMB OUT. MAINTENANCE INSPECTED AND FOUND THE HEATER BLOWER INOPERATIVE. THIS WAS REPLACED WITH NO FURTHER DEFECTS NOTED.

Source: SDR HYIA20211224001 · FAA SDRS
O · 2018-08-13 Matched by certificate designator
ATA 5530

CORROSION WAS DISCOVERED ON ONE OF THE LEFT SIDE VERTICAL STABILIZER AFT ANGLES. REMOVED AND REPLACED THE ANGLE.

Source: SDR HYIA20180815001 · FAA SDRS
O · 2016-07-14 Matched by certificate designator
ATA 3233

PILOT REPORTED RT MLG DOWN AND LOCKED LIGHT INOPERATIVE AFTER EXTENSION, EMERGENCY T-HANDLE PULLED. MAINTENANCE INSPECTED AND REPLACED THE RT MLG ACTUATOR ASSEMBLY IAW 32-30-02, PERFORMED SEVERAL GEAR SWINGS AND OPERATIONALLY CHECKED GOOD. SERVICED THE EMERGENCY BLOW DOWN BOTTLE.

Source: SDR HYIA20160718001 · FAA SDRS
O · 2015-06-18 Matched by certificate designator
ATA 5711

DURING SCHEDULED INSPECTION, AREAS OF EXFOLIATING CORROSION WERE FOUND AT LT WING LOWER FWD SPAR CAP STRAP, OEM PN 5292029-1, PREVIOUSLY INSTALLED VIA SERVICE KIT SK402-47 ON MARCH 10, 2004 TO SATISFY REQUIREMENT OF AD2005-12-13 CONCURRENT WITH MEB05-2 AS TERMINATING ACTION FOR AD2005-05-52. THE AFFECTED PARTS WILL BE REPLACED WITH FACTORY NEW FOLLOWING A DETAILED INSPECTION OF SURROUNDING STRUCTURE UPON DISASSEMBLY.

Source: SDR HYIA20150622001 · FAA SDRS
O · 2015-06-06 Matched by certificate designator
ATA 3242

PILOT REPORTED LT BRAKE FAILURE. ACFT IS CURRENTLY IN HEAVY MX, CORRECTIVE ACTION NOT AVAILABLE AT THIS TIME.

Source: SDR HYIA20150611001 · FAA SDRS
B · 2014-04-18 Matched by certificate designator
ATA 2120

PILOT REPORTED A FUEL ODOR IN THE COCKPIT. PERFORMED A FUEL PRESSURE TEST & NO DEFECTS WERE NOTED, NO ACTION TAKEN.

Source: SDR HYIA20140421109 · FAA SDRS
K B · 2012-09-07 Matched by certificate designator
ATA 2820

PILOT REPORTED THAT DURING PREFLIGHT INSPECTION, THERE WAS A STRONG ODOR OF FUEL IN THE COCKPIT. MX INSPECTED THE ENTIRE FUEL SYS IN ACFT AND IN THE HEATER. FOUND A LOOSE B-NUT IN LT WHEEL WELL WITH EVIDENT STAINS. B-NUT WAS TIGHTENED AND NO OTHER LEAKS WERE NOTED.

Source: SDR HYIA20120907001 · FAA SDRS
K B · 2012-08-31 Matched by certificate designator
ATA 2820

THE PILOT REPORTED THAT DURING FLIGHT, THERE WAS A FUEL ODOR PRESENT IN THE CABIN. ON LANDING AND INSPECTION, A B-NUT ON THE RT CROSSFEED LINE IN THE FUEL BOWL BAY WAS TIGHTENED. THIS RESOLVED THE ISSUE WITHOUT FURTHER DISCREPANCY.

Source: SDR HYIA20120904003 · FAA SDRS
B · 2012-08-23 Matched by certificate designator
ATA 3297

DURING CLIMB, PILOT EXPERIENCED A MOMENTARY BURNING ODOR IN COCKPIT DURING GEAR RETRACTION. AFTER INSPECTION, THE DISCREPANCY WAS RESOLVED BY REPAIRING AND REROUTING WIRE BUNDLE IN NOSE GEAR WHEEL WELL.

Source: SDR HYIA08242012001 · FAA SDRS
O · 2011-04-05 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE, OEM PN 5142002-5, WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE WITHIN ALLOWABLE LIMIT. THIS UNIT HAS BEEN REPAIRED IAW PROCEDURE OUTLINED IN MEB941-11R1 & RETURNED TO SERVICE.

Source: SDR HYIA20140415041 · FAA SDRS
N · 2010-02-24 Matched by certificate designator
ATA 3260

IN CRUISE FLIGHT, CREW REPORTED, WITH LANDING GEAR UP AND LOCKED, AND ALL GEAR INDICATIONS NORMAL, NUMEROUS CAUTION/WARNING LIGHT FLICKERED AND THEN REMAINED ILLUMINATED. GEAR WARNING HORN ALSO SOUNDED FOR A SECOND. ANNUCIATOR LIGHTS THAT ILLUMINATED WERE, LOW VOLTAGE, LT AND RT ALTERNATOR INOP LIGHTS, HYD PRESSURE LIGHT, LT AND RT HYD FLOW LIGHTS, TURN AND BANK TEST, ALL 3 DOWN AND LOCK LIGHTS AND GEAR UNLOCK (IN TRANSIT) LIGHT. NO EVIDENCE OF ACTUAL GEAR EXTENSION WAS NOTED. AFTER COMPLETEING GEAR WILL NOT EXTEND HYD CHECKLIST AND PERFORMING EMERGENCY GEAR EXTENSION, GEAR WARNING HORN STILL SOUNDED WITH THROTTLES RETARDED OR WITH FLAPS BELOW 15 DEGREES. EMERGENCY WAS DECLARED, BUT LANDING WAS UNEVENTFUL. MX INSPECTED ACFT, CLEANED AND RESECURED CONNECTIONS TO ANNUCIATOR DIODE BOARD ASSY. ALL SYS CHECKED NORMAL.

Source: SDR HYIA223PBANNUC · FAA SDRS
J · 2009-11-12 Matched by certificate designator
ATA 3222

CREW REPORTED, AFTER TAKEOFF, HYD PRESSURE LIGHT AND GEAR UNLOCK LIGHT REMAINED ILLUMINATED. SECOND ATTEMPT RESULTED IN SAME INDICATIONS. CREW SELECTED GEAR DOWN WITH NORMAL INDICATIONS (3 GREEN DOWN AND LOCKED LIGHTS). AFTER LOW APPROACH, TOWER REPORTED GEAR SEEMED TO BE DOWN. TO INSURE THAT GEAR WAS DOWN AND LOCKED, CREW ELECTED TO USE EMERGENCY EXTENSION PROCEDURES. EMERGENCY WAS DECLARED, LANDING WAS UNEVENTFUL. MX INSPECTED ACFT, FOUND NOSE GEAR STRUT UNDER INFLATED. SERVICED NOSE STRUT, PERFORMED SEVERAL EXTENSION AND RETRACTION TEST, SYS CHECKED NORMAL. ACFT RELEASED BACK TO SERVICE.

Source: SDR HYIA223PB1112NLG · FAA SDRS
N · 2009-10-13 Matched by certificate designator
ATA 3260

CREW REPORTED AFTER TAKE OFF AND GEAR RETRACTION,(DOWN LOCK LIGHTS EXTINGUISHED) THE HYD PRESSURE LIGHT AND GEAR UNLOCK LIGHT REMAINED ILLUMINATED. RECYCLED GEAR, SAME INDICATION. CREW ELECTED TO EXTEND GEAR, NORMAL EXTENSION (3 GREEN ILLUMINATED AND HYD PRESSURE LIGHT EXTINGUISHED). RETURNED TO BLOCK, LANDING UNEVENTFUL. MX PERFORMED SEVERAL EXTENSION AND RETRACTION TEST, COULD NOT DUPLICATE LANDING GEAR MALFUNCTION. AS A PRECAUTIONARY MEASURE, CLEANED AND LUBED ALL UPLOCK SWITCHES.

Source: SDR HYIA223PBGEAR1013 · FAA SDRS
J · 2007-08-05 Matched by certificate designator
ATA 2497

ON 08-05-07, LEFT ALTERNATOR OUT LIGHT CAME ON IN FLIGHT AND RT ALT OUT CAME ON INTERMITTENTLY. MX INSPECTED AND REPAIRED WIRING TO LT ALT AND SECURED WIRE TO RT ALT FUSE IN COCKPIT, SECONDARY INSP AND RUN UP WAS PERFORMED ON 08-06-07 WITH NO DEFECTS NOTED.

Source: SDR 135N223PB · FAA SDRS
H · 2006-06-26 Matched by certificate designator
ATA 2460

CREW REPORTED AVIONICS MASTER SWITCH INOP. MX CHANGED CIRCUIT BREAKER.

Source: SDR 135N223PB0502 · FAA SDRS