N236AL

BEECH C-99 · 1987 · Valid Registration

Registered owner: ALPINE AVIATION INC, UT (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ALPINE AVIATION, INC. (TIMA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

B · 2024-03-04 Matched by certificate designator
ATA 3310

6 MILES FROM IAF OKAVE FOR RNAV 35 INTO KRXE SMELLED SOMETHING ACRID & LOOKED AROUND COCKPIT. SAW A SMALL BIT OF WHITE SMOKE COMING OUT FROM LOWER RT OF INSTRUMENT PANEL. SAW ANOTHER PUFF OF SMOKE & A FAINT FLICKERING LIGHT IN REFLECTION OF THE PNEUMATIC PRESSURE GAUGE. TURNED OFF PANEL LIGHTS & TURNED OFF OTHER ELECTRICAL SOURCES, LOOKED AT CIRCUIT BREAKER PANEL & VERIFIED NO TRIPPED BREAKERS. CONTINUED TO MONITOR PANEL & FIRE THERE WAS DID NOT APPEAR TO SPREAD OR WORSE. SMOKE STOPPED EMANATING FROM PANEL. TOLD ATC I HAD A POTENTIAL ELECT FIRE & THEY ASKED IF I WANTED TO DECLARE AN EMERGENCY & ASKED IF I NEEDED ANY ASSISTANCE. SINCE ISSUE APPEARED TO ME TO BE UNDER CONTROL, DIDN’T WANT TO DECLARE & DIDN’T NEED ANY ASSISTANCE SINCE WAS IN VMC SO CLOSE TO DESTINATION & SUFFERED NO LOSS OF SYSTEMS OR CONTROLS. ALREADY HAD CLEARANCE, CONTINUED APPROACH & LANDED IN VMC. AFTER LANDING, BROUGHT FLAPS UP & TURNED OFF AVIONICS & BATTERY MASTER SWITCHES, CALLED FLT SERVICES HAD LANDED SAFELY. AT NO POINT DID IT SEEM NECESSARY TO ENGAGE COCKPIT FIRE EXTINGUISHER. MECHANIC FOUND THAT A PANEL CONTAINING THE DIODES FOR INSTRUMENT BACKLIGHTING WAS THE CULPRIT. ONE OF THE DIODES HAD SHORTED & ARC CREATED FLASHING & SMOKE. THE LIGHT PANEL WAS REMOVED AND PANEL LIGHTS WERE DEFERRED.

Source: SDR TIMA20240304006 · FAA SDRS
O · 2018-02-13 Matched by certificate designator
ATA 3244

DURING POST-FLIGHT INSPECTION, FOUND A CHUNK OF RE-TREAD MISSING.

Source: SDR TIMA20180223004 · FAA SDRS
S · 2017-05-03 Matched by certificate designator
ATA 3244

DURING LANDING ROLL THE TIRE TREAD SEPARATED FROM THE NR 3 MLG TIRE. TIRE WAS A RECAP.

Source: SDR TIMA20170503008 · FAA SDRS
O · 2016-08-22 Matched by certificate designator
ATA 5730

THE LEFT WING LEADING EDGE CENTER SECTION WAS FOUND TO HAVE CORROSION ON SKIN BETWEEN BONDED LAYERS DURING MAINTENANCE.

Source: SDR TIMA20160822014 · FAA SDRS
S · 2016-02-27 Matched by certificate designator
ATA 2432

SHORTLY AFTER LEVEL OFF, BOTH FUEL QTY INDICATORS SHOWED ZERO FUEL. PILOT ELECTED TO RETURN TO TAKEOFF LOCATION. TROUBLESHOOTING REVEALED A LOW VOLTAGE CONDITION DUE TO A WEAK ACFT BATTERY.

Source: SDR TIMA20160227003 · FAA SDRS
O · 2014-02-17 Matched by certificate designator
ATA 5521

INSPECTION REVEALED A CRACK IN THE RT ELEVATOR LE RIB. THE RIB WAS REPLACED WITH A NEW RIB.

Source: SDR TIMA20140217006 · FAA SDRS
O · 2010-02-10 Matched by certificate designator
ATA 5753

LIB FLAP CRACKED.

Source: SDR TIMA2010000014 · FAA SDRS
K J · 2006-06-16 Matched by certificate designator
ATA 7210

OIL PRESSURE ANNUNCIATOR ILLUMINATED, GAUGE INDICATED OIL PRESSURE WAS LOW. PILOT ELECTED TO SHUTDOWN ENGINE. INVESTIGATION REVEALED CORROSION INTERNALLY IN THE REAR RGB CASE HAD CREATED AN OIL LEAK RESULTING IN EXCESSIVE OIL LOSS FOR THE ENGINE.

Source: SDR TIMR200600001 · FAA SDRS
O · 2003-03-03 Matched by certificate designator
ATA 5711

DURING AN ANNUAL WING OUTBOARD UPPER AND LOWER MAIN SPAR CAP INSPECTION SEVERAL SMALL SPOTS WERE NOTICED. FURTHER INVESTIGATING REVEALED CONSIDERABLE CORROSION.

Source: SDR TIM2003F00000 · FAA SDRS
W · 2000-07-17 Matched by certificate designator
ATA 3222

THE PART WAS ORDERED NEW FROM BEECHCRAFT WITH THE TOP HOLES DRILLED INCORRECTLY. THE TOP LEFT HOLE IS SUPPOSED TO BE 1.75 INCHES AND IT WAS DRILLED ON THIS UNIT 1.50 INCHES. (X)

Source: SDR 20000811SH005 · FAA SDRS