N241BC

EMBRAER EMB-145EP · 1998 · Valid Registration

Registered owner: IBC AIRWAYS INC, FL (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
IBC AIRWAYS, INC. (OZCA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

N · 2026-02-06 Matched by certificate designator
ATA 3260

CREW REPORTED ON DEPARTURE THE LANDING GEAR ICAS MESSAGE LG/LEVER DISAGREE. RH MLG NOTED AS NOT UP AND LOCKED. CREW PUT THE GEAR DOWN AND REPORTED THREE DOWN AND LOCKED. AN EMERGENCY WAS DECLARED AND THE AIRCRAFT LANDED WITHOUT INCIDENT. UPON INSPECTION OF THE RH MLG, IT WAS FOUND THAT THE SUPPORT FOR THE PROXIMITY SWITCH (PN 2309-2070-004) WAS CRACKED THROUGH THE MOUNTING HOLE FOR THE SWITCH ON THE SUPPORT. THE CRACK ALLOWED THE PROXIMITY SWITCH TO SEPARATE FROM THE SUPPORT. THE SUPPORT WAS REPLACED, OPERATIONAL CHECK WAS PERFORMED AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 2026F00011 · FAA SDRS
B · 2024-10-09 Matched by certificate designator
ATA 3460

ENROUTE FROM KMIA TO WMCR FOR HURRICANE EVACUATION, OVER CUBAN AIRSPACE, THE FMS DISPLAY AS WELL AS ROUTE INFORMATION ON THE MFD WERE LOST, AFTER THIS A SMELL OF BURNT CABLES COULD BE DETECTED. FMS CB'S WERE PULLED AND AN EMERGENCY DECLARED TO LAND AT SANTA CLARA AIRPORT. AFTER PULLING THE CBS THE SMELL DISSIPATED. TECHNICIANS ON BOARD SECURED THE CBS AND DEFERRED THE FMS IAW THE MEL. THE AIRCRAFT CONTINUED TO WMCR AND LANDED WITHOUT INCIDENT. WHEN THE AIRCRAFT RETURNED TO KMIA, MAINTENANCE REPLACED THE FMS CDU AND RETURNED THE AIRCRAFT TO SERVICE.

Source: SDR OZCA2024007241 · FAA SDRS
B · 2020-04-02 Matched by certificate designator
ATA 2150

PACK 2 FAILED CAUSING RISE IN CABIN TEMP AND FA REPORTED SMOKE SMELL IN CABIN

Source: SDR OZCA20200515402 · FAA SDRS
K J · 2019-03-14 Matched by certificate designator
ATA 2761

WHILE TAXING TO THE GATE AFTER LANDING, INBOARD SPOILER FAIL MESSAGE ILLUMINATED ON EICAS SCREEN. SHORTLY FOLLOWED BY E1 HYDRAULIC PUMP FAIL AND HYD SYSTEM FAIL. CORRECTIVE ACTION: UPON INSPECTION, FOUND LEFT INBOARD SPOILER ACTUATOR CRACKED CAUSING LEAKAGE OF FLUID DURING SPOILER ACTIVATION. REMOVED AND REPLACED SPOILER ACTUATOR AS PER AMM. OPERATIONAL AND LEAKS CHECKS SATISFACTORY.

Source: SDR OZCA2019F00155 · FAA SDRS
K J · 2014-06-21 Matched by certificate designator
ATA 2910

CREW RECEIVED HYD SYS 1 FAILURE MSG ON THE ICAS DURING DESCEND. AS A PRECAUTIONARY MEASURE, CREW ELECTED TO DECLARE AN EMER, SUBSEQUENT LANDING WAS UNEVENTFUL. FOUND A HYD LEAK AT ENG DRIVEN PUMP HYD PRESS SWITCH. REPLACED ENG DRIVEN HYD PUMP PRESS SWITCH O RING. PERFORMED LEAK & OPERATIONS CHECKED & RELEASED ACFT BACK TO SERVICE.

Source: SDR OZCA20140623001 · FAA SDRS
K J · 2013-10-30 Matched by certificate designator
ATA 2761

WARNING INDICATION ON EICAS, HYD SYSTEM NR 1 LOW. MX INSPECTED THE ACFT AND FOUND THE RT INBD GROUND SPOILER ACTUATOR HOUSING WAS CRACKED. UNIT REPLACED WITH REPAIRED UNIT AND ACFT RELEASED TO SERVICE.

Source: SDR OZCA20131031001 · FAA SDRS