N243JX

EMBRAER EMB-145LR · 2000 · Valid Registration

Registered owner: DELUX PUBLIC CHARTER LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
DELUX PUBLIC CHARTER LLC (4DPA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

N · 2025-04-06 Matched by certificate designator
ATA 3150

CREW REPORTED-AT FL330 GOT BLD VLV 2 FAIL. EXECUTED QRH. RETURNED TO OPF. CORR ACTION- REMOVED, CLEANED, INSPECTED AND REINSTALLED FAN AIR VALVE FILTER #2. INSPECTED ALL SENSE LINES AROUND FAN AIR VALVE #2 AS WELL AS LEAK CHECKS WITH ENGINES RUNNING. PERFORMED OPS CHECK OF ENGINE BLEED VALES WITH OPS CHECK GOOD.

Source: SDR 4DPA2025040600001 · FAA SDRS
O · 2024-05-21 Matched by certificate designator
ATA 5743

LH AFT MAIN LANDING GEAR TRUNNION FITTING CRACKED. REMOVED AND REPLACED LH MAIN LANDING GEAR TRUNNION FITTING IAW TI-145-14-018LH REV.F DATE 07-NOV-2022

Source: SDR V0XR20240711001 · FAA SDRS
O · 2024-05-21 Matched by certificate designator
ATA 5743

RIGHT MAIN LANDING GEAR TRUNNION CRACKED. REMOVED AND REPLACED RT MAIN LANDING GEAR TRUNNION IAW TI-145-14-018 RH REV.G 07-NOV-2022

Source: SDR V0XR20240711AV2 · FAA SDRS
K · 2024-03-23 Matched by certificate designator
ATA 2810

CREW REPORTED AFTER TAKEOFF, SUSPECTED FUEL LEAK ON LEFT WING REPORTED BY FA IN FLIGHT. INDICATIONS SHOWED LESS FUEL ON LEFT WING THAN RIGHT WING. AIR RETURN. FUEL STOPPED SPRAYING BEFORE LANDING. NORMAL INDICATIONS ON GROUND. CORR ACTION- MX INSPECTED LEFT WING FOR FUEL LEAK NONE NOTED RTS'D AIRCRAFT.

Source: SDR 4DPA2023032300001 · FAA SDRS
J · 2022-08-29 Matched by certificate designator
ATA 2210

ISSUE- CREW REPORTED AT LEVEL FL350. TOUCHED NOTHING. RECEIVED A “PTRIP MAIN INOP” EICAS MESSAGE FOLLOWED BY AN ASSOCIATED “AP TRIM FAIL” AN “AP ELVE MISTRIM”. RAN AND FOLLOWED QRH PROCEDURES DIVERTED TO DAL. CORR ACTION MX TROUBLESHOT TO BAD HSCU R&R HSCU. OPS CHECK GOOD NO DEFECTS NOTED.

Source: SDR 4DPA2022082900001 · FAA SDRS
J B O · 2022-07-04 Matched by certificate designator
ATA 7100

CREW REPORTED-THERMAL RUNAWAY SHORTLY AFTER LEVELING AT FL370. ITT BEGAN CLIMBING. PULLED BACK #2 THRUST LEVER AND ITT CLIMBED ABOVE 1000. ELECTED TO SHUT DOWN ENGINE #2 AS IT GAVE UP THE GHOST AS WELL. ENGINE SHUT DOWN WITHOUT ISSUE. BEFORE SHUTDOWN OIL PRESSURE ON #2 AT ZERO. FA REPORTED HEARING A “POP” AND A SMALL AMOUNT OF DETECTABLE SMOKE APPEARED IN THE CABIN. STARTED APU. SMOKE CLEARED. MADE NORMAL LANDING ON ENGINE #1. AND ON DESCENT EICAS MESSAGE #1 FIRE DETECT FAIL. CLEARED ON ITS OWN. CORR ACTION- R&RING #2 ENGINE

Source: SDR 4DPA2020070400001 · FAA SDRS
J · 2021-07-19 Matched by certificate designator
ATA 2130

CREW RTF BACK TO LAS DUE TO AN UNUSUAL WIND SOUND BUT EVERYTHING WAS WORKING NORMALLY. AIRCRAFT WAS PRESSURIZING BUT CABIN ALT STOPPED AT APPROXIMATELY 1500’ AND THEN PRESSURE CONTINUED TO GO UP, REACHING AROUND 5PSI. BETWEEN 15000 AND 19000 FEET PRESSURE STARTED CLIMBING QUICKLY BUT CABIN ALT REMAINED AROUND 1500’. WE LEVELED OFF AND CONTACTED CLEARANCE FOR RETURN AT WHICH TIME CABIN PRESSURE WAS AT 7.6 AND ALT SHOWED ZERO. AS WE STARTED TO DESCEND TO 15000’ CABIN PRESS CLIMBED TO 8.0 PSI, WITH ALT BLANKED, AND RATE WAS ALL OVER THE PLACE BETWEEN 3200 DOWN AND 1900 UP. TRIED SECURING A PACKS BUT DIDN’T DO MUCH TO RATE. TURNED PACKS BACK ON AND TRIED IN MANUAL WITH THE SAME RESULT. PASSING 13000’ TURNED BOTH PACKS OFF AGAIN AND GOT THE PLANE TO SLOWLY BLEED OFF PRESSURE TO COINCIDE WITH DESCENT. UNEVENTFUL ON GROUND. REMOVED CPAM AND INSTALLED SERVICEABLE CPAM FROM N246JX,PERFORMED OPS CHECK NO FAULT NOTED

Source: SDR 4DPA202107219001 · FAA SDRS