N244JX

EMBRAER EMB-145LR · 2000 · Valid Registration

Registered owner: DELUX PUBLIC CHARTER LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
DELUX PUBLIC CHARTER LLC (4DPA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2025-01-17 Matched by certificate designator
ATA 3040

CREW REPORTED-AFTER TAKEOFF AT KHPN UPON REACHING 8000FT, THE RIGHT WINDSHIELD WIPER STARTED TO SLOWLY MOVE AND ROTATE ON ITS OWN WHILE THE CONTROLS WERE IN THE OFF POSITION. TO ATTEMPT TO RESET THE WIPER, WE ACTIVATED EACH OF THE WIPER CONTROL SETTINGS SWITCHING FROM LOW TO HIGH TO TIMER. THE WIPER DID NOT RESPOND TO OUR CONTROLS AND CONTINUED TO SLOWLY MOVE ON ITS OWN. DUE TO THE WIPER SPEED RESTRICTIONS WE DECIDED TO AIR RETURN BACK TO HPN. CORR ACTION MX PERFORMED WIPER CB RESET AND OPS CHECK WITH THE CREW OPS CHECK NORMAL. NO PREVIOUS HISTORY.

Source: SDR 4DPA2025011700001 · FAA SDRS
E W · 2025-01-06 Matched by certificate designator
ATA 5300

CREW REPORTED- PASSING 10000’ FEET A LOUD HUMMING NOISE AND STRONG VIBRATION FROM THE COCKPIT THROUGH ROW 7 , CAB RATE WAS SHOWING ZERO AS WE WERE CLIMBING OUT AN AIR RETURN WAS MADE TO BCT DUE TO THE ISSUE. CORR ACTION- MX FOUND WET RTV FWD OF STARLINK WIFI ANTENNA. RTV 230 SEALANT WAS APPLIED.

Source: SDR 4DPA2025010600002 · FAA SDRS
O · 2024-01-08 Matched by certificate designator
ATA 5330

REAR FUSELAGE I SKIN DAMAGED FORWARD OF THE CARGO DOOR AT FRAME 61 AND STRINGER 17L. THE DAMAGE IS ALONG THE RIVETS AND LOOKS LIKE A CRACKED PUNCTURE. AFTER FURTHER INSPECTION, THE CORROSION GOES COMPLETELY THROUGH. REPAIRED IAW EMBRAER ETD2021-145-000003 REV.:/

Source: SDR V0XR20240116AV1 · FAA SDRS
J · 2022-07-17 Matched by certificate designator
ATA 3460

CREW REPORTED-IC 600 1 FAIL IN FLIGHT LEVEL 340. LOST ASSOCIATED SCREENS (PFD1, MFD1, EICAS) AND AUTOPILOT. RAN QRH PROCEDURE AND RETURNED TO DAL. CORR ACTION- MX PERFORMED SYSTEM RESET AND RERACK OF IC-600 #1 SYSTEM OPS TESTED GOOD. HAS FLOWN THREE 3 LEGS SINCE NO FURTHER ISSUES NOTED.

Source: SDR 4DPA2022071700001 · FAA SDRS
O · 2022-01-14 Matched by certificate designator
ATA 2210

ISSUE: AP YAW DAMP WOULDN'T ENGAGE ON CLIMB OUT APPROX 500' CREW CONTACTED MISSION CONTROL AND RETURNED TO DALLAS. AIRCRAFT STILL BEING TROUBLESHOT AS OF 1/24/2022.

Source: SDR 4DPA2022011400001 · FAA SDRS