N249TX

BOMBARDIER INC CL-600-2B16 · Valid Registration

Registered owner: CRITERION AVIATION LOGISITCS LLC, DE (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
JET LINX AVIATION, LLC (9JLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2022-09-17 Matched by certificate designator
ATA 2210

THE FLIGHT CREW REPORTED THAT THE AUTO PILOT FAILED, AFTER FAIL OF THE YAW DAMPENER NO2 AND THE FAILURE OF THE FD NO2 AND ALL RIGHT SIDE NAV DATA WENT BLANK. THE FLIGHT CREW RAN THE CHECKLIST AND ELECTED TO DIVERT THE FLIGHT AND LAND FOR MAINTENANCE CONSIDERATIONS. THE MAINTENANCE PROVIDER TROUBLESHOOT AND DETERMINED THE FLIGHT CONTROL COMPUTER 2A WAS DEFECTIVE. THE DEFECTIVE COMPUTER WAS REMOVED AND A REPLACED WITH AN OVERHAULED UNIT. OPS CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2022100325746 · FAA SDRS
J · 2022-09-11 Matched by certificate designator
ATA 3040

THE FLIGHT CREW DESCRIBED AFTER TURNING ON WINDSHIELD HEAT, EITHER HIGH OR LOW SETTING. AFTER 2 MINUTES THE CAUTION LIGHT AND LH WINDOW HEAT CAUTION MESSAGE WOULD ILLUMINATE. RECYCLING SWITCH DID NOT CORRECT ISSUE. THE MAINTENANCE TEAM TROUBLESHOT THE LEFT WINDSHIELD HEAT AND FOUND SENSOR WITH TERMINALS A&B DEFECTIVE. THE TECH SWAPPED WIRES TO THE SPARE SENSOR WITH TERMINALS C&D. PERFORMED OPERATIONAL CHECKS, OPS CHECKS GOOD. NO OTHER DEFECTS NOTED. THIS WINDSHIELD WAS INSTALLED AS NEW 14 MONTHS PRIOR.

Source: SDR 9JLA2022091525745 · FAA SDRS
J · 2022-08-04 Matched by certificate designator
ATA 4990

THE FLIGHT CREW REPORTED THAT THE APU FAILED DURING TAXI. THEY INDICATED THIS WAS THE FORTH TIME IT HAD FAILED. THE MAINTENANCE TEAM TROUBLESHOT AND DETERMINED THE APU LOW OIL PRESSURE SWITCH WAS DEFECTIVE. A NEW APU LOW OIL PRESSURE SWITCH WAS INSTALLED. OPS CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2022081125742 · FAA SDRS
J · 2021-12-05 Matched by certificate designator
ATA 3040

THE FLIGHT CREW REPORTED A RIGHT WINDSHIELD CAS MESSAGE IN FLIGHT. THE MAINTENANCE TEAM TROUBLESHOT AND DETERMINED THE DUEL CHANNEL TEMP CONTROLLER WAS DEFECTIVE. THE TEMP CONTROLLER WAS REMOVED AND A INSPECTED CONDITION CONTROLLER WAS INSTALLED. OPERATIONAL CHECKS WEE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021120927794 · FAA SDRS
O · 2021-10-22 Matched by certificate designator
ATA 2752

THE MAINTENANCE TEAM DISCOVERED DURING POSTFLIGHT CHECKS THE LEFT INBOARD FLAP OUTBOARD ACTUATOR WAS MAKING A GRINDING NOISE WHEN THE FLAPS WERE OPERATED. AFTER EXTENSIVE TROUBLESHOOTING IT WAS DETERMINED THAT THE INBOARD FLAP ACTUATOR WAS FOUND TO BE DEFECTIVE. THE DEFECTIVE ACTUATOR WAS REMOVED AND A NEW ACTUATOR WAS INSTALLED. RIGGING AND OPERATIONAL CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE. A TEARDOWN REPORT WAS REQUESTED.

Source: SDR 9JLA2021110227789 · FAA SDRS
N · 2021-09-28 Matched by certificate designator
ATA 7500

THE FLIGHT CREW REPORTED THAT DURING FLIGHT RECEIVING AN AMBER "BLEED AIR OVERTEMP - L" ADVISORY. THE CREW ATTEMPTED ONE RESET OF SYSTEM, BUT THE MESSAGE RE-APPEARED. THE CREW TURNED THE LH BLEED AIR SYSTEM OFF PER CHECKLIST THE REMAINDER OF THE FLIGHT. THE MAINTENANCE TEAM GAINED ACCESS TO THE LH ENGINE PYLON AREA, TROUBLESHOT THE SYSTEM AND DETERMINED THE LH PRECOOLER TEMP CONTROL SENSOR WAS DEFECTIVE. A NEW SENSOR WAS INSTALLED AND FUNCTIONAL CHECKS WERE SATISFACTORY. THE AIRCRAFT WAS THEN RETURNED TO SERVICE.

Source: SDR 9JLA2021093033079 · FAA SDRS
J · 2021-09-24 Matched by certificate designator
ATA 7500

THE FLIGHT CREW REPORTED THE 14TH STAGE VALVE CHECK FAIL. THE MAINTENANCE TEAM TROUBLESHOT AND FOUND THE 14TH STAGE ISOLATION VALVE WAS DEFECTIVE. THE DEFECTIVE VALVE WAS REMOVED AND OVERHAULED VALVE WAS INSTALLED. OPERATIONAL CHECKS WERE SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021100527786 · FAA SDRS
N · 2021-07-03 Matched by certificate designator
ATA 7200

THE FLIGHT CREW REPORTED THAT DURING THE TAKEOFF ROLL ATTEMPT A RED CAS ENGINE LIGHT ILLUMINATED BELOW V1 DUE TO THIS THE CREW ABORTED THE TAKEOFF AND RETURNED BACK TO PARKING FOR EVALUATIONS. THE FLIGHT CREW SUSPECTED AN OVERSPEED HAD OCCURRED ON THE NO1 ENGINE. THE MAINTENANCE TEAM DOWNLOADED THE ENGINE COMPUTER AND DETERMINED THAT THE EXCEEDANCE WAS STILL WITHIN THE NORMAL OPERATING RANGE OF THE ENGINE. PREFORMED MAX POWER RUNS WITH NO DEFECTS NOTED. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2021072727767 · FAA SDRS