N24MG
Operators of this aircraft
Who operated this tail, and how firmly we know it.
| Operator | Role | Period | Basis |
|---|---|---|---|
| REDDING AERO ENTERPRISES, INC. (MNVA) | Operator | 2020-02-06 – 2020-02-06 | Operator named in NTSB report |
Accident & incident history
Maintenance disclosures
SHORTLY AFTER TAKEOFF FROM ISP THE PILOT NOTICED SMOKE IN THE COCKPIT. THE PILOT IMMEDIATELY RETURNED TO DEPARTURE AND LANDED. THE PILOT REPORTED THAT THE SMOKE APPEARED TO BE CAUSED BY AN ELECTRICAL PROBLEM. THE PILOT REPORTED THAT THE GPS NO LONGER OPERATED. ON 9/12/2007, MECHANIC INSPECTED THE AIRCRAFT, REMOVED THE GPS AND FOUND THAT IT SMELLED OF ELECTRICAL SMOKE, THE MECHANIC EXAMINED THE RADIO RACK, WIRING HARNESSES AND ENTIRE INSTRUMENT PANEL AREA AND FOUND NO PROBLEM. THE ENGINE COMPARTMENT AND ELECTRICAL EQUIPMENT BOX WERE INSPECTED WITH NO PROBLEMS FOUND. THE AIRCRAFT WAS GROUND RUN AND ALL ELECTRICAL EQUIPMENT WAS OPERATIONAL TESTED WITH THE GPS UNIT REMOVED AND ALL OPERATED NORMALLY. THE GPS WAS PLACED ON MEL AND THE AIRCRAFT WAS RELEASED FOR SERVICE. (K)
PILOT REPORTED RT ENGINE RUNS ROUGH. FOUND NO COMPRESSION NR 6 CYLINDER. FOUND METAL IN MAIN OIL SCREEN. FOUND NR 6 ROD BOLT BROKEN AND CONNECTING ROD BROKEN LOOSE FROM CRANKSHAFT. MAJOR DAMAGE TO CRANKCASE, CRANKSHAFT, ROD, AND CYLINDERS. SUBMITTER SUSPECTED IMPROPER HEAT TREATMENT OF ROD BOLT. BOLT TO BE SENT TO THE MANUFACTURER FOR FURTHER TESTING.