N24MG

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
REDDING AERO ENTERPRISES, INC. (MNVA)Operator2020-02-06 – 2020-02-06Operator named in NTSB report

Accident & incident history

Acc · 2020-02-06 Operator named in NTSB report
Cessna 208 Minor injury Part 135REDDING AERO ENTERPRISES, INC.
Source: NTSB case WPR20CA089

Maintenance disclosures

B · 2007-09-11 Unresolved
ATA 3457

SHORTLY AFTER TAKEOFF FROM ISP THE PILOT NOTICED SMOKE IN THE COCKPIT. THE PILOT IMMEDIATELY RETURNED TO DEPARTURE AND LANDED. THE PILOT REPORTED THAT THE SMOKE APPEARED TO BE CAUSED BY AN ELECTRICAL PROBLEM. THE PILOT REPORTED THAT THE GPS NO LONGER OPERATED. ON 9/12/2007, MECHANIC INSPECTED THE AIRCRAFT, REMOVED THE GPS AND FOUND THAT IT SMELLED OF ELECTRICAL SMOKE, THE MECHANIC EXAMINED THE RADIO RACK, WIRING HARNESSES AND ENTIRE INSTRUMENT PANEL AREA AND FOUND NO PROBLEM. THE ENGINE COMPARTMENT AND ELECTRICAL EQUIPMENT BOX WERE INSPECTED WITH NO PROBLEMS FOUND. THE AIRCRAFT WAS GROUND RUN AND ALL ELECTRICAL EQUIPMENT WAS OPERATIONAL TESTED WITH THE GPS UNIT REMOVED AND ALL OPERATED NORMALLY. THE GPS WAS PLACED ON MEL AND THE AIRCRAFT WAS RELEASED FOR SERVICE. (K)

Source: SDR 2007FA0000856 · FAA SDRS
O · 1998-12-07 Unresolved
ATA 8530

PILOT REPORTED RT ENGINE RUNS ROUGH. FOUND NO COMPRESSION NR 6 CYLINDER. FOUND METAL IN MAIN OIL SCREEN. FOUND NR 6 ROD BOLT BROKEN AND CONNECTING ROD BROKEN LOOSE FROM CRANKSHAFT. MAJOR DAMAGE TO CRANKCASE, CRANKSHAFT, ROD, AND CYLINDERS. SUBMITTER SUSPECTED IMPROPER HEAT TREATMENT OF ROD BOLT. BOLT TO BE SENT TO THE MANUFACTURER FOR FURTHER TESTING.

Source: SDR 99ZZZX376 · FAA SDRS