N255CA

COSTRUZIONI AERONAUTICHE TECNA P2012 TRAVELLER · 2019 · Valid Registration

Registered owner: HYANNIS AIR SERVICE INC, MA (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
HYANNIS AIR SERVICE INC. (HYIA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2026-04-16 Matched by certificate designator
ATA 7810

DURING SCHEDULED INSPECTION MAINTENANCE FOUND THE LEFT ENGINE TURBO TRANSITION PIPE CRACKED. THE TRANSITION PIPE WAS REPLACED WITH NO FURTHER DEFECTS NOTED.

Source: SDR HYIA20260508005 · FAA SDRS
R J · 2026-04-06 Matched by certificate designator
ATA 8530

PILOT REPORTED EXCESSIVE ENGINE VIBRATION DURING TAKE OFF AND CRUISE. MAINTENANCE INSPECTED AND FOUND THE #6 CYLINDER DEAD, THE CYLINDER WAS REPLACED ALONG WITH CYLINDER #5'S SPARK PLUGS WITH NO FURTHER DEFECTS NOTED.

Source: SDR HYIA20260410002 · FAA SDRS
M · 2024-02-24 Matched by certificate designator
ATA 3030

PILOT REPORTED STALL HEAT INOPERATIVE. MAINTENANCE INSPECTED AND FOUND THE LIFT TRANSDUCER HEATING ELEMENT SWITCH AND CONNECTOR MELTED. THE CONTROL PANEL WAS REPLACED WITH NO FURTHER DEFECTS.

Source: SDR HYIA202405174004 · FAA SDRS
B · 2023-04-28 Matched by certificate designator
ATA 2140

PILOT REPORTED SMOKE SMELL IN THE COCKPIT ASSOCIATED WITH THE HEATER. MAINTENANCE INVESTIGATED AND CONFIRMED FAULT TO BE HEATER RELATED AND PLACED SYSTEM ON MEL.

Source: SDR HYIA20230501002 · FAA SDRS
O · 2023-02-22 Matched by certificate designator
ATA 5342

DURING SCHEDULED INSPECTION, EXCESSIVE RADIAL END PLAY WAS NOTED IN THE AFT ATTACH BEARINGS (HINGE ASSY.) FOR THE HORIZONTAL STABILIZER PN: 212-55-10-1006-000. THESE ATTACH BEARING ASSEMBLIES WILL BE REMOVED AND REPLACED USING NEW PARTS.

Source: SDR HYIA20230321003 · FAA SDRS
O · 2020-05-28 Matched by certificate designator
ATA 5320

THE NLG ATTACH STRUCTURE WAS FOUND TO BE DAMAGED DURING AN INSPECTION INITIATED DUE TO SIMILAR FINDINGS ON OTHER COMPANY AIRCRAFT. THE DAMAGE IS LOCATED AT FWD MOST FUSELAGE BULKHEAD, LWR CENTER SECTION, IN THE AREA CORRESPONDING TO THE NLG MOUNTS. THE STRUCTURE AFT OF NLG BULKHEAD WAS INSPECTED WITH THE FOLLOWING DEFECTS NOTED: THE FWD SECTIONS OF FLOORBOARD SUPPORTS AS THEY ARE RIVETED TO FORWARD-MOST FUSELAGE BULKHEAD ARE CRACKED. THE OEM HAS BEEN NOTIFIED AND A FLEETWIDE INSPECTION HAS BEEN ISSUED FOR ALL COMPANY AIRCRAFT.

Source: SDR HYIA20200528002 · FAA SDRS
O · 1999-04-03 Matched by certificate designator
ATA 3230

LANDING GEAR SELECTOR LOCK DID NOT RELEASE AFTER TAKEOFF. SECURED LOOSE AIR/GROUND SENSOR WIRING CONNECTION (PO316).

Source: SDR COMA9910054 · FAA SDRS
K · 1999-03-29 Matched by certificate designator
ATA 3231

HYDRAULIC LEAK, RIGHT HAND WHEEL WELL. REPLACED O RING AT DOOR SEQUENCE VALVE.

Source: SDR COMA9910049 · FAA SDRS
J · 1999-01-16 Matched by certificate designator
ATA 5246

DOOR WARNING DURING TAKEOFF. FOUND FUEL SERVICE DOOR OPEN, CLOSED AND LATCHED DOOR.

Source: SDR COMA9910013 · FAA SDRS
W · 1998-11-01 Matched by certificate designator
ATA 5246

DOOR WARNING DURING TAKEOFF. SINGLE POINT FUEL SERVICE DOOR NOT LATCHED. SECURED DOOR.

Source: SDR COMA9810247 · FAA SDRS
O · 1998-06-24 Matched by certificate designator
ATA 5320

DURING AIRCRAFT MAINTENANCE, CORROSION WAS FOUND ON THE FUSELAGE FORWARD CABIN FLOOR SUPPORT STRUCTURE CENTER BUTT STRAP. THE BUTT-STRAP WAS REPLACED PER SRM STANDARD PRACTICES.

Source: SDR COMA9810141 · FAA SDRS
O · 1998-06-24 Matched by certificate designator
ATA 5320

DURING AIRCRAFT MAINTENANCE, CORROSION WAS FOUND ON THE FUSELAGE FORWARD CABIN FLOOR SUPPORT STRUCTURE LEFT HAND T-SECTION AT FRAME 16. THE T-SECTION WAS REPLACED PER SRM STANDARD PRACTICES.

Source: SDR COMA9810142 · FAA SDRS
O · 1998-06-24 Matched by certificate designator
ATA 5320

DURING AIRCRAFT MAINTENANCE, CORROSION WAS FOUND ON THE FUSELAGE FORWARD CABIN FLOOR SUPPORT STRUCTURE CENTER OMEGA BEAM. THE OMEGA BEAM WAS REPAIRED PER AERODESIGN REPORT NR 1957-5, REV IR, 6-23-98.

Source: SDR COMA9810145 · FAA SDRS
O · 1998-06-24 Matched by certificate designator
ATA 5320

DURING AIRCRAFT MAINTENANCE, CORROSION WAS FOUND ON THE FUSELAGE FORWARD CABIN FLOOR SUPPORT STRUCTURE RIGHT HAND T-SECTION AT FRAME 16. THE T-SECTION WAS REPLACED PER SRM STANDARD PRACTICES.

Source: SDR COMA9810143 · FAA SDRS
O · 1998-06-24 Matched by certificate designator
ATA 5320

DURING AIRCRAFT MAINTENANCE, CORROSION WAS FOUND ON THE FUSELAGE FORWARD CABIN FLOOR SUPPORT STRUCTURE CENTER BUTT STRAP. THE BUTT STRAP WAS REPLACED PER AERODESIGN REPORT NR 1671-1, REV A, 1-28-97.

Source: SDR COMA9810144 · FAA SDRS
J · 1998-05-19 Matched by certificate designator
ATA 2750

FLAP AND ADVANCED SWS INDICATIONS ON MAP. REPLACED THE FLAP CONTROL UNIT.

Source: SDR COMA9810124 · FAA SDRS
K J · 1998-05-14 Matched by certificate designator
ATA 7921

LOW OIL PRESSURE WARNING ON RIGHT HAND ENGINE INFLIGHT SHUTDOWN. REPLACED OIL COOLER HOSE ASSEMBLY THAT WAS LEAKING DUE TO CHAFING DAMAGE.

Source: SDR COMA9810122 · FAA SDRS
N · 1998-03-30 Matched by certificate designator
ATA 3260

THE LT MLG INTRANSIT LIGHTS REMAINED ON AFTER GEAR RETRACTION. LANDING GEAR WAS CYCLED AND 2ND RETRACTION WAS NORMAL. COULD NOT DUPLICATE DISCREPANCY. CLEANED INDICATION SENSORS AND CONNECTIONS. AIRCRAFT RETURNED TO SERVICE.

Source: SDR COMA9810083 · FAA SDRS
O · 1998-03-02 Matched by certificate designator
ATA 6113

DURING PREFLIGHT INSPECTION, THE RIGHT PROPELLER SPINNER BULKHEAD WAS FOUND TO BE CRACKED APPROXIMATELY 1.5 INCH ALONG THE BULKHEAD OUTER WALL BEHIND BLADE NR 2. AIRCRAFT WAS FERRIED BACK TO CVG HANGAR AND BULKHEAD REMOVED FOR REPAIR. DAMAGE APPEARS TO BE DUE TO MATERIAL DEFECT, NO EXTERNAL DAMAGE WAS FOUND.

Source: SDR COMA9810049 · FAA SDRS
J · 1997-12-15 Matched by certificate designator
ATA 3230

LANDING GEAR DID NOT EXTEND WHEN SELECTED DOWN. EMERGENCY SYSTEM USED TO LOWER LANDING GEAR. REPLACED DEFECTIVE RT MLG DOWNLOCK PROXIMITY SENSOR.

Source: SDR COMA9710498 · FAA SDRS
O · 1997-09-19 Matched by certificate designator
ATA 3242

DURING TEARDOWN OF BRAKE ASSY P/N 2-1585, THE ACCESSORY SHOP FOUND THE NUMBER ONE STATOR CRACKED. OVERHAULED BRAKE.

Source: SDR COMA9710415 · FAA SDRS
O · 1997-08-12 Matched by certificate designator
ATA 5320

DURING 4C INSEPCTION TASK 5320-151-01I, REVEALED RIGHT T-SECTION AT FRAME 28 TO BE CORRODED. REMOVED CORRODED T-SECTION AND INSTALLED SERVICEABLE PART USING EMB SRM STANDARD PRACTICES CHAPTER 51.

Source: SDR COMA9710372 · FAA SDRS
O · 1997-08-12 Matched by certificate designator
ATA 5315

DURING 4C INSPECTION TASK 5320-151-01I, REVEALED RIGHT FLOORBEAM AT FRAME 33 TO BE HEAVILY CORRODED. REMOVED CORRODED PART AND INSTALLED SERVICEABLE PART USING EMB SRM STANDARD PRACTICES CHAPTER 51 FOR LIKE TO LIKE PART REPLACEMENT.

Source: SDR COMA9710370 · FAA SDRS
O · 1997-08-12 Matched by certificate designator
ATA 5320

DURING 4C INSPECTION TASK 5330-161-01I, REVEALED RIGHT CARGO COMPARTMENT SILL TO BE CORRODED BEYOND LIMITS. REMOVED SILL AND INSTALLED SERVICEABLE SILL USING EMB SRM STANDARD PRACTICES CHAPTER 51.

Source: SDR COMA9710371 · FAA SDRS
O · 1997-08-12 Matched by certificate designator
ATA 5320

DURING 4C INSPECTION TASK 5320-151-01I, REVEALED AFT EMERGENCY EXIT GUIDE PIN FITTINGS TO HAVE CORROSION BETWEEN FITTINGS AND THE EXIT SILL LOWER ATTACHE ANGLE. FURTHER INVESTIGATION REVEALED THAT THERE IS NO PRIMER OR SEALANT BETWEEN OR ON THESE PIECES. REPLACED CORRODED ANGLE WITH SERVICEABLE PART IAW EMB SRM CHAPTER 51.

Source: SDR COMA9710369 · FAA SDRS
O · 1997-08-12 Matched by certificate designator
ATA 5320

DURING 4C INSPECTION TASK 5320-151-01I, REVEALED AFT EMERGENCY EXIT GUIDE PIN FITTINGS TO HAVE CORROSION BETWEEN THE FITTINGS AND THE EXIT SILL LOWER ATTACH ANGLE. FURTHER INVESTIGATION REVEALED THAT THERE IS NO PRIMER OR SEALANT BETWEEN OR ON THESE PIECES. REPLACED CORRODED FITTINGS WITH SERVICEABLE PARTS. INSTALLED PARTS WITH PRIMER AND SEALANT USING EMB STANDARD SRM PRACTICES CHAPTER 51.

Source: SDR COMA9710368 · FAA SDRS
O · 1997-07-17 Matched by certificate designator
ATA 3520

ON C-CHECK TASK 35-09, THE PASSENGER OXYGEN MASKS AT SEAT 1BC FAILED TO DEPLOY. THE OXYGEN MASK DOOR SOLENOID AT THAT LOCATION WAS REPLACED, SYSTEM TESTS NORMAL.

Source: SDR COMA9710332 · FAA SDRS
O · 1997-03-17 Matched by certificate designator
ATA 3230

LANDING GEAR WOULD NOT RETRACT. REPLACED DEFECTIVE WIRING CONNECTOR AT RT MLG UPLOCK.

Source: SDR COMA9710181 · FAA SDRS
O · 1997-02-03 Matched by certificate designator
ATA 6120

PROPELLER ASSEMBLY REMOVED FROM AIRCRAFT DUE TO BEING STRUCK BY LAVORATORY CART WHILE STATIC ON AIRCRAFT RAMP. DURING PROPELLER IMPACT INSPECTION ACTUATOR FEATHER STOP TAB WAS FOUND TO BE DISPLACED APPROXIMATELY .125 FEET. ACTUATOR S/N 20383 WAS SUBSEQUENTLY REMOVED FROM THE PROPELLER ASSEMBLY AND THE PITCHLOCK SCREW S/N 49 WAS REMOVED FROM ACTUATOR AND RETURNED TO MANUFACTURER.

Source: SDR COMA9710099 · FAA SDRS
J · 1997-01-25 Matched by certificate designator
ATA 5754

OUTBOARD FLAPS FAILED TO RETRACT. REPLACED THE ROLLERS ON THE RT OUTBOARD FLAP.

Source: SDR COMA9710088 · FAA SDRS
J · 1997-01-20 Matched by certificate designator
ATA 5753

FLAP DISAGREEMENT AFTER TAKEOFF. CLEANED LEFT OUTBOARD FLAP TRACKS.

Source: SDR COMA9710047 · FAA SDRS
J · 1997-01-16 Matched by certificate designator
ATA 5753

FLAP FAIL WARNING. REPLACED LEFT OUTBOARD FLAP, OPERATIONAL CHECK GOOD.

Source: SDR COMA9710039 · FAA SDRS
J · 1997-01-13 Matched by certificate designator
ATA 5753

FLAP DISAGREEMENT UPON FLAP RETRACTION AFTER TAKEOFF. REPLACED LT OUTBOARD FLAP ROLLERS 4 EACH. OPERATIONAL CHECK GOOD.

Source: SDR COMA9710030 · FAA SDRS
J · 1997-01-12 Matched by certificate designator
ATA 5246

DOOR LIGHT ON MAP CAME ON DURING TAKEOFF. RESECURED FUEL DOOR FASTENERS.

Source: SDR COMA9710025 · FAA SDRS
O · 1996-08-19 Matched by certificate designator
ATA 5413

INSPECTION REVEALED A CRACK IN THE RIGHT NACELLE LT STRINGER 1. THE STRINGER WAS REPAIRED PER AERODESIGN REPORT NR 2000-1, DATED 8-17-96.

Source: SDR COMA9610256 · FAA SDRS
O · 1996-08-19 Matched by certificate designator
ATA 5320

INSPECTION REVEALED CORROSION ON THE FORWARD CABIN FLOOR SUPPORT OM26A BEAM BUTT STRAP ON THE LEFT SIDE GALLEY AREA. THE BUTT STRAP WAS REPLACED WITH A NEW PART PER EMB120 5RM STANDARD PRACTICES.

Source: SDR COMA9610250 · FAA SDRS
J · 1996-08-03 Matched by certificate designator
ATA 2910

RT HYDRAULIC RESERVOIR LOW PRESSURE WARNING ILLUMINATED. DRAINED MOISTURE FROM RESERVOIR, SYSTEM CHECK NORMAL.

Source: SDR COMA9610240 · FAA SDRS
N · 1996-06-08 Matched by certificate designator
ATA 3620

RT BLEED AIR DUCT OVERHEAT WARNING CAME ON DURING FLIGHT. REPLACED DEFECTIVE DUCT OVERHEAT SWITCH.

Source: SDR COMA9610171 · FAA SDRS
O · 1996-05-15 Matched by certificate designator
ATA 6120

AUTO FEATHER SYSTEM WILL NOT TEST OR ARM. REPLACED THE RT ENGINE SIGNAL CONDITIONER UNIT.

Source: SDR COMA9610144 · FAA SDRS
N · 1996-02-07 Matched by certificate designator
ATA 3150

TAKEOFF TRIM AURAL WARNING SOUNDED DURING TAKEOFF. TRIM WAS CONFIRMED IN THE GREEN BAND. REPLACED THE LT ELEVATOR TRIM PROXIMITY SENSOR.

Source: SDR COMA9610070 · FAA SDRS
K · 1996-02-06 Matched by certificate designator
ATA 7310

RT ENGINE IS LEAKING FUEL. REPLACED THE MOTIVE FLOW FUEL RETURN HOSE AND FITTING AT THE ENGINE HMU, DUE TO DAMAGED THREADS.

Source: SDR COMA9610072 · FAA SDRS
N · 1996-01-28 Matched by certificate designator
ATA 3150

TAKEOFF AURAL WARNING SOUNDED DURING TAKEOFF ROLL. REPLACED THE AURAL WARNING UNIT.

Source: SDR COMA9610045 · FAA SDRS
O · 1996-01-25 Matched by certificate designator
ATA 2913

RT ELECTRIC HYDRAULIC PUMP IS INOP. REPLACED THE RT ELECTRIC MOTOR DRIVEN HYDRAULIC PUMP.

Source: SDR COMA9610040 · FAA SDRS
O · 1996-01-09 Matched by certificate designator
ATA 3413

PILOTS VSI TUBE BLANK. REPLACED THE 1VA-81A TA/VS1.

Source: SDR COMA9610006 · FAA SDRS
J · 1995-12-23 Matched by certificate designator
ATA 2750

FLAP DISAGREEMENT WARNING DURING TAKEOFF CLIMB. REPLACED THE OUTBD FLAP SECTION ROLLERS.

Source: SDR COMA9512040 · FAA SDRS
B · 1995-08-13 Matched by certificate designator
ATA 2400

STRONG SMELL OF ELECTRICAL BURNING IN COCKPIT AREA. FOUND BURNED GALLEY POWER WIRE. SECURED POWER TO GALLEY BY PULLING BREAKERS AND PLACED ON DEFERRED MAINT LIST.

Source: SDR COM11952 · FAA SDRS
N · 1995-05-26 Matched by certificate designator
ATA 3418

DURING TAKEOFF ROLL, THE STALL WARNING CAME ON. REPLACED STALL WARNING COMPUTER.

Source: SDR COM11905 · FAA SDRS
O · 1995-04-24 Matched by certificate designator
ATA 7603

CREW REPORTED, THAT POWER LEVERS WERE NOT EVEN AT FLIGHT IDLE STOP. THE RT POWER LEVER FLIGHT IDLE STOP PIN AND ROLLER WERE FOUND TO BE WORN OVER 50 PERCENT. THE RT POWER LEVER ASSY WAS REPLACED.

Source: SDR COM11878 · FAA SDRS
O · 1995-03-31 Matched by certificate designator
ATA 2731

ELEVATOR TRIM IS BINDING. REPLACED THE RT ELEVATOR TRIM ACTUATOR.

Source: SDR COM11845 · FAA SDRS
O · 1995-02-23 Matched by certificate designator
ATA 5530

DURING INSPECTION TASK 5530-324-03I AND 5530-324-02I, VERTICAL STABILIZER TO FUSELAGE ANGLE WAS FOUND TO BE CRACKED. REPLACED ANGLE IAW AERODESIGN REPORT 1446-1 AND EMB SRM.

Source: SDR COM11798 · FAA SDRS
K · 1995-02-12 Matched by certificate designator
ATA 3230

HYDRAULIC LEAK, LEFT MLG. TIGHTENED FITTINGS ON HYDRAULIC SWIVEL.

Source: SDR COM11783 · FAA SDRS
K J · 1995-02-12 Matched by certificate designator
ATA 3240

HYDRAULIC LEAK, LEFT MLG. REPLACED LEAKING BRAKE LINE SWIVEL.

Source: SDR COM11777 · FAA SDRS
N · 1995-01-23 Matched by certificate designator
ATA 3260

LT MLG GREEN SAFE LIGHT IS INOP, AND RED INTRANSIT LIGHT IS ILLUMINATED. REPLACED THE DOWN LOCK PROXIMITY SENSOR.

Source: SDR COM11738 · FAA SDRS