N259JX

EMBRAER EMB-135LR · 2001 · Valid Registration

Registered owner: DELUX PUBLIC CHARTER LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
DELUX PUBLIC CHARTER LLC (4DPA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2024-11-05 Matched by certificate designator
ATA 3230

CREW REPORTED- LOWERED LANDING GEAR FOR CCR. GOT EICAS MESSAGE “LG AIR/GND FAIL”. ULTIMATELY, WRH HAS LANDING DISTANCE MULTIPLIED BY 1.7. CCR RUNWAYS TOO SHORT. DIVERTED TO OAK. CORR ACTION- PERFORM TEST AND CLEAN ALL CANNON PLUG. OPS CHECK OK THIS CLEARS THE SNAG.

Source: SDR 4DPA2024110500001 · FAA SDRS
J · 2022-07-01 Matched by certificate designator
ATA 2120

CREW REPORTED-WHILE IN ROUTE PACK TWO VALVE CLOSED. FLIGHT ATTENDANT SAID SHE HEARD THE HOSE BLOW OFF. THEY WERE CLIMBING THROUGH 23,000 FEET AND LEVELED OUT AT 25,000 FOR SINGLE PACK ALTITUDE. A COUPLE MINUTES LATER THE CABIN ALTITUDE STARTED TO CLIMB AGGRESSIVELY. CREW DECIDED TO RETURN TO OAK. CORRECTIVE ACTION- REMOVED AND REPLACED BLOWN DUCT IN PAC 1 AND REMOVED AND REPLACE DAMAGED AND LEAKING DUCT IN PAC 2. OPS AND PRESSURE CHECK GOOD.

Source: SDR 4DPA2022070100001 · FAA SDRS
O · 2022-06-06 Matched by certificate designator
ATA 3610

ISSUE-CREW REPORTED WITH PACK 2 ON MEL, PACK 1 OUTPUT INADEQUATE TO PRESSURIZE AIRCRAFT AND RETURNED TO KBUR. MX CORR ACTION-MX REPORTED NO FLOW OF AIR COMING FROM HEAT EXCHANGER EXHAUST, LH SIDE. PERFORMED THE INSPECTION/CHECK OF THE LH PACK DUCTS AND FOUND DUCT TO HEAT EXCHANGER HAD BLOWN OFF. RESCURED THE DUCT OPERATIONAL & LEAK CHECK GOOD.

Source: SDR 4DPA2022060600001 · FAA SDRS
J · 2021-08-18 Matched by certificate designator
ATA 2120

ISSUE: PACK 1-2 VALVE CLOSED MESSAGE AND PACK 2 WAS ALREADY DEFERRED RESULTED IN PRESSURIZATION ISSUES. CREW RETURNED TO BURBANK. CORR ACTION PACK1 DISCOVERED BLOWN OFF DUCT AND SLEEVE REINSTALLED OPS/LK CHECK GOOD. PACK2 DISCOVERED BLOWN OFF DUCT AND SLEEVE REINSTALLED OPS/LK CHECK GOOD. (HAS FLOWN 7 LEGS SINCE NO ISSUES)

Source: SDR 4DPA2021082080002 · FAA SDRS
J · 2021-07-09 Matched by certificate designator
ATA 7500

RTF DUE TO BLD 1 LK(PACK 2 WAS ALREADY ON MEL) DISC: BLD 1 LEAK MESSAGE CORR ACTION: FOUND O-RING IN JOINTS 9, 15,17,19 BROKEN REMOVED AND REPLACED O-RINGS COMPLETED BLEED LEAK OPS CHECK GOOD

Source: SDR 4DPA2021071300001 · FAA SDRS
O · 2021-05-04 Matched by certificate designator
ATA 2520

HAD 1 EACH SINGLE SEAT PN 41042002-109 SN 03893 AND 1 EACH SINGLE SEAT PN 41042002-111 SN 03569 CRACKED ON THEIR AISLE SEAT FRAMES UNDER THE AISLE ARMREST.

Source: SDR 4DPA2021050400003 · FAA SDRS
J · 2021-02-15 Matched by certificate designator
ATA 2421

RECEIVED A GEN NR 4 BRG FAIL EICAS MESSAGE DURING BUR-EUG REPO LEG. REMOVED AND REPLACED NR 4 GENERATOR OPS TEST GOOD.

Source: SDR 4DPA202102150001 · FAA SDRS