N263JX

EMBRAER EMB-135LR · 2001 · Valid Registration

Registered owner: DELUX PUBLIC CHARTER LLC, TX (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
DELUX PUBLIC CHARTER LLC (4DPA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2024-10-24 Matched by certificate designator
ATA 3222

CREW REPORTED- ON DEPARTURE LG AIR/GRND FAIL. LND GEAR LOCKED DOWN, RAN QRH WITH NO RESOLUTION. AIR RETURNED. WHEN PARKED FRONT NOSE STRUT FULLY COMPRESSED. CORR ACTION MX DETERMINED THAT THE NLG STRUT HAD BEEN INCORRECTLY SERVICED WITH EITHER HYDRAULIC FLUID OR NITROGEN. SERVICED NLG STRUT WITH BOTH HYDRAULIC FLUID AND NIGROGEN. NO ABNORMALITIES FOUND DURING SERVICING. OPS CHECK GOOD. CYCLED THE GEAR UP AND DOWN 3 TIMES WITHOUT ANY ISSUES. JACKED AND DOWNJACKED AIRCRAFT AND OBSERVED SMOOTH MOVEMENT OF STRUT.

Source: SDR 4DPA2024102400001 · FAA SDRS
J · 2023-09-04 Matched by certificate designator
ATA 3200

ISSUE-CREW REPORTED LG AIR/ GND FAIL PRESENTED IMMEDIATELY AFTER TAKEOFF. RAN QRH 12-6 AND NAP 22. RETUNED TO LAS. CORR ACTION MX FOUND NLG PROXIMITY SWITCH CANNON PLUG DISCONNECTED. RECONNECTED CANNON PLUG OPS TEST GOOD.

Source: SDR 4DPA2023090400001 · FAA SDRS
J · 2023-07-21 Matched by certificate designator
ATA 3220

ISSUE; PILOT REPORTED AFTER TAKEOFF, GEAR RETRACTION NORMAL. ACCELERATING THRU ABOUT 230 IT’S, 6000 FEET, NOSE GEAR DOOR OPENED. SLOWED TO 200, LOWERED GEAR, ALL NORMAL. RETRACTING GEAR, GEAR RETRACTED BUT NOSE DOOR REMAINED OPEN. HYDRAULICS NORMAL. CORR ACTION; MX RR NOSE LANDING GEAR SOLENOID VALVE . OPS CHECK GOOD. NO FURTHER DEFECTS NOTED AT THIS TIME. OPS AND LEAK CHECK GOOD. RETRACTED AND EXTENDED GEARS 10 TIMES.

Source: SDR 4DPA2023072100001 · FAA SDRS
J · 2023-01-26 Matched by certificate designator
ATA 3200

CREW REPORTED-LG AIR/GND FAIL MESSAGE DISPLAYED UPON LANDING GEAR SELECTED UP. FLAP AND TRIM ANNUNCIATION AT FULL POWER. AIR RETURN LANDING BACK IN PHX. CORR ACTION- MX R&R'D LGEU AND RAN PROX SWITCH TEST ALL OPS TESTS GOOD.

Source: SDR 4DPA2023012600001 · FAA SDRS
N · 2021-08-18 Matched by certificate designator
ATA 2197

ISSUE: PACK 1 OVERHEAT AND PACK 2 FAIL MESSAGES ON CLIMB OUT CREW DECLARED AN EMERGENCY AND RETURNED. PACK 1 OVERHEAT RAN FIM CLEANED AND CHECKED CONTINUITY AT P0944 & P0454 NO DEFECTS. PACK 2 FAIL CLEANED AND RESEATED PACK VALVE CONNECTOR COULDN'T DUPLICATE PACK 2 FAIL OPS TESTED GOOD.

Source: SDR 4DPA2021082018001 · FAA SDRS
J · 2021-06-17 Matched by certificate designator
ATA 2130

ISSUE: DEPARTING LAS VEGAS PILOT NOTICED AT 8000’ THAT THE PLANE WASN’T AUTO PRESSURING. CREW RECYCLED THE PACKS TWICE AND IT DID NOT FIX THE ISSUE. CREW RAN THE QRH AND STARTED TO MANUALLY PRESSURIZE THE AIRPLANE. EVERYTHING WORKED NORMALLY UNTIL THEY GOT TO 29000’ AND THE CABIN ALTITUDE SHOT UP FROM 8000’ TO 11800’ IN ABOUT 30 SECONDS. THE DELTA P STAYED AT APPROXIMATELY 5.2. PILOT TURNED THE MANUAL PRESSURE DIAL TO THE 2 O’CLOCK POSITION AND HE STILL COULDN’T CLIMB THE CABIN. HE ASKED FOR LOWER ALT AND TIME TO TROUBLESHOOT THE PROBLEM BUT ATC TURNED THEM BACK TO VEGAS. CORR ACTION: INSTALLED SERVICABLE CABIN PRESSURE ACQUISITION MODULE FROM N246JX IN REF TO EMB-135 AMM 21-32-01 ND AP4134059 ACCOMPLISHED OPS CHECK OF CPAM IAW EMB 135 AMM 21-32-01. ALL CHECKS GOOD.

Source: SDR 4DPA2021061700001 · FAA SDRS
O · 2019-08-07 Matched by certificate designator
ATA 5610

FIRST OFFICER'S WINDSHIELD CRACKED AT FL290. AIRCRAFT DIVERTED.

Source: SDR 4DPA201908080239 · FAA SDRS