N263MC

DORNIER DORNIER 228-202 · 1987 · Valid Registration

Registered owner: BIGHORN AIRWAYS INC, WY (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
BIGHORN AIRWAYS, INC. (BIGA)Certificate holderMatched by certificate designator

Accident & incident history

Incident · 1989-07-09 Matched by aircraft (N-number)
Dornier DO-228 None injuryBIGHORN AIRWAYS, INC.
Source: NTSB case CHI89IA144

Maintenance disclosures

N · 2016-02-19 Matched by certificate designator
ATA 2612

AFTER CONFIRMING A BLEED AIR SEAL COUPLING LEAK ON SDR BIGA20160114-001, THE ACFT FIRE DETECTION SYS WAS GND TESTED NORMAL. A TEST FLIGHT WAS REQUESTED, DURING THE FLIGHT THE LT FIRE DETECTION FLICKERED. AGAIN THE SYS WAS TESTED ON THE GND & COULD NOT BE DUPLICATED, THE ENG FIRE LOOPS WERE SWAPPED FROM THE LT ENG TO THE RT ENG & ALL CONNECTIONS WERE INSPECTED, CLEANED & REASSEMBLED. GND CHECKS WERE NORMAL, TWO TEST FLIGHT WERE PERFORMED & THE PROBLEM COULD NOT BE DUPLICATED. THE SUSPECTED HARNESS MAY HAVE HAD A CONNECTION PROBLEM THAT WAS NOT IDENTIFIED, THAT WAS CORRECTED DURING THE FIRE LOOP REMOVAL & INSTALLATION.

Source: SDR BIGA20160219001 · FAA SDRS
J · 2016-01-11 Matched by certificate designator
ATA 3610

PILOT WAS PERFORMING A NIGHT CURRENCY FLIGHT, AS HE BEGAN HIS FINAL APPROACH THE LT ENG FIRE WARNING CAME ON. THE PILOT PULLED BACK POWER & THE FIRE LIGHT WENT OUT BELOW 40% TORQUE. PUSHING THE POWER UP CAUSED THE LIGHT TO COME BACK ON. THE PILOT LANDED WITHOUT INCIDENT. INSPECTED THE ACFT, NO HEAT DAMAGE, OR FIRE COULD BE FOUND & THE SYS GND TESTED NORMAL. THE ACFT WAS GND RUN & THE PROBLEM COULD NOT BE DUPLICATED. FOUND ONE BLEED AIR DUCT COUPLING & CONNECTOR SEEMED LOOSE GOING FROM THE ENG COMPARTMENT INTO THE AIRFRAME. THE SYS WAS PRESS CHECKED & FOUND EXCESSIVE LEAKAGE. THIS BLEED AIR LEAKAGE WAS INLINE WITH THE FIRE DETECTION WIRE LOOP. THE COUPLING SEALS WERE REMOVED & FOUND TO BE WORN & HARD. THE SEALS IN THE COUPLER & CONNECTOR WERE REPLACED & THE ACFT WAS GND RUN & TESTED NORMAL.

Source: SDR BIGA20160114001 · FAA SDRS
J · 2014-07-09 Matched by certificate designator
ATA 2497

THE LEFT GENERATOR SYSTEM KICKED OFF LINE. AFTER TROUBLESHOOTING THE SYSTEM THE 20 GAUGE "D" WIRE WAS FOUND TO BE BROKEN INSIDE THE SHEATH IN THE ENGINE COMPARTMENT AND WAS ONLY DETECTABLE BY OHM CHECKING THE HARNESS. DURING THE OHM READING CHECKS OF THE GENERATOR SYSTEM A SECONDARY PROBLEM WAS FOUND WITH HIGH RESISTANCE ON THREE WIRES AT THE LEFT GCU CANNON PLUG. THEY WERE BREAKING AWAY AT THE AT THE PINS DOWN IN THE PLUG PAST THE STRAIN RELIEF. THESE WERE ALL REPAIRED. VIBRATION AND THE FREQUENT REMOVAL OF THE GCUS AND STARTER GENERATORS FOR REPLACEMENT, TROUBLESHOOTING, AND INSPECTION MAY BE LEADING TO THE WIRING TO BREAKDOWN.

Source: SDR BIGA20140711001 · FAA SDRS
O · 2002-07-11 Matched by certificate designator
ATA 5511

CRACKS FOUND ON RIB NR 12 ON RIGHT SIDE AND RIB NR 13 ON LEFT SIDE. LT RIB CRACKED THROUGH 4 RIVETS HOLES ON TOP SKIN, LENGTH OF CRACK WAS 5 INCHES. RT RIB CRACKED THROUGH 1 RIVET HOLE, LENGTH OF CRACK WAS 2 INCHES. CRACKS WERE FOUND DURING COMPLIANCE WITH AD 2001-21-01 AND DORNIER SB228-234.

Source: SDR 2002F00759 · FAA SDRS