N270PR

CESSNA 560XL · 2004 · Valid Registration

Registered owner: COBBLESTONE AVIATION LLC, WI (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
CD PILOT AND AIRCRAFT MANAGEMENT SD, LLC (64MA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2014-10-30 Matched by certificate designator
ATA 7600

DURING THE TAKEOFF ROLL THE NR 1 ENG COMPUTER, LEEC, WENT INTO MANUAL MODE REQUIRING THE CREW TO ABORT THE TAKEOFF. THE DISCREPANCY WITH THE LEEC WAS DEFERRED. TROUBLESHOOTING AFTER THE ACFT RETURNED TO HOME BASE IDENTIFIED THE NR 1 ENG TORQUE MOTOR PN 30J3490-01 SN TR4775 AS DEFECTIVE & WAS REMOVED & A NEW UNIT INSTALLED. FUNCTIONAL CHECKS WERE SATISFACTORY. CLEARED MEL & RETURNED THE ACFT TO SERVICE.

Source: SDR 9JLA2015012906973 · FAA SDRS
N · 2014-07-29 Matched by certificate designator
ATA 5270

DURING PREFLIGHT OPERATIONS THE MAIN CABIN DOOR ANNUNCIATOR LIGHT WOULD NOT EXTINGUISH. THE SYS WAS TROUBLE SHOT & IT WAS FOUND THAT THE DOOR VENT SOLENOID HAD FAILED. THE SOLENOID PN 6711335-1 WAS REMOVED FROM SERVICE & A NEW UNIT WAS INSTALLED. OPERATION CHECKS SATISFACTORY.

Source: SDR 9JLA2014091006971 · FAA SDRS
N · 2014-06-24 Matched by certificate designator
ATA 5270

THE CREW REPORTED THE CABIN DOOR ANNUNCIATOR ILLUMINATED & WOULD NOT EXTINGUISH. TROUBLESHOOTING FOUND THE PAX DOOR LOWER AFT PIN SWITCH PN A4-18EM4111 DEFECTIVE. THE SWITCH WAS REPLACED WITH NEW, FUNCTIONAL CHECKS SATISFACTORY.

Source: SDR 9JLA2014072106970 · FAA SDRS
P · 2014-01-08 Matched by certificate designator
ATA 3020

THE FLIGHT CREW REPORTED THE RT ENG ANTI-ICE LIGHT TEST WAS OK WITH THE ROTARY SWITCH BUT WHEN THE SYS WAS ACTIVATED WITH ANTI-ICE SWITCH THE RT SIDE DOES NOT COME ON IN FLIGHT EVEN AFTER A 1 HOUR CRUISE. TROUBLESHOOTING FOUND THE RT TEMP SWITCH DEFECTIVE. NEW SWITCH INSTALLED IAW AMM 30-21-00.

Source: SDR 9JLA201401240659 · FAA SDRS
J · 2013-07-08 Matched by certificate designator
ATA 5210

CREW REPORTED THAT DURING THE PREFLIGHT CHECKS THE CABIN VENT DOOR WAS FOUND TO BE INOPERATIVE. CABIN VENT DOOR NOT CLOSING AUTOMATICALLY. THE SYS WAS TROUBLE SHOT & THE VENT DOOR SOLENOID WAS FOUND TO BE DEFECTIVE. THE DEFECTIVE PART WAS R & R WITH A NEW SOLENOID PN 6711335-1. OPERATIONS CHECKED GOOD.

Source: SDR 9JLA2014041006954 · FAA SDRS