N2714M

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
HYANNIS AIR SERVICE INC. (HYIA)Certificate holderMatched by certificate designator

Accident & incident history

Accident · 1970-08-20 Unresolved
Piper PA-12 Fatal injuryoperator not yet resolved
Source: NTSB case LAX71AL008

Maintenance disclosures

A · 2017-10-23 Matched by certificate designator
ATA 3397

DURING APPROACH, THE CAPTAINS OVERHEAD LIGHT SWITCH WAS ACTUATED AND THE LIGHT DID NOT ILLUMINATED. THE CREW SUBSEQUENTLY ACTUATED THE COPILOT'S OVERHEAD LIGHT SWITCH WHICH ILLUMINATED AND WAS ACCOMPANIED BY AN ODOR OF SMOKE. THE CAPTAIN SHUTDOWN ALL ELECTRICAL SYSTEMS AND WAS ABLE TO SEE A SMALL FLAME IN THE OVERHEAD CONSOLE. AN EMERGENCY WAS DECLARED AND THE FLIGHT DIVERTED. THE FLAME SELF EXTINGUISHED PRIOR TO ARRIVAL. SUBSEQUENT INSPECTION REVEALED A RESISTOR WITHIN THE OVERHEAD DIMMER ASSEMBLY HAD FAILED AND CAUSED THE FLAME.

Source: SDR HYIA20171027001 · FAA SDRS
O · 2017-03-03 Matched by certificate designator
ATA 5415

DURING A ROUTINE INSPECTION, TWO CRACKS WERE FOUND IN THE RT OUTBOARD NACELLE FITTING. THERE WAS ONE CRACK IN THE INBOARD SIDE OF THE FITTING, JUST FORWARD OF THE SPAR STRAP. THE CRACK WAS .108 IN LENGTH. THE OTHER CRACK WAS DISCOVERED ON THE OUTBOARD SIDE OF THE FITTING, JUST FORWARD OF THE SPAR STRAP. THE CRACK WAS .060 IN LENGTH.

Source: SDR HYIA20170828006 · FAA SDRS
O · 2017-03-03 Matched by certificate designator
ATA 5415

DURING A ROUTINE INSPECTION, A CRACK WAS FOUND ON THE LT OUTBOARD NACELLE FITTING. THE CRACK WAS FOUND ON THE INBOARD SIDE OF THE FITTING, JUST FORWARD OF THE SPAR STRAP. THE CRACK WAS MEASURED AT .191 IN LENGTH.

Source: SDR HYIA20170828005 · FAA SDRS
O · 2016-09-29 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION; EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20161010165 · FAA SDRS
O · 2016-09-29 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION; EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20161010163 · FAA SDRS
O · 2016-09-29 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION; EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20161010164 · FAA SDRS
O · 2016-09-29 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION; EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20161010167 · FAA SDRS
O · 2016-09-29 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION; EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20161010166 · FAA SDRS
O · 2016-08-17 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION. EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20160818082 · FAA SDRS
O · 2016-08-17 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION. EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20160818080 · FAA SDRS
O · 2016-08-17 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION. EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20160818081 · FAA SDRS
O · 2016-07-20 Matched by certificate designator
ATA 8530

CYLINDER REMOVED DUE TO LOW COMPRESSION AT INSPECTION. EXHAUST VALVE DISPLAYS EVIDENCE OF HEAT DAMAGE.

Source: SDR HYIA20160803051 · FAA SDRS
O · 2015-01-07 Matched by certificate designator
ATA 5711

UPON DISASSEMBLY OF RT NACELLE LOWER FAIRING FOR INSPECTION OF RT WING SPAR STRAP IAW SID 57-10-16, UNINTENTIONAL DRILL DAMAGE AT WING SPAR STRAP WAS FOUND BY VISUAL INSPECTION. THE DAMAGE EXISTS JUST OTBD OF THE INBD NACELLE FITTING WITH FWD FACE OF RT WING SPAR STRAP 5292029-2. THE LOWER FWD WING SPAR CAP STRAP 5292029-2 WAS ORIGINALLY INSTALLED ON 04/08/2004 & HAS BEEN IN SERVICE FOR A TOTAL OF 12498.0 HOURS. THE DRILL DAMAGE LOCATED AT THIS DATE APPEARS TO HAVE BEEN INDUCED AT A PREVIOUS REPAIR OF NACELLE FIREWALL. THIS AREA OF WING SPAR STRAP IS NOT ACCESSIBLE FOR VISUAL INSPECTION WITHOUT DISASSEMBLY OF LOWER NACELLE FAIRING WHICH IS INSTALLED WITH MS RIVETS. DAMAGE MAPPING & REPORT REQUIRED BY MANUFACTURER HAS BEEN SUBMITTED. THIS DISCREPANCY WILL BE REPLACEMENT OF SPAR STRAP ASSEMBLY IAW CURRENT REVISION OF MANUFACTURER’S INSTRUCTIONS SK402-47B. A SUPPLEMENTAL FILE WILL BE SUBMITTED ALONG WITH THIS SDR ILLUSTRATING DAMAGE.

Source: SDR HYIA20150107001 · FAA SDRS
R · 2014-09-01 Matched by certificate designator
ATA 7331

ON INITIAL CLIMB, THE PILOT REPORTED FUEL FLOW OF 160PPH. AFTER REACHING CRUISING ALTITUDE THE FUEL FLOW WENT TO 0 & THE PILOT REPORTED TEMP POWER LOSS. THE PILOT WENT THROUGH THE ENG FAILURE CHECKLIST & PLACED THE AUXILIARY BOOST PUMP ON IN THE HIGH SETTING. THE FUEL FLOW WENT TO 170PPH, BUT THE PILOT REPORTED THERE WAS STILL A POWER LOSS. THE PILOT THEN PLACED THE AUXILIARY PUMP IN LOW & THE ENG REGAINED NORMAL POWER INDICATIONS & PERFORMANCE. THE PILOT RETURNED TO DEPARTURE AIRPORT. MAINTENANCE INSPECTED THE ACFT & REPLACED THE RT ENG FUEL FLOW TRANSDUCER IAW THE SIM & SET UP THE RT ENG FUEL FLOW IAW MM 73-20-01. THE ACFT WAS RUN WITH NO DEFECTS OR POWER REDUCTION NOTED. BASED ON THE PILOTS REPORT & MAINTENANCE FINDING THE POWER LOSS WAS LIKELY DUE TO THE AUXILIARY PUMP PLACED ON HIGH CAUSING TOO RICH MIXTURE.

Source: SDR HYIA20140905116 · FAA SDRS
O · 2012-09-11 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE, PN 5142002-5, WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE BEYOND LIMIT ALLOWABLE OF MEB91-11R1. THIS UNIT HAS BEEN SCRAPPED & A REPLACEMENT DRAG BRACE HAS BEEN INSTALLED IN ACFT.

Source: SDR HYIA20140414020 · FAA SDRS
O · 2012-05-16 Matched by certificate designator
ATA 5311

DURING A MX EVENT, DAMAGE WAS DISCOVERED ON THE FORWARD CARRY THROUGH SPAR ASSY. DAMAGE INCLUDES FWD LOWER SPAR WEB FLANGE CRACK AND CORRESPONDING VERTICAL STIFFENER CRACKED AT SAME LOCATION. UPON DISCOVERY OF DAMAGE ACFT WAS SUBMITTED TO MRO. MRO REQUESTED AND RECEIVED EO. REPAIRS ARE IN PROCESS.

Source: SDR HYIA201205170005 · FAA SDRS
O · 2011-12-08 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE, PN 5142002-5, WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE WITHIN ALLOWABLE LIMIT OF MEB91-11R1. THIS UNIT HAS BEEN REPAIRED IAW PROCEDURE OUTLINED IN MEB941-11R1 & RETURNED TO SERVICE.

Source: SDR HYIA20140415075 · FAA SDRS
O · 2011-04-05 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE, OEM PN 5142002-5, WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE WITHIN ALLOWABLE LIMIT. THIS UNIT HAS BEEN REPAIRED IAW PROCEDURE OUTLINED IN MEB941-11R1 & RETURNED TO SERVICE.

Source: SDR HYIA20140415043 · FAA SDRS
O · 2011-02-08 Matched by certificate designator
ATA 3230

AT SCHEDULED INSPECTION, NLG DRAG BRACE OEM PN 5142002-5 WAS FOUND TO BE CRACKED IN THE AREA OF NLG ACTUATOR ATTACH POINT. METHOD OF INSPECTION WAS DYE PENETRANT. THIS CRACK WAS FOUND TO BE WITHIN ALLOWABLE LIMIT. THIS UNIT HAS BEEN REPAIRED IAW PROCEDURE OUTLINED IN MEB941-11R1 & RETURNED TO SERVICE.

Source: SDR HYIA20140415025 · FAA SDRS
O · 2010-01-03 Matched by certificate designator
ATA 2460

CREW REPORTED AVIONICS BUSS FAILURE. MX R & R CIRCUIT BREAKER SWITCH. SYS CHECKS OK. ACFT RELEASED BACK TO SERVICE.

Source: SDR HYIA2714MAVMSTR · FAA SDRS
O · 2009-02-07 Matched by certificate designator
ATA 5400

RT ENG SURGING AT CRUISE POWER. RESHAPED LEFT NOSE BOWL DUE TO PROP CABLE ROD END CLEARANCE.

Source: SDR HYIA2714M · FAA SDRS
B · 2007-12-03 Matched by certificate designator
ATA 8120

PILOT LOG READS THE FOLLOWING: LEFT ENG SMOKES ON APPROACH. MAINTENANCE INSPECTED AND FOUND TURBO TO HAVE FAILED. MAINTENANCE REMOVED AND REPLACED THE TURBO.

Source: SDR 1357141120307 · FAA SDRS
B · 2003-09-30 Matched by certificate designator
ATA 3310

AFTER REACHING CRUISE ALTITUDE, CREW NOTICED SMOKE FROM PEDESTAL LIGHTING RHEOSTATS. DAY/NIGHT SWITCH TURNED OFF, CIRCUIT BREAKERS PULLED, SMOKE STOPPED. DIVERTED TO MECHANIC BASE. MECHANIC REMOVED AND REPLACED DIMMER ASSY AND RETURNED AIRCRAFT TO SERVICE.

Source: SDR HYI2003F00022 · FAA SDRS
B J · 2003-09-03 Matched by certificate designator
ATA 2210

5 MINUTES INTO CLIMB, CREW REPORTED SMOKE FROM AVIONICS RACK, RETURNED W/O INCIDENT. MECHANIC FOUND A/P PITCH SERVO HARNESS SHORTED, CAUSING A/P COMPUTER TO FAIL INTERNALLY, (TRANSISTORS OVERHEATED AND BURNED) REPAIRED SHORTED HARNESS. REPAIRED A/P COMPUTER, RETURNED MECHANIC TO SERVICE. (NE01200306064)

Source: SDR HYI2003F00011 · FAA SDRS
K R J · 2003-08-29 Matched by certificate designator
ATA 2810

ON CLIMB OUT, AFTER FIRST POWER REDUCTION, RIGHT ENGINE COST POWER, ATTEMPTED AUX FUEL PUMP, CROSSFEED, NO HELP. SECURED ENGINE AND FEATHERED PROP. RETURNED W/O INCIDENT. MECHANIC FOUND MAIN FUEL LINE TO ENGINE PUMP LOOSE. TIGHTENED LINE, RETURNED A/C TO SERVICE.

Source: SDR HYI2003F00014 · FAA SDRS
R J · 2003-08-27 Matched by certificate designator
ATA 2822

ON CLIMB OUT, TOWER REPORTED SMOKE FROM LT ENGINE, CREW REPORTED LOSS OF POWER AFTER AUX BOOST PUMP WAS TURNED ON, ENGINE SHUT DOWN, RETURNED W/O INCIDENT. MECHANIC REMOVED AND REPLACED LT ENGINE DRIVEN FUEL PUMP. RETURNED AC TO SERVICE.

Source: SDR HYI2003F00015 · FAA SDRS