N314TL

PERRY DICLEMENTE TUCANO REPLICA · 2019 · Valid Registration

Registered owner: SCHAAF RODNEY B, ND (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

O · 2014-09-14 Matched by certificate designator
ATA 5260

DURING PAX DEPARTURE FROM ACFT THAT THE LOWER STEP OF THE MAIN ENTRY STAIRS FAILED. THE LOWER STEP & SUPPORT CONTROLLER WAS REPLACED WITH NEW.

Source: SDR 9JLA2014122905065 · FAA SDRS
J · 2014-09-05 Matched by certificate designator
ATA 2215

AN INTERMITTENT YAW DAMPENER FAULT, INDICATING THAT THE AUTO PILOT WOULD TRIP OFF WHILE IN TURBULENCE. TROUBLESHOOTING FOUND THE RUDDER SERVO PN 622-6717-104 SN 1MNXJ TO BE WEAK. THIS UNIT WAS REMOVED FROM SERVICE & AN OVERHAULED UNIT WAS INSTALLED. OPERATIONS CHECKED OK.

Source: SDR 9JLA2014091005063 · FAA SDRS
J · 2014-01-04 Matched by certificate designator
ATA 3010

CREW REPORTED AN ANTI-ICE BLEED AIR DUCT FAILURE WARNING IN FLIGHT. TROUBLESHOOTING FOUND THE WING ANTI-ICE CONTAINMENT DUCT PRESS SWITCH HAD FAILED. THE SWITCH WAS REPLACED WITH NEW. LEAK & OPERATIONAL CHECKS WERE SATISFACTORY.

Source: SDR 9JLA2014012404246 · FAA SDRS
J · 2013-08-30 Matched by certificate designator
ATA 3340

THE FLIGHT CREW REPORTED THAT THE RT RETRACTABLE LANDING LIGHT WOULD NOT RETRACT AND STOW. TROUBLESHOOTING IDENTIFIED THE LANDING LIGHT ACTUATOR AS DEFECTIVE. REMOVED THE RT LANDING LIGHT ACTUATOR AND INSTALLED AN OVERHAULED UNIT. FUNCTIONAL CHECKED SATISFACTORY, ACFT RETURNED TO SERVICE.

Source: SDR 9JLA2013090504239 · FAA SDRS
N · 2013-04-19 Matched by certificate designator
ATA 3417

THE FLIGHT CREW REPORTED THAT THE NR 1 PDF INDICATED THE LOSS OF IAS AND ALT ON THE CAPTAINS SIDE WHILE ENROUTE. TROUBLESHOOTING INDICATED THE NR 1 ADC DEFECTIVE. THE ADC WAS REPLACED WITH AN O/H UNIT IAW AMM 34-10-01.

Source: SDR 9JLA2013052204235 · FAA SDRS
O · 2012-06-20 Matched by certificate designator
ATA 2110

CREW REPORTED THAT THE AIR CONDITIONING WAS INOPERATIVE. TROUBLESHOOTING IDENTIFIED THE AIR CON COMPRESSOR MOTOR AS DEFECTIVE. A MODIFIED MOTOR WAS INSTALLED, FUNCTIONAL CHECKED SATISFACTORY.

Source: SDR 9JLA201271904219 · FAA SDRS
O · 2012-06-20 Matched by certificate designator
ATA 2110

THE CREW REPORTED THE AIR CONDITIONING SYSTEM INOPERATIVE. TROUBLESHOOTING FOUND THE AIR CONDITIONER COMPRESSOR MOTOR DEFECTIVE. A MODIFIED MOTOR WAS INSTALLED. OPS CHECKS GOOD.

Source: SDR 9JLA2012071704219 · FAA SDRS
S · 2012-04-18 Matched by certificate designator
ATA 2422

CREW REPORTED THE LT INVERTER FAILED IN FLIGHT. FOUND THE LT AC INVERTER TO BE DEFECTIVE. INSTALLED AN O/H UNIT, FUNCTIONAL CHECKED SATISFACTORY.

Source: SDR 9JLA2012071704216 · FAA SDRS
B · 2007-02-22 Matched by certificate designator
ATA 2497

FLIGHT CREW REPORTED HEARING A POPPING SOUND FROM BEHIND THE COCKPIT LT SIDEWALL AREA FOLLOWED BY A SLIGHT ELECTRICAL ODOR FOR A PERIOD OF 15 SECONDS. NO SYSTEMS WERE AFFECTED AS ALL WERE OPERATING NORMALLY FOR THE DURATION OF THE FLIGHT (1.2 HRS). MFG AIRCRAFT SERVICES TECHNICIANS WERE DISPATCHED AND REMOVED ALL LT SIDEWALL PANELS FOR ACCESS. INSPECTION OF ALL ELECTRICAL COMPONENTS, CONNECTORS, AND WIRING REVEALED NO DEFECTS. SUBSEQUENT FLIGHTS WERE ALL UNEVENTFUL.

Source: SDR DIXA200700001 · FAA SDRS