N314XA

BOEING 737-484 · 1991 · Valid Registration

Registered owner: EASTERN 737 ASSET HOLDINGS LLC, MO (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

N · 2025-06-09 Matched by certificate designator
ATA 2697

#1 ENGINE FIRE HANDLE ILLUMINATED, AND FIRE BELL RANG LESS THAN 3 SECONDS DURING LEVEL OFF AT 3300 FT. AT THE START OF APPROACH. FOLLOWING QRH, DECLARED EMERGENCY. POWER WAS REDUCED ON #1 ENGINE AND NO FIRE HANDLE WAS PULLED. INSPECTED #1 ENGINE, NO EVIDENCE OF FIRE. ACCOMPLISHED PNUEMATIC LEAK CHECK, NO LEAKS NOTED. FOUND #1 ENGINE RH THRUST REVERSER PRESSING AGAINST WIRE HARNESS THAT'S MOUNTED TO PRSOV. REPOSITIONED PRSOV AND SECURED WIRE BUNDLE. FIRE LOOP TEST GOOD.

Source: SDR 4TXA202506130001 · FAA SDRS
L H · 2023-09-29 Unresolved
ATA 3350

EMERGENCY LIGHT AT STA 727+10R INOP. REMOVED AND REPLACED BATTERY PACK MODULE M1137, STA 975 IAW B737-400 AMM 33-51-51

Source: SDR I5EA2023092900032 · FAA SDRS
L · 2023-05-12 Unresolved
ATA 3350

EMERGENCY LIGHTS BATTERY CHARGER REQUIRES REPLACING AT STA. 308L. REMOVE AND REPLACED BATTERY CHARGER AT M1478 STA. 308L IAW B737-400 AMM 33-51-51. OPS CHECK GOOD.

Source: SDR I5EA2023051200003 · FAA SDRS
L · 2023-05-12 Unresolved
ATA 3350

EMERGENCY LIGHTS INOP LH FWD CABIN. REMOVED AND REPLACED BATTERY PACK AT M1478 STA. 308L IAW B737-400 AMM 33-51-51 OPS CHECK GOOD.

Source: SDR I5EA2023051200002 · FAA SDRS
L · 2021-11-19 Unresolved
ATA 3350

EMERGENCY LIGHT OUT R/H AT EMERGENCY EXIT HATCH AFT. REMOVED AND REPLACE BATTERY PACK AT M1435 STA. 747R, OPS CHECH GOOD IAW B737-400 AMM 33-51-51.

Source: SDR I5EA2021111900005 · FAA SDRS
L · 2021-10-02 Unresolved
ATA 3350

L/H OVER WING EXIT EMERGENCY SIGN INOP. REMOVED AND REPLACED BATTERY PACK AT M1134 AT STA.629L. OPS CHECK GOOD. IAW B737-400 AMM 33-51-51.

Source: SDR I5EA2021100200001 · FAA SDRS
R J · 2020-12-07 Unresolved
ATA 7200

NR 1 ENGINE, N1 ROLLBACK, UNCOMMANDED IN FLIGHT.

Source: SDR I5EA2020120900003 · FAA SDRS
J O · 2018-10-23 Unresolved
ATA 3610

AT FL320, CABIN ALT WARNING HORN, PERFORMED QRH PROCEDURE, DESCEND TO 10,000, RETURN TO GSO. AT CRUISE PRIOR TO PRESSURE LOSS RT PNEUMATIC PRESSURE 50 PSI, LEFT PNEUMATIC PSI 10. REMOVED AND REPLACED NR 1 ENG BLEEP AIR REGULATOR, NO LEAKS NOTED, OPERATIONAL TEST GOOD IAW AMM 36-11-16.

Source: SDR I5EA2018102400001 · FAA SDRS
O · 2018-04-27 Matched by certificate designator
ATA 3241

TROUBLESHOOTING REVEALED THE ANTI-SKID CONTROL HAD FAILED. THE ANTI-SKID CONTROL WAS REPLACED. OPS AND BITE CHECKED GOOD.

Source: SDR BJNA20180501001 · FAA SDRS
J · 2017-08-22 Matched by certificate designator
ATA 2780

AFTER TAKE OFF, AND FLAPS RETRACTED, THE LEADING EDGE FLAPS TRANSIT AMBER LIGHT REMAINED ILLUMINATED. NR 2 SLAT GREEN LIGHT REMAINED ILLUMINATED. AIRPLANE WAS TAKEN OUT OF SERVICE TO PERFORMED MAINTENANCE.

Source: SDR BJNA20170822007 · FAA SDRS