N31GV

GULFSTREAM AEROSPACE G-IV · 1988 · Valid Registration

Registered owner: AIRCRAFT FIDELITY CORP TRUSTEE, DE (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2022-12-26 Matched by certificate designator
ATA 3200

PILOTS REPORTED HEAVIER THAN NORMAL BRAKING ON TAXI OUT FOR TAKE OFF ROLL. ON TAKE OFF, ANTI SKID FAIL AMBER CAS AND BRAKE MAINT REQD CYAN CAS ILLUMINATED. FOLLOWED QRH PROCEDURES AND ATTEMPTED TO RESET ANTI SKID SYSTEM. WHEN IT WAS DETERMINED THAT THEY WERE UNABLE TO DO SO. LANDED WITHOUT FAULT AND USED MAX TR AND RUNWAY LENGTH TO SLOW DOWN SAFELY. ATC DECLARED EMERGENCY FOR THE PILOTS. ON LANDING, EVEN A SLIGHT TOUCH TO THE BRAKES CAUSED THE SYSTEM TO LOCK UP ALMOST IMMEDIATELY. PILOT USED A MIXTURE OF HAND BRAKE AND TR FOR CONTROL UNTIL ARRIVING AT THE FBO. TECHNICIAN WAS ABLE TO VISIT THE AIRCRAFT ON 12/24 AND PERFORM TROUBLESHOOTING WITH THE OEM. IT HAS BEEN DETERMINED THAT A BRAKE CONTROL UNIT IS FAULTY AT THIS POINT.

Source: SDR 6TXA2022122600001 · FAA SDRS
J · 2022-12-23 Matched by certificate designator
ATA 3240

PILOTS REPORTED HEAVIER THAN NORMAL BRAKING ON TAXI OUT FOR TAKE OFF ROLL. ON TAKE OFF, ANTI SKID FAIL AMBER CAS AND BRAKE MAINT REQD CYAN CAS ILLUMINATED. PILOT FOLLOWED QRH PROCEDURES AND ATTEMPTED TO RESET ANTI SKID SYSTEM. WHEN IT WAS DETERMINED THAT THEY WERE UNABLE TO DO SO, REQUESTED A LONGER RUNWAY IN THE AREA NEAR WHERE WE ORIGINALLY FILED TO LAND. PILOT LANDED WITHOUT FAULT AND USED MAX TR AND RUNWAY LENGTH TO SLOW DOWN SAFELY. ATC DECLARED EMERGENCY. ON LANDING,, EVEN A SLIGHT TOUCH TO BRAKES CAUSED SYSTEM TO LOCK UP ALMOST IMMEDIATELY. PILOT USED A MIXTURE OF HAND BRAKE AND TR FOR CONTROL UNTIL ARRIVING AT THE FBO. IT HAS BEEN DETERMINED THAT A BRAKE CONTROL UNIT IS FAULTY AT THIS POINT.

Source: SDR 6TXA2023122700002 · FAA SDRS
J · 2022-11-28 Matched by certificate designator
ATA 2133

CREW DEPARTED KVNY AND AS THEY APPROACHED 10K THEY NOTICED THEIR EARS WERE BEGINNING TO FEEL INTENSE PRESSURE AND FELT THE PRESSURE BUILDING UP. ATTEMPTED TO ADJUST CLIMB RATE FROM 500-300 FT / MINUTE WITH NO LUCK. CABIN WAS 1800-2000 / MINUTE. AT 12K THE RED CAS CAME ON ALERTING THEM TO DON THEIR MASKS. THEY STOPPED CLIMBING AND DESCENDED TO 10K. THEY DECIDED TO LAND AND ABORT THE CURRENT LEG. NO PASSENGERS ON BOARD AND THE O2 MASKS WERE NOT DEPLOYED IN THE CABIN. UPON LANDING A RUNDOWN OF THE ISSUE WAS GATHERED FROM THE PILOTS. NO KNOWN ISSUES OTHER THAN THE PRESSURIZATION. WE DISPATCHED TECHNICIANS TO PERFORM A THOROUGH PRESSURIZATION CHECK OF THE CABIN AND OPERATIONAL CHECK OF THE OUTFLOW VALVE. NO DEFECTS NOTED. SCHEDULED A MAINTENANCE CHECK FLIGHT FOR VERIFICATION AND NO ISSUES WERE PRESENT. AT THIS TIME WE FEEL THAT THE ISSUE WAS RELATED TO IMPROPER PREFLIGHT SET UP OF THE PRESSURIZATION PANEL. THIS IS THE SECOND EVENT ON A SECOND AIRCRAFT WHERE THE SAME SIC WAS INVOLVED.

Source: SDR 6TXA2022112800474 · FAA SDRS