N358F

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
Southern Jet of Boca Raton, Inc. (Q2JA)Certificate holderMatched by certificate designator

Accident & incident history

Accident · 1967-07-09 Matched by aircraft (N-number)
Fairchild PC-6CH Serious injurySouthern Jet of Boca Raton, Inc.
Source: NTSB case SEA68D0042

Maintenance disclosures

J · 2023-02-08 Matched by certificate designator
ATA 3417

THE FLIGHT CREW REPORTED AN AIR DATA COMPUTER FAILURE. THE MAINTENANCE PROVIDER VERIFIED DISCREPANCY AND REPLACED THE NO2 ADC WITH REPAIRED UNIT. OPS AND LEAK CHECKS WERE SATISFACTORY, AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2023021642202 · FAA SDRS
N · 2022-12-25 Matched by certificate designator
ATA 7600

THE FLIGHT CREW REPORTED THAT A RIGHT AMBER ENGINE COMPUTER ANNUNCIATOR ILLUMINATED DURING FLIGHT. THE MAINTENANCE PROVIDER TROUBLESHOT AND CONFIRMED THAT THE FLAP AND ENGINE SYNC RELAY BOX WAS DEFECTIVE. THE RELAY BOX WAS REMOVED, AND A REPAIRED RELAY BOX WAS INSTALLED. OPERATIONAL CHECKS WERE SATISFACTORY. THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2023010632293 · FAA SDRS
O · 2022-10-06 Matched by certificate designator
ATA 2110

THE FLIGHT CREW REPORTED THAT DURING THE POSTFLIGHT IT WAS DISCOVERED THE FREON AIR CONDITIONING SYSTEM WAS INOP. THE AIR CONDITIONING SYSTEM WAS DEFERRED ON MEL AND AIRCRAFT OPERATIONS WERE CONTINUED. THE MAINTENANCE PROVIDER TROUBLESHOT AND FOUND THE COMPRESSOR MOTOR WAS NOT WORKING. THE MOTOR WAS REMOVED, AND AN OVERHAULED UNIT WAS INSTALLED. OPERATIONAL CHECKS WERE SATISFACTORY. MEL WAS CLEARED AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA2022101232269 · FAA SDRS