N35TJ

BEECH V35B · 1973 · Valid Registration

Registered owner: BEECH D9462 LLC, OH (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

N · 2007-11-26 Unresolved
ATA 2612

UPON TAKEOFF, AC CLEARED TO FL410 AND THEN REQUESTED, AND WAS APPROVED FOR FL430. DURING CLIMB TO FL430, RT ENGINE FIRE WARNING LIGHT ILLUMINATED. FLIGHT CREW SLIGHTLY RETARDED THE POWER BACK ON THE RT ENGINE (WHICH WAS AT MAX CONTINUOUS ITT INDICATION) REQUESTED CLEARANCE TO FL390 AND DECLARED AN EMERGENCY. UPON PULLING POWER BACK THE FIRE WARNING LIGHT EXTINGUISHED. ADVANCING POWER ON THE AFFECTED ENGINE DID NOT CAUSE THE LIGHT TO ILLUMINATE AGAIN. NO DIFFERENCES OBSERVED BETWEEN LT AND RT ENGINE INDICATIONS. FLIGHT CREW PERFORMED FIRE WARNING CHECKLIST AND DETERMINED THAT THERE WAS A FALSE FIRE INDICATION. FLIGHT CREW UNDECLARED THE EMERGENCY. AIRCRAFT LANDED WITHOUT INCIDENT. AN EXTENSIVE VISUAL INSPECTION OF THE FIRE WARNING SYSTEM WAS PERFORMED WITH NO DEFECTS NOTED. FIRE LOOP TEST, AND ENGINE RUNS WERE PERFORMED WITH NO DEFECTS NOTED. UPON DISCUSSION WITH MFG SPECIALISTS, IT WAS STATED THAT, WHEN CLEARED TO FL DIRECT, AND AT MAX ITT AN OCCASIONAL FALSE FIRE WARNING WILL BE TRIGGERED. FALSE FIRE INDICATION HAS NOT RECURRED. SUSPECT NON-RECURRING ELECTRICAL PHENOMENON. (K)

Source: SDR VUC2007F00001 · FAA SDRS
N · 2007-11-26 Unresolved
ATA 2612

DURING CLIMB, RT ENGINE FIRE WARNING LIGHT ILLUMINATED. FLT CREW RETARDED POWER PACK ON RT ENGINE (WHICH WAS AT MAX CONTINUOUS ITT INDICATION), REQUESTED CLEARANCE TO FL 390 AND DECLARED AN EMERGENCY. UPON PULLING POWER BACK THE FIRE WARNING LIGHT EXTINGUISHED. ADVANCING POWER ON THE AFFECTED ENGINE DID NOT CAUSE THE LIGHT TO ILLUMINATE AGAIN. NO DIFFERENCES OBSERVED BETWEEN LT AND RT ENGINE INDICATIONS. FLIGHT CREW PERFORMED FIRE WARNING CHECKLIST AND DETERMINED THAT THERE WAS A FALSE FIRE INDICATION. FLIGHT CREW UNDECLARED THE EMERGENCY. AC LANDED WITHOUT INCIDENT. AN EXTENSIVE VISUAL INSPECTION OF THE FIRE WARNING SYS WAS PERFORMED WITH NO DEFECTS NOTED. FIRE LOOP TEST WAS PERFORMED WITH NO DEFECTS NOTED. ENGINE RUNS WERE PERFORMED WITH NO DEFECTS NOTED. UPON DISCUSSION WITH MFG SPECIALISTS, IT WAS STATED THAT, WHEN CLEARED TO FL DIRECT, AND AT MAX ITT AN OCCASIONAL FALSE FIRE WARNING WILL BE TRIGGERED. FALSE FIRE INDICATION HAS NOT RECURRED. SUSPECT NOT-RECURRING ELECTRICAL PHENOMENON.

Source: SDR VUC2007F00000 · FAA SDRS
O · 2004-01-29 Unresolved
ATA 7230

4TH LPC STATOR LOST 1 EACH VANE, RELATED DAMAGE INCLUDES HIGH AND LOW PRESSURE COMPRESSORS, AND HIGH AND LOW PRESSURE TURBINES.

Source: SDR UO22004F00000 · FAA SDRS
O · 2004-01-29 Unresolved
ATA 7210

1 EACH PLANETARY BEARING FAILED, CAUSING MASSIVE CHAIN REACTION FAILURE WITHIN FAN GEARBOX.

Source: SDR UO22004F00001 · FAA SDRS
O · 2004-01-29 Unresolved
ATA 7210

1 EA PLANETARY BEARING FAILED, CAUSING MASSIVE CHAIN REACTION FAILURE WITHIN FAN GEARBOX.

Source: SDR UO22004F00007 · FAA SDRS
B · 2000-10-27 Matched by certificate designator
ATA 2121

CREW NOTICED SMOKE IN CABIN AFTER TAKEOFF AND RETURNED TO AIRPORT. MOTOR INSIDE BLOWER ASSY WAS FOUND HEAT AND SMOKE DAMAGED. (X)

Source: SDR 20001120SH031 · FAA SDRS