N366JA
Operators of this aircraft
Who operated this tail, and how firmly we know it.
No operator established for this aircraft.
Accident & incident history
No NTSB accidents or incidents on file for this aircraft.
Maintenance disclosures
AFTER TAKEOFF, WHEN THE CREW SELECTED GEAR UP THEY NOTICE UNUSUAL SOUNDS. ALL INDICATIONS SEEMED TO BE NORMAL AND FLAPS WERE SELECTED UP. THE COMBINE HYDRAULIC SYS BEGAN TO FALL. THE CREW GOT INDICATIONS THAT THE PRESSURE WAS LOW, THEN OK, THEN LOW AGAIN. THE UTILITY PUMP CYCLED ON AND OFF. THE CREW RETURNED THE FLAPS TO TEN, THE COMBINE HYD WARNING LIGHT BEGAN TO FLASH. THE CREW THEN LOWERED THE GEAR AND REQUESTED TO RETURN TO DEPARTURE. WHEN THE CREW SELECTED THE FLAPS TO 20 THEY GOT NO MOVEMENT OF THE FLAPS. THE CREW THEN RAN THE COMBINE HYDRAULIC FALL AND FLAP TEN LANDING CHECKLIST JUST PRIOR TO TOUCHDOWN AND TURNED ON THE AUX HYD PUMP. HALFWAY DOWN THE RUNWAY THE CREW LOST THE TOE BRAKES AND USED THE PARKING BAKES TO STOP THE AIRCRAFT. WE TROUBLESHOT THE HYD SYS AND FOUND THE GROUND SPOILER DEACTIVATION VALVE LEAKING. (K)
DURING CLIMB OUT, AFTER TAKEOFF, APPROXIMATELY 5K FEET THE CREW HEARD A LOUD BANG FROM THE LT ENGINE. THE CREW CHECKED THE ENGINE PARAMETERS AND FOUND 0 EPR AND NOTICED THAT THE POWER LEVER WAS UNRESPONSIVE ON THE LT ENGINE. LP HP WAS APPROXIMATELY 30 PERCENT AND THE TGT WAS 500 DEGREES AND THE CREW SHUT THE ENGINE DOWN AND LANDED THE ACFT. (K)