N376

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

Incident · 1970-02-05 Unresolved
Grumman G-159 None injuryoperator not yet resolved
Source: NTSB case NYC70IN082
Incident · 1964-12-02 Unresolved
Grumman G159 None injuryoperator not yet resolved
Source: NTSB case UNK65X0905

Maintenance disclosures

F J · 2019-04-08 Matched by certificate designator
ATA 2760

AT FL450 ACTIVATED THE SPOILERS THEY CAME OUT THEN RETRACTED RIGHT AWAY.  RECEIVED GRND SPLR FAIL CAS MESSAGE AND SPOILER FAULT CAS PERFORMED FIM TASK 27-66-00. PERFORMED MULTIPLE F/T OF SPOILER SYSTEM WITH NO DEFECTS NOTED. PER CUSTOMER REQUEST REPOSITIONED LT AND RT FCE. LT FCE NOW P/N 462900-1017 S/N 1199. RT FCE NOW 462900-1017 S/N 1200. PERFORMED FLAP SYSTEM RIGGING WITH REF TO MM 27-50-00. PERFORMED SPOILER SYSTEM RIGGING WITH REF TO MM 27-60-00. ALL SUBSEQUENT OPS CHECKS SATISFACTORY.

Source: SDR DJFA20190408001 · FAA SDRS
E · 2004-11-20 Unresolved
ATA 7200

ON ADVANCING THRUST LEVERS, CREW FELT A VIBRATION COMING FROM NR 2 ENGINE, AT THE SAME TIME A TRIPLE CHIME OF "E2 LOW N1". TAKEOFF ABORTED JUST BEFORE 80 KNOTS & TAXIED A SHORT DISTANCE TO J INTERSECTION. AFTER TAKEOFF ABORTED TRIPLE CHIME MESSAGE WENT AWAY & "E2 NO DISP" REMAINED ON. AFTER EXITING RUNWAY NR 2 ENGINE SHUTDOWN. WHEN MZ ARRIVED THEY SAW THE ATS ACCESS DOOR BLOWN OPEN & FOUND METAL SHAVINGS IN THE TAIL PIPE. MAINTENANCE STARTED THE NR 2 ENGINE & NOTICED THERE WAS NO N1 IND & SHUT IT DOWN. MX INSPECTED ENGINE & FOUND IT WAS SEVERELY DAMAGED. R/R NR 2 ENGINE. LEAKS AND OPS CHECKS GOOD.

Source: SDR CHQA000588 · FAA SDRS
O · 2002-05-25 Unresolved
ATA 2121

CREW REPORTED PFD FAILURE AND POPPED C/B TO F30 ELECT BAY COOLING. CREW DECIDED TO RETURN TO FIELD. PFP OPS CHECK GOOD. CLEANED DEBRIS FROM COOLING FAN.

Source: SDR 000161 · FAA SDRS