N39FN

GATES LEAR JET 35 · 1974 · Valid Registration

Registered owner: GH EQUIPMENT LLC, DE (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

No operator established for this aircraft.

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

F · 2012-03-21 Matched by certificate designator
ATA 2700

AFTER TAKE OFF, ACFT EXPERIENCED AN UN-COMMANDED ROLL. FULL RT YOKE REQUIRED FOR STRAIGHT AND LEVEL FLIGHT. FULL DOWN TRIM TO RIGHT REQUIRED FOR STRAIGHT AND LEVEL FLIGHT. DUMPED 1500 LBS OF FUEL AT 7000", 15-20 NAUTICAL MILES OVER SEA.

Source: SDR BHKA2012032100001 · FAA SDRS
J · 2009-11-24 Unresolved
ATA 3510

DURING THE ENROUTE CLIMB, PERFORMED THE 10,000 FOOT PORTION OF CLIMB CHECKLIST. WHEN TESTING THE O2 MASKS, DISCOVERED THAT NEITHER CREW O2 MASK HAD OXYGEN FLOW. DUE TO LOSS OF THE SUPPLEMENTAL OXYGEN SYS, ELECTED TO RETURN TO BASE. LANDED WITHOUT INCIDENT. UPON LANDING, THE O2 VALVE IN THE NOSE OF THE ACFT WAS EXAMINED AND FOUND TO BE SLIGHTLY OUT OF THE "ON" DETENT.

Source: SDR 2009FA0000990 · FAA SDRS
B · 2009-08-20 Matched by certificate designator
ATA 2121

DURING CLIMBOUT PASSING THROUGH 16000 FT A ODOR WAS DETECTED IN COCKPIT. AIR CONDITIONER BLOWER WAS TURNED OFF WHICH APPEARED TO HELP. ALL OK UNTIL THROTTLES PULLED TO IDLE AND RADIO DESCENT INITIATED. DECIDED TO RTB AND FOLLOWED SMOKE/FUMES IN COCKPIT CHECKLIST WITH NO DIFFERENCE IN ODOR. DURING DESCENT TO 10000 FT CABIN BLOWER C/B WAS FOUND POPPED, COCKPIT AIR WAS TURNED ON WHICH LESSENED THE ODOR. O2 MASKS WERE PULLED OUT AS A PRECAUTION BUT WERE NOT NEEDED.

Source: SDR 2009FA0000728 · FAA SDRS