N400TC

RAYTHEON AIRCRAFT COMPANY 400A · 1999 · Valid Registration

Registered owner: MORNING STAR AVIATION LLC, IN (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
JET LINX AVIATION, LLC (9JLA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

K · 2022-01-14 Matched by certificate designator
ATA 2810

THE FLIGHT CREW REPORTED THAT DURING FLIGHT THE LEFT WING FUEL CAP WAS VENTING FUEL. THE FLIGHT CREW ELECTED TO DIVERT FLIGHT AND RETURN BACK TO THE AIRPORT FOR MAINTENANCE CONSIDERATIONS. THE LANDING WAS UNEVENTFUL. THE MAINTENANCE TEAM DETERMINED THE FUEL CAP SEAL WAS WORN. THE FUEL CAP WAS REMOVED AND REPLACED WITH A NEW CAP. OPS CHECKS GOOD AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 9JLA202201188731 · FAA SDRS
L · 2021-05-13 Matched by certificate designator
ATA 2432

FLIGHT CREW REPORTED THAT THE BATTERY FEED TEST DID NOT TEST CORRECTLY DURING PREFLIGHT CHECKS, FLIGHT WAS CANCELLED. THE MAINTENANCE VENDOR TROUBLESHOT AND FOUND A FAULTY BATTERY FEEDER PROTECTOR UNIT P/N 50284-003 S/N 98054. THE UNIT WAS REMOVED AND A NEW UNIT WAS REMOVED AND A NEW UNIT WAS INSTALLED. OPERATIONAL CHECKS WERE SATISFACTORY. THE AIRCRAFT WAS THEN RETURN TO SERVICE.

Source: SDR 9JLA2021052729346 · FAA SDRS
O · 2021-05-08 Matched by certificate designator
ATA 3510

THE FLIGHT CREW REPORTED THAT A SMALL PIECE OF CO-PILOTS OXYGEN MASK SEPARATED FROM THE MASK ASSEMBLY. THE PLANNED FLIGHT WAS CANCELLED. THE MAINTENANCE TEAM REMOVED THE DEFECTIVE CO-PILOTS OXYGEN P/N 174252-92 S/N10710 AND INSTALLED AN OVERHAULED MASK ASSEMBLY. THE AIRCRAFT WAS RETURNED TO SERVICE. TOTAL TIME IN SERVICE 709.3 HRS

Source: SDR 9JLA2021051829344 · FAA SDRS
O · 2020-11-29 Matched by certificate designator
ATA 7421

A FLIGHT WAS CANCELLED WHEN THE FLIGHT CREW WAS UNABLE TO ACHIEVE NR 2 ENGINE START. THE FLIGHT CREW REPORTED THAT THE ENGINE FAILED TO LIGHT OFF. THE MAINTENANCE VENDOR DETERMINED THAT THE IGNITOR PLUGS WERE WORN AND REQUIRED TO BE REPLACED. THE VENDOR REPLACED THE IGNITOR PLUGS WITH NEW P/N 68032.

Source: SDR 9JLA20201202 · FAA SDRS