N4057C

CESSNA 414A · 1982 · Valid Registration

Registered owner: ABERDEEN FLYING SERVICE, SD (owner ≠ operator)

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
ABERDEEN FLYING SERVICE INC (BGJA)Certificate holderMatched by certificate designator
ABERDEEN FLYING SERVICE INC (BGJA)Operator2011-03-22 – 2011-03-22Operator named in NTSB report

Accident & incident history

Acc · 2011-03-22 Operator named in NTSB report
CESSNA 414A None injury Part 135ABERDEEN FLYING SERVICE INC
Source: NTSB case CEN11LA273

Maintenance disclosures

R E · 2015-07-15 Matched by certificate designator
ATA 7314

DURING TAKEOFF ROLL THE RIGHT ENGINE WOULD NOT MAKE FULL POWER. THE PILOT CANCELLED THE TAKEOFF AND RETURNED TO THE SHOP. THE AIRCRAFT NEVER LEFT THE GROUND. MAINTENANCE WAS NOTIFIED AND TROUBLESHOOT THE ISSUE. MAINTENANCE FOUND THE RIGHT ENGINE WASTE GATE WAS LEAKING OIL OUT OF THE CASE AT THE SEAL, THIS WOULD HAVE CAUSED THE TURBOCHARGER TO NOT ENGAGE PROPERLY. THE WASTE GATE WAS REPLACED WITH AN OVERHAULED UNIT. A GROUND RUN WAS PERFORMED AND A SECOND ISSUE WAS FOUND. THE ENGINE DRIVE FUEL PUMP WAS PUMPING ERRATIC AT HIGH POWER SETTINGS. THE FUEL PUMP WAS REPLACED WITH AN OVERHAULED UNIT. WE RIGGED THE FUEL PUMP TO THE ENGINE AND PERFORMED SEVERAL GROUND RUNS AT VARIOUS POWER SETTINGS. ALL SYSTEMS CHECKED GOOD ON THE GROUND. A FLIGHT CHECK WAS PERFORMED WITH A PILOT. THE ENGINE RAN AS DESIGNED IN FLIGHT. NO FURTHER ISSUES NOTED.

Source: SDR BGJA20150721002 · FAA SDRS
K R E · 2015-07-15 Matched by certificate designator
ATA 8120

DURING TAKEOFF ROLL, THE RT ENG WOULD NOT MAKE FULL POWER. THE PILOT CANCELLED THE TAKEOFF & RETURNED TO THE SHOP. THE ACFT NEVER LEFT THE GND. MX WAS NOTIFIED & TROUBLE SHOT THE ISSUE. THE RT ENG WASTE GATE WAS LEAKING OIL OUT OF THE CASE AT THE SEAL, THIS WOULD HAVE CAUSED THE TURBOCHARGER TO NOT ENGAGE PROPERLY. THE WASTE GATE WAS REPLACED WITH AN OVERHAULED UNIT. A GND RUN WAS PERFORMED & A SECOND ISSUE WAS FOUND. THE ENG DRIVE FUEL PUMP WAS PUMPING ERRATIC AT HIGH POWER SETTINGS. THE FUEL PUMP WAS REPLACED WITH AN OVERHAULED UNIT. WE RIGGED THE FUEL PUMP TO THE ENG & PERFORMED SEVERAL GND RUNS AT VARIOUS POWER SETTINGS. ALL SYS CHECKED GOOD ON THE GND. A FLIGHT CHECK WAS PERFORMED WITH A PILOT. THE ENG RAN AS DESIGNED IN FLIGHT. NO FURTHER ISSUES NOTED.

Source: SDR BGJA20150721001 · FAA SDRS
O · 2014-02-02 Matched by certificate designator
ATA 8530

DURING INSPECTION WE FOUND THE NR 3 CYLINDER TO HAVE A CRACK & WAS LEAKING FUEL DOWN ON TO THE INTAKE PIPE. PROCEEDED TO INSPECT THE CYLINDER & IT WAS FOUND TO HAVE A CRACK. THE CRACK WAS BETWEEN THE 1ST & 2ND LARGE COOLING FIN BEHIND THE FUEL INJECTOR & DOWN ALONG THE SIDE AREA. THE CRACK APPEARED TO BE NEAR THE AREA OF THE VLV SEAT. REPLACEMENT CYLINDER SENT IN TO US FOR FULL WARRANTY. A BORESCOPE INSPECTION ON A FEW CYLINDERS, CHECKED THE EGT & CHT PROBE. AFTER ALL INSPECTIONS & TEST FOUND NOTHING WRONG IN THE CYLINDERS OR OUR OPERATION OF THE ACFT.

Source: SDR BGJA20140501001 · FAA SDRS
O · 2013-12-16 Matched by certificate designator
ATA 8530

DURING INSPECTION FOUND CYLINDER CRACKED.

Source: SDR BGJA2013121600749 · FAA SDRS
O · 2013-12-16 Matched by certificate designator
ATA 8530

DURING INSPECTION, FOUND CYLINDER CRACKED.

Source: SDR BGJA2013121600031 · FAA SDRS
O · 2013-11-23 Matched by certificate designator
ATA 8530

CRACKED ENGINE CYLINDER.

Source: SDR 2013FA0000679 · FAA SDRS
O · 2013-10-29 Matched by certificate designator
ATA 8530

DURING INSPECTION, FOUND CYLINDER CRACKED.

Source: SDR LZ2R2014121700064 · FAA SDRS
O · 2013-10-29 Matched by certificate designator
ATA 8530

DURING INSPECTION, FOUND CYLINDER CRACKED.

Source: SDR LZ2R2014121700065 · FAA SDRS
O · 2013-10-29 Matched by certificate designator
ATA 8530

DURING INSPECTION, FOUND CYLINDER CRACKED.

Source: SDR LZ2R2014121700034 · FAA SDRS
O · 2013-10-29 Matched by certificate designator
ATA 8530

DURING INSPECTION, FOUND CYLINDER CRACKED.

Source: SDR LZ2R2014121700041 · FAA SDRS
O · 2013-10-29 Matched by certificate designator
ATA 8530

CRACKED ENGINE CYLINDER.

Source: SDR 2013FA0000689 · FAA SDRS
O · 2013-10-29 Matched by certificate designator
ATA 8530

CRACKED ENGINE CYLINDER.

Source: SDR 2013FA0000690 · FAA SDRS
O · 2013-10-29 Matched by certificate designator
ATA 8530

CRACKED ENGINE CYLINDER.

Source: SDR 2013FA0000691 · FAA SDRS
O · 2013-04-01 Matched by certificate designator
ATA 8530

DURING INSPECTION, FOUND CYLINDER CRACKED.

Source: SDR BGJA2013121600750 · FAA SDRS
O · 2013-04-01 Matched by certificate designator
ATA 8530

DURING AN INSPECTION, FOUND CYLINDER CRACKED.

Source: SDR BGJA2013121600751 · FAA SDRS
O · 2013-01-15 Matched by certificate designator
ATA 8530

CRACKED ENGINE CYLINDER.

Source: SDR 2013FA0000677 · FAA SDRS
O · 2013-01-15 Matched by certificate designator
ATA 8530

CRACKED CYLINDERS.

Source: SDR BGJA2014F00062 · FAA SDRS
O · 2013-01-15 Matched by certificate designator
ATA 8530

CRACKED ENGINE CYLINDER.

Source: SDR 2013FA0000678 · FAA SDRS
O · 2013-01-11 Matched by certificate designator
ATA 8530

DURING AN INSPECTION WE FOUND SEVERAL ECI CYLINDERS CRACKED EITHER BY THE FUEL INJECTOR PORT OR BETWEEN THE FIRST SET OF FINS.

Source: SDR BGJA20131274141 · FAA SDRS
O · 2013-01-11 Matched by certificate designator
ATA 8530

DURING AN INSPECTION WE FOUND SEVERAL ECI CYLINDER TO BE CRACKED AT EITHER THE SPARK PLUG PORT OR BETWEEN THE FINS.

Source: SDR BGJA201312174142 · FAA SDRS
B · 2012-08-16 Matched by certificate designator
ATA 3100

ACFT DEPARTED ON A IFR FLIGHT PLAN AT 13:17Z WITH 5 PASSENGERS ONBOARD. JUST AFTER DEPARTURE, AT APPROX 500 FEET, THE CAPTAIN SMELLED AND NOTICED SMOKE COMING FROM THE THROTTLE QUADRANT AREA, SPECIFICALLY THE INTERIOR LIGHT CONTROL PANEL. HE IMMEDIATELY NOTIFIED THE CONTROL TOWER AND LANDED THE ACFT. DISPATCHED BY THE DIRECTOR OF MAINTENANCE TO INVESTIGATE THE PROBLEM AND THEY CONFIRMED THAT IN FACT THE INSTRUMENT LIGHT ON-OFF SWITCH IN THE LIGHTING CONTROL PANEL HAD FAILED.

Source: SDR 2012F00166 · FAA SDRS
O · 2005-03-08 Matched by certificate designator
ATA 5310

LOWER DOOR FRAME CRACKING BY THE REAR HINGE.

Source: SDR 2005F00039 · FAA SDRS