N405PA

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
PHOENIX AIR GROUP INC (ESPA)Certificate holderMatched by certificate designator

Accident & incident history

Incident · 1969-10-14 Unresolved
Boeing 707 None injuryoperator not yet resolved
Source: NTSB case UNK70X0100
Incident · 1965-11-25 Unresolved
BOWING 707 321 None injuryoperator not yet resolved
Source: NTSB case NYC66I0059

Maintenance disclosures

A Y J · 2025-10-01 Matched by certificate designator
ATA 7200

TRANSPORTING PASSENGERS FROM KNTD TO KNSI. ONCE THE ACFT BEGAN CLIMBING TO CRUISE ALTITUDE, CAPT & 1ST OFFICER NOTICED SIGNS OF A LT ENGINE FAILURE & RESPONDED TO AN ENGINE FAILURE. FA1 NOTIFIED CAPT OF THE ENG FIRE, & CAPT ATTEMPTED TO PUT OUT THE FIRE WHILE 1ST OFF DECLARED AN EMERGENCY TO ATC. CAPT SUCCESSFULLY EXTINGUISHED FIRE MID-FLIGHT. ACFT LANDED SAFELY, FIRE DEPART CONFIRMED FIRE EXTINGUISHED. ENGINE 1 SUSTAINED SUBSTANTIAL FIRE DAMAGE, BUT FIRE WAS CONTAINED WITHOUT AIRFRAME FIRE OR EXPLOSION. BASED ON EXAMINATION BY PAGS MAINTENANCE TECHS, EVIDENCE INDICATES THAT EVENT WAS PRECIPITATED BY A SUDDEN STOPPAGE OF CORE COMPONENTS OF ENGINE’S ROTATING ASSY, CONSISTENT WITH A MAIN SHAFT BEARING FAILURE. THIS SUDDEN STOPPAGE DISRUPTED THE ANNULAR COMBUSTION PATTERN WITHIN THE BURNER CAN, PERMITTING UNBURNED FUEL TO MIGRATE INTO THE TAILPIPE, WHERE IT IGNITED. ONCE THE CREW EXECUTED SHUTDOWN & FIRE CHECKLIST THE TAILPIPE FIRE EXTINGUISHED.

Source: SDR ESPA202510010675 · FAA SDRS
Y A · 2025-06-12 Matched by certificate designator
ATA 7200

ON JUNE 12TH, 2025, PHOENIX AIR GROUP, INC. (PAG) WAS TRANSPORTING PASSENGERS FROM POINT MUGU NAVAL AIR STATION (KNTD) TO SAN NICOLAS ISLAND NAVAL OUTLYING FIELD (KNSI) USING AIRCRAFT N405PA. ONCE THE AIRCRAFT BEGAN CLIMBING TO ITS CRUISE ALTITUDE, CAPTAIN 1 (CA1) AND FIRST OFFICER 1 (FO1) NOTICED SIGNS OF A LEFT ENGINE FAILURE AND RESPONDED TO AN ENGINE FAILURE. FLIGHT ATTENDANT 1 (FA1) NOTIFIED CA1 OF THE ENGINE FIRE, AND CA1 ATTEMPTED TO PUT OUT THE ENGINE FIRE WHILE FO1 DECLARED AN EMERGENCY TO AIR TRAFFIC CONTROL (ATC). CA1 SUCCESSFULLY EXTINGUISHED THE FIRE MID-FLIGHT. FIRE TRUCKS WERE ON STANDBY AS THE AIRCRAFT WAS LANDING, THE AIRCRAFT LANDED SAFELY, AND THE FIRE DEPARTMENT CONFIRMED THAT THE FIRE HAD BEEN EXTINGUISHED AND THAT THE AIRCRAFT WAS SAFE TO RETURN TO THE TERMINAL TO UNLOAD PASSENGERS. ENGINE 1 SUSTAINED SUBSTANTIAL FIRE DAMAGE, BUT THE FIRE WAS CONTAINED WITHOUT AIRFRAME FIRE OR EXPLOSION. BASED ON EXAMINATION BY PHOENIX AIR GROUP’S MAINTENANCE TECHNICIANS, EVIDENCE INDICATES THAT THE EVENT WAS PRECIPITATED BY A SUDDEN STOPPAGE OF THE CORE COMPONENTS OF THE ENGINE’S ROTATING ASSEMBLY, CONSISTENT WITH A MAIN SHAFT BEARING FAILURE. THIS SUDDEN STOPPAGE DISRUPTED THE ANNULAR COMBUSTION PATTERN WITHIN THE BURNER CAN, PERMITTING UNBURNED FUEL TO MIGRATE INTO THE TAILPIPE, WHERE IT IGNITED. ONCE THE CREW EXECUTED THE ENGINE SHUTDOWN AND FIRE CHECKLIST THE TAILPIPE FIRE EXTINGUISHED.

Source: SDR 2025F00223 · FAA SDRS
P · 2023-04-19 Matched by certificate designator
ATA 3234

NO NOSE GEAR DOWN LOCK INDICATION WHEN GEAR HANDLE SELECTED DOWN. REMOVED AND REPLACED GEAR SELECTOR WITH INSPECTED /SERVICEABLE UNIT.

Source: SDR ESPA2023042000307 · FAA SDRS
O · 2004-06-07 Matched by certificate designator
ATA 5280

STEEL HINGE (PW 4752932) FAILED PRIOR TO AD 2000-25-01 INTERVAL. (GL13200409283)

Source: SDR W1X2004F00000 · FAA SDRS
O · 1999-10-12 Matched by certificate designator
ATA 3213

AIRCRAFT PARKED. NOTICED LT WHEEL TILTED INBOARD AT TOP. BRAKE DISC HAD CONTACTED FORK. REMOVED WHEEL TO INVESTIGATE, FOUND AXLE HAD CRACKED HALF WAY AROUND. AIRCRAFT HAD FLOWN DAY BEFORE. CRACK SEEMED TO HAVE STARTED AT VERY BOTTOM. NOT BELIEVED TO BE CAUSED FROM BOUNCED LANDING. "STRESS CORROSION AND AGE" CRACK IS RIGHT IN SEAM WHERE BOSS AND BEARING AREAS NEED A CLOSE VISUAL INSPECTION.

Source: SDR 99ZZZX4057 · FAA SDRS