N406FJ

No registry detail on file · not in current registry

Operators of this aircraft

Who operated this tail, and how firmly we know it.

OperatorRolePeriodBasis
Ultimate JETCHARTERS, LLC (DTHA)Certificate holderMatched by certificate designator

Accident & incident history

No NTSB accidents or incidents on file for this aircraft.

Maintenance disclosures

J · 2014-03-17 Matched by certificate designator
ATA 7250

AFTER TAKEOFF, DURING CLIMB AT APPROXIMATELY 12,000 FEET THE LT ENGINE SN CD0072 SHUTDOWN WITH A VERY LOUD NOISE OCCURRING AND AT THE SAME TIME A VERY DESTINCT VIBRATION UNTIL THE ENGINE ROTAION STOPPED. IMMEDIATELY THE ACFT WAS RETURNED TO FIELD WITH NO INCIDENT. A PRELIMANARY BORESCOPE INSPECTION REVEALED DAMAGE TO THE FIRST, SECOND, THIRD, FOURTH AND FIFTH STAGE HIGH PRESSURE TURRBINE SECTIONS. IT HAS NOT BEEN DETERMINED AT THIS TIME THE SPECIFIC CAUSE OF THIS EVENT.

Source: SDR DTHA201403250001 · FAA SDRS
M H · 2006-02-27 Matched by certificate designator
ATA 3160

THE HONEYWELL DU-870 DISPLAY UNIT REFERENCED HEREIN FAILED JUST PRIOR TO TAKEOFF. THE SUSPECTED SPECIFIC COMPONENT FAILURE IS THE HIGH VOLTAGE POWER SUPPLY P/N:7018704-902 INSTALLED INSIDE THE CRT DISPLAY UNIT. FURTHER INSPECTION WILL BE REQUIRED TO VERIFY THE EXACT CAUSE OF DU FAILURE.

Source: SDR CMRR200602002 · FAA SDRS
H M · 2006-02-22 Matched by certificate designator
ATA 3160

+THE NR 1 PFD DU-870 DISPLAY UNIT REFERENCED HERE IN FAILED DURING GROUND OPERATIONS. THE SUSPECTED SPECIFIC COMPONENT FAILURE IS THE HIGH VOLTAGE POWER SUPPLY PN 7018704-902 INSTALLED INSIDE THE CRT DISPLAY UNIT. FURTHER INSPECTION WILL BE REQUIRED TO VERIFY THE EXACT CAUSE OF DU FAILURE.

Source: SDR CMRR200602003 · FAA SDRS
E · 2004-10-02 Matched by certificate designator
ATA 3244

VIBRATION IN NOSE LANDING GEAR DURING CLIMB. RTF. MX PERFORMED DETAILED INSPECTION OG NLG, NOSE GEAR BAY, NOSE GEAR DOORS, RADOME. NO DEFECTS NOTED, FOUND NLG TIRES OUT OF ROUND. REMOVED AND REPLACED LT & RT TIRES IAW DORNIER 328 JIC 32-41-01, LANDING GEAR INSPECTION JIC 32-11-00.

Source: SDR 04276406 · FAA SDRS
S · 2004-08-31 Matched by certificate designator
ATA 7532

ABORTED TAKEOFF DUE TO BLEED SOV FAILURE (HPSOV DID NOT OPEN AND LPSOV DID NOT OPEN ABOVE 80 PERCENT). MX INSPECTED BOTH ENGINES AND PERFORMED FUNCTIONAL CHECK FOR BOTH BSOV IAW JIC 71-03-03. NO FURTHER DISCREPANCIES AT THAT TIME.

Source: SDR 04244406 · FAA SDRS
L · 2004-08-22 Matched by certificate designator
ATA 3350

CENTER FLOOR EMERGENCY LIGHTS INOP. RECYCLED POWER. OPS CHECK GOOD.

Source: SDR 04235406 · FAA SDRS
O · 2003-10-02 Matched by certificate designator
ATA 3350

DURING INSPECTION THE EMERGENCY LIGHTS WERE FOUND INOPERATIVE. MAINTENANCE PERSONNEL FOUND THE FLIGHT ATTENDANTS EMERGENCY LIGHT SWITCH IN THE ON POSITION AND RECHARGED THE EMERGENCY BATTERIES VIA AIRCRAFT DC POWER. A SATISFACTORY OPERATIONAL CHECK WAS PERFORMED AND AIRCRAFT WAS RELEASED FOR CONTINUED SERVICE.

Source: SDR 03275406 · FAA SDRS
O · 2003-09-09 Matched by certificate designator
ATA 3350

DURING MAINTENANCE INSPECTION THE THIRD SECTION OF EMERGENCY TRACK LIGHTING WAS FOUND INOPERATIVE. MAINTENANCE PERSONNEL REMOVED AND REPLACED THE EMERGENCY POWER SUPPLY. A SATISFACTORY OPERATIONAL CHECK WAS PERFORMED AND AIRCRAFT WAS RELEASED FOR CONTINUED SERVICE.

Source: SDR 03252406 · FAA SDRS
O · 2003-08-07 Matched by certificate designator
ATA 3350

DURING MAINTENANCE INSPECTION THE NR 7 EMERGENCY BATTERY WAS DISCOVERED INOPERATIVE. MAINTENANCE PERSONNEL REMOVED AND REPLACED THE EMERGENCY POWER SUPPLY. A SATISFACTORY OPERATIONAL CHECK WAS PERFORMED AND AIRCRAFT WAS RELEASED FOR CONTINUED SERVICE.

Source: SDR 03219406 · FAA SDRS
O · 2003-05-06 Matched by certificate designator
ATA 3350

DURING PREFLIGHT INSPECTION, THE CREW REPORTED THAT THE EMERGENCY EXIT LIGHTS AT SEAT ROWS 9 AND 10 WERE INOPERATIVE. MAINTENANCE PERSONNEL RESET THE CIRCUIT BREAKER FOR THE EMERGENCY EXIT LIGHTS. AN OPERATIONAL CHECK WAS SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 03126406 · FAA SDRS
O · 2003-04-19 Matched by certificate designator
ATA 3397

DURING PREFLIGHT INSPECTION, THE CREW REPORTED THAT THE EMERGENCY FLOOR TRACK LIGHTS WERE INOPERATIVE FROM SEAT ROW 4 THROUGH 6. MAINTENANCE PERSONNEL SECURED A LOOSE CONNECTOR FOR THE EMERGENCY EXIT LIGHTS. AN OPERATIONAL CHECK WAS SATISFACTORY AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 03109406 · FAA SDRS
O · 2003-03-21 Matched by certificate designator
ATA 5246

DURING CLIMB, THE CREW REPORTED HEARING A LOUD BANG FOLLOWED BY AIRFRAME VIBRATION. THE FLIGHT RETURNED TO BOS AND LANDED WITHOUT FURTHER INCIDENT. MAINTENANCE PERSONNEL FOUND THAT THE OXYGEN SERVICE FAIRING PANEL HAD DEPARTED THE AIRCRAFT. THE PANEL WAS REPLACED AND THE AIRCRAFT WAS RETURNED TO SERVICE.

Source: SDR 03080406 · FAA SDRS